ENS 51775: Difference between revisions

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| event date = 03/07/2016 10:18 EST
| event date = 03/07/2016 10:18 EST
| last update date = 03/07/2016
| last update date = 03/07/2016
| title = Emergency Diesel Generators Auto-Started On Valid Actuation Signal
| title = Emergency Diesel Generators Auto-Started on Valid Actuation Signal
| event text = During Emergency Diesel Generator (EDG) surveillance testing, the normal 480V Bus 3A supply breaker tripped open.  All EDGs auto-started as per plant design.  During restoration of normal power to the 480V Buses, 23 EDG output breaker opened on overcurrent.  All plant systems responded as per design.  
| event text = During Emergency Diesel Generator (EDG) surveillance testing, the normal 480V Bus 3A supply breaker tripped open.  All EDGs auto-started as per plant design.  During restoration of normal power to the 480V Buses, 23 EDG output breaker opened on overcurrent.  All plant systems responded as per design.  
There was no loss of core cooling since steam generators were coupled with an operational RCP.  No other ESF [Engineered Safety Feature] equipment automatically started.  
There was no loss of core cooling since steam generators were coupled with an operational RCP.  No other ESF [Engineered Safety Feature] equipment automatically started.  

Latest revision as of 21:45, 1 March 2018

ENS 51775 +/-
Where
Indian Point Entergy icon.png
New York (NRC Region 1)
Reporting
10 CFR 50.72(b)(3)(iv)(A), System Actuation
LER: 05000247/LER-2016-002
Time - Person (Reporting Time:+1.9 h0.0792 days <br />0.0113 weeks <br />0.0026 months <br />)
Opened: Tom Oggeri
17:12 Mar 7, 2016
NRC Officer: Howie Crouch
Last Updated: Mar 7, 2016
51775 - NRC Website
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