ENS 54525: Difference between revisions

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| unit = 2
| unit = 2
| utype = GE-4, GE-4
| utype = GE-4, GE-4
| cfr = 10 CFR 50.72(b)(2)(iv)(B), 10 CFR 50.72(b)(3)(iv)(A)
| cfr = 10 CFR 50.72(b)(2)(iv)(B)
| emergency class = Non Emergency  
| emergency class = Non Emergency
| notification date = 02/14/2020 03:36
| notification date = 02/14/2020 03:36
| notification by = Tom Rydzewski
| notification by = Tom Rydzewski
Line 18: Line 18:
| title = Manual Reactor Scram Due to Rising Condenser Backpressure
| title = Manual Reactor Scram Due to Rising Condenser Backpressure
| event text = At 0025 EST on February 14, 2020, Susquehanna Steam Electric Station Unit 2 reactor was manually scrammed due to rising Main Condenser backpressure caused by a loss of the Unit 2 Offgas Recombiner.
| event text = At 0025 EST on February 14, 2020, Susquehanna Steam Electric Station Unit 2 reactor was manually scrammed due to rising Main Condenser backpressure caused by a loss of the Unit 2 Offgas Recombiner.
Unit 2 reactor was being operated at maximum facility output, approximately 98% RTP, when at 0012 EST, Unit 2 Recombiner 0C145 Panel Trouble and 2C198 HWC Panel Trouble alarms were received along with rising Main Condenser backpressure. Initial Main Condenser backpressure was 2.6 in HgA and was rising at approximately 0.3 HgA/min. A Recirc Lim 2 was inserted to lower reactor power and condenser backpressure continued to rise following the reduction in reactor power. A manual scram was inserted at 0025 EST by placing the Mode Switch to Shutdown when condenser backpressure rose to 6 in HgA. All control rods inserted. Reactor water level lowered to -30 inches causing Level 3 (+13 inches) isolation and partial (Division 2) Level 2 (-38 inches) isolation. No ECCS actuations occurred and RCIC initiated. The Operations crew subsequently maintained reactor water level at the normal operating band using Reactor Feed Water. No steam relief valves opened. The Reactor Recirculation Pumps remained in service.
Unit 2 reactor was being operated at maximum facility output, approximately 98% RTP, when at 0012 EST, Unit 2 Recombiner 0C145 Panel Trouble and 2C198 HWC Panel Trouble alarms were received along with rising Main Condenser backpressure. Initial Main Condenser backpressure was 2.6 in HgA and was rising at approximately 0.3 HgA/min. A Recirc Lim 2 was inserted to lower reactor power and condenser backpressure continued to rise following the reduction in reactor power. A manual scram was inserted at 0025 EST by placing the Mode Switch to Shutdown when condenser backpressure rose to 6 in HgA. All control rods inserted. Reactor water level lowered to -30 inches causing Level 3 (+13 inches) isolation and partial (Division 2) Level 2 (-38 inches) isolation. No ECCS actuations occurred and RCIC initiated. The Operations crew subsequently maintained reactor water level at the normal operating band using Reactor Feed Water. No steam relief valves opened. The Reactor Recirculation Pumps remained in service.
The reactor is currently stable in Mode 3. Investigation into the cause of the loss of Unit 2 recombiner is underway.
The reactor is currently stable in Mode 3. Investigation into the cause of the loss of Unit 2 recombiner is underway.
The NRC Senior Resident Inspector was notified. A voluntary notification to PEMA and press release will occur.
The NRC Senior Resident Inspector was notified. A voluntary notification to PEMA and press release will occur.
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2020/20200217en.html#en54525
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2020/20200217en.html#en54525
}}{{unit info
| Unit =  2
| type =
| Scram code =  M/R
| Reactor critical =  Y
| Initial power =  98
| Initial reactor mode =  Power Operation
| Current power =  0
| Current reactor mode =  Hot Shutdown
}}
}}


{{ENS-Nav}}[[Category:Power Reactor]]
{{ENS-Nav}}[[Category:Power Reactor]]

Latest revision as of 12:55, 15 January 2021

ENS 54525 +/-
Where
Susquehanna Talen Energy icon.png
Pennsylvania (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation
Time - Person (Reporting Time:+-1.82 h-0.0758 days <br />-0.0108 weeks <br />-0.00249 months <br />)
Opened: Tom Rydzewski
03:36 Feb 14, 2020
NRC Officer: Brian P. Smith
Last Updated: Feb 14, 2020
54525 - NRC Website
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