ML20202D089: Difference between revisions
StriderTol (talk | contribs) StriderTol Bot insert |
StriderTol (talk | contribs) StriderTol Bot change |
||
| Line 1: | Line 1: | ||
{{Adams | |||
| number = ML20202D089 | |||
| issue date = 12/01/1997 | |||
| title = Discusses Insp Repts 50-298/97-07 & 50-298/97-12 on 970629- 0809 & 970708-0905 & Forwards Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $110,000 | |||
| author name = Merschoff E | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) | |||
| addressee name = Horn G | |||
| addressee affiliation = NEBRASKA PUBLIC POWER DISTRICT | |||
| docket = 05000298 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-298-97-07, 50-298-97-12, 50-298-97-7, EA-97-424, NUDOCS 9712040142 | |||
| package number = ML20202D095 | |||
| document type = CORRESPONDENCE-LETTERS, OUTGOING CORRESPONDENCE | |||
| page count = 6 | |||
}} | |||
See also: [[see also::IR 05000298/1997007]] | |||
=Text= | |||
{{#Wiki_filter:, | |||
. | |||
f* "g uNITtostatts | |||
p I t, NUCLEAR HEGULATORY COMMISSION | |||
,I Rt oinN av | |||
{ | |||
% Gli RYAN PLAZA DRivt.sulT E 400 | |||
ARLINGioN.1f xAs 7f 0118064 | |||
3,***** December 1, 1997 | |||
EA 97 424 | |||
G. R. Horn, Senior Vice Precident | |||
of Energy Supply | |||
Nebraska Public Power District | |||
141415th Street | |||
Columbus, Nebraska 68001 | |||
SUBJECT: NOTICE OF VIOLATION AND PROPOSED IMPOSITION OF CIVIL PENALTY - | |||
$ 110,000 | |||
(NRC Inspection Report Nos. 50-298/97 07 and 9712) | |||
Dear Mr. Horn: | |||
This refers to the inspections conducted on June 29 through August 9,1997, and July 8 | |||
through September 5,1997, at your Cooper Nuclear Station f acility. The inspections were | |||
conducted to review the circumstances surrounding severalinstances of failures to | |||
identify, correct, or prevent recurrence of conditions adverse to quality. These issues were | |||
discussed with you during an exit briefing conducted on September 5,1997, and were | |||
documented in NRC Inspectinn Report Nos. 50 298/97 07 and 9712 dated September 4, | |||
and October 3,1997, respectively. A predecisional enforcement conference was held in | |||
the NRC Region IV office in Arlington, Texas, on October 17,1997, to discuss apparent | |||
violations identified during these inspections. | |||
Based on the information developed during the inspection and the information that you | |||
provided during the conference, the NRC has determined that violations of NRC < | |||
requirements occurred. These violations are cited in the enclosed Notice of Violation and | |||
Proposed imposition of Civil Penalty and the circumstances surrounding them were | |||
described in detailin the subject inspection reports. These violations involve several | |||
examples of failures to meet the requirements of 10 CFR Part 50, Appendix B, | |||
Criterion XVI. The first example involves a failure to recognize and correct instances | |||
whereby large volumes of water could cause both trains of the standby gas treatment | |||
system to be inoperable under certain circumstances. This problom htad been identified in | |||
1994 (reference LER 94 035 and NRC Inspection Report 90 26) when plant personnel | |||
recognized that backflow of water from Sump Z, under design basis accident conditions, | |||
could render both trains of the standby gas treatment system inorserabic. However, the | |||
corrective actions taken in 1994 were ineffective and the District identified this as an issue | |||
again in July 1997 (reference LER 97-010). | |||
The second example involves a failure to identify and correct significant blockage of | |||
Residual Heat Removal (RHR) Heat Exchanger B which reduced the heat transfer capability | |||
- below design requirements. After questioning by an NRC inspector, the District opened a | |||
condition adverse to qt,ality tracking number (CAO 97-0742) regardin0 the issue of mud , | |||
found in the heat exchanger. The CAO was closed after concluding that the heat | |||
^ 1 | |||
' 97 204 142 97 201 | |||
G PDR hh k, | |||
_. | |||
, | |||
. | |||
Nebraska Public Power District 2- | |||
exchanger had been operable, that the condition was not reportable, and (of concern to the | |||
NRC) that na condition adverse to nuclear safety or unexpected condition existed. Attor | |||
significant involvement from the NRC expressing concerns about the District's conclusion | |||
that the condition was not adverse to nuclear safety, several months later, the | |||
CAO 07 0742 and related CAQs were reopened to more thoroughly review the issues. | |||
The remaining seven violations also involve situations in which the District inadequately | |||
identified or corrected conditions adverse to quality. These violations occurred during | |||
similar timeframes and had similar causes. | |||
During the conference, your staff discussed severaiinitiatives that the District has | |||
implemented to improve its safety focus, especially in the area of problem identification | |||
and resolution. The District noted that an alert radwaste operator identified the issue | |||
involving the standby gas treatment system (the first example in the Notice). The NRC | |||
recognizes that the District identified this issue, but notes that this condition could have | |||
resulted in a common modo failure for a safety system, and was not corrected for over | |||
2 years. There also were prior missed opportunities to identify this problem. The situation | |||
involving RHR Heat Exchanger B (the second example in the Notice) is significant because | |||
your staff did not recognize a significant condition adverse to quality on a safety system, | |||
even af ter significant NRC involvement. The circumstances surrounding these two | |||
violations, as well as the other seven, indica'.e contemporary weaknesses in your staff's | |||
ability to recognize and correct problems. Therefore, these violations are classified in the | |||
aggregate in accordance with the " General Statement of Policy and Procedure for NRC | |||
Enforcement Actions" (Enforcement Policy), NUREG 1600, as a Severity Level lli problem. | |||
In accordance with the Enforcement Policy, a base civil penalty in the amount of $55,000 ; | |||
is considered for a Severity Level lll problem. Because your f acility has been the subject of | |||
escalated enforcement actions within the last 2 years,' the NRC considered whether credit | |||
was warranted for /dentification and Conective Action in accordance with the civil penalty | |||
assessment process in Section VI.B.2 of the Enforcement Policy. Given the circumstances | |||
surrounding the identification of the violation involving RHR Heat Exchanger 8, and the fact | |||
that NRC identified most of the violations, the NRC has determined that the District is not | |||
deserving of Identification credit. in evaluating whether credit is warranted for the | |||
Conectivo Action factor, the NRC considered whether the District's corrective actions will | |||
prevent recurrence of the specific violations, and are sufficiently comprehensive, given the | |||
significance and complexity of the violations, to prevent recurrence of violations with | |||
similar root causes. The District has been undertaking actions to improve personnel | |||
performance in problem identification and resolution. Examples of the District's actions | |||
include evaluating self identification rates, focusing on engineering teamwork, better | |||
' A Notice of Violation and Exercise of Discretion (EA97-017) was isst ed on June 25.1997 involving a | |||
Severity level til probletn telated to failurn to update the USAR and to perform adequate safety evaluations in | |||
accordance with 10 CFR $0.$9. The NRC exerdsed discretion and did not propose a civil penalty. | |||
.. _- | |||
_. - __ __ | |||
, | |||
. | |||
! | |||
i 1 | |||
i Nebraska Public Power District 3- - | |||
! | |||
focusing on conservative decision-making, emphasizing fundamentals such as procedure | |||
use and adherence, reducing challenges in the control room, enhancing training, | |||
conducting self assessments, and improving the tracking and trending of prngrams such as . | |||
CAQ/SCAQ. Many of these actiont were ongoing at the time of the violations, and little ! | |||
information was provided at the conference relative to additional actions, timetables, etc., | |||
that would result in improved performance. Given the District's past performance as well | |||
as the circumstances surrounding the violations, the NHC was unable to justify giving the- | |||
District credit for time Correct /va Act/on factor. | |||
Therefore, to emphasize the importance of prompt identification and comprehensive | |||
correction of violations, and in recognition of your previous escalated enforcement actions, | |||
I have been authorized, after consultation with the Director, Office of Enforcement, to | |||
issue the enclosed Notice of Violation and Proposed Imposition of Civil Penalty (Notice)in | |||
the amount of $110,000 for the Severity Levellli problem, | |||
it should be noted that, on the basis of information provided to the NRC during the~ | |||
conference, the apparent violation related to the Automatic Depressurization System relief | |||
valve accumulator low pressure alarm was not a violation. As such, this issue was not | |||
cited in the encinse.1 Notice. | |||
You are required to respond to this letter and should follow the instructions specified in the | |||
encloted Notice when preparing your response, in your response, you should document | |||
the specific actions taken and any additional actions you plan to prevent recurrence. The | |||
NRC will use your response, in part, to determine whether further enforcement action is | |||
necessary to ensure compliance with regulatory requirements, | |||
in accordance with 10 CFR 2,790 of the NRC's " Rules of Practice," a copy of this letter, e | |||
its enclosure, and your response will be placed in the NRC Public Document Room. | |||
Sincerely, | |||
Ellis W. Merse f | |||
Regional Ad , fiistrator | |||
Docket No. 50 298 | |||
License No. DPR-4G | |||
Enclosure: Notice of Violation and | |||
Proposed imposition of Civil Penalty | |||
cc w! Enclosure: (see next page) | |||
. _ . | |||
- . - . _. . . | |||
_ _ . | |||
, | |||
, t | |||
) | |||
, | |||
g | |||
f | |||
f | |||
r | |||
' i | |||
Nebraska Public Power District - 4I i | |||
i | |||
* | |||
l. | |||
i | |||
! | |||
cc w/ Enclosure:~ , | |||
" | |||
-John R. McPhail, General Counsel ' | |||
Nebraska Public Power District i | |||
P.O. Box 499 | |||
Columbus, Nebraska 68602 0499 | |||
, | |||
P. D. Graham, Vice President of : | |||
Nuclear Energy - 1 | |||
Nebraska Public Power District | |||
; P.O. Box 98 | |||
Brownville, Nebraska 68321 l | |||
! | |||
~ | |||
B. L. Houston, Nuclear Licensing | |||
and Safety Manager l | |||
Nebraska Public Power District | |||
P.O. Box 98 | |||
. | |||
Brownville, Nebraska 68321 * | |||
i | |||
Dr. William D. Leech | |||
MidAmerican Energy t | |||
4 | |||
007 Walnut Street ! | |||
P.O. Box 657 - | |||
Des Moines, Iowa 50303 0657 l | |||
1 | |||
Mrz Hon Stoddr d | |||
Lincoln Electric Gystem ' | |||
i 11th'and O Streets | |||
Lincoln, Nebraska 68508 i | |||
Randolph Wood, LJt ector | |||
Nebraska Departmt at of Environmental ' | |||
Ouality | |||
P.O. Box 98922 | |||
-Lincoln, Nebraska 68509 8922. ! | |||
Chairman.- | |||
! | |||
Nemaha County Board of Commissioners ! | |||
Nemaha County Courthouse * | |||
1824 N Street ' i | |||
Auburn, Nebraska 68305 ~ | |||
! | |||
E | |||
I | |||
i | |||
, | |||
4 | |||
* -a | |||
yy dyv~ f y g A -4 p -- y -- me. .-4+ fW-p s ah p ,,e v --g,. y- py pg.-- ,.9.,,q.9.q.spe=gew.-,_wgge--sty--g+4 --y-e w-.w-- -..-g m ---y.ep erw--*,r-,-,.i -uw- -- -- 7 v me n s +: mw- | |||
L s s ,- s u - +s . | |||
, | |||
! | |||
Nebraska Public Power District - | |||
5 | |||
Chery! Ro0ers, LLRW Program Manager | |||
Environmental Protection Section | |||
flebraska Department of Health | |||
301 Centennial Mall, South | |||
P.O. Box 95007 | |||
Lincoln, Nebraska 08509 5007 | |||
R. A. Kucera, Department Director | |||
of intergovernmental Ccoperation | |||
' | |||
Department of Natutal Resources | |||
P.O. Box 170 | |||
Jefferson City, Missouri 05102 | |||
Kantas Radiation Cortrol Program Director | |||
) | |||
^ | |||
:[ i | |||
os | |||
3/ | |||
lY | |||
Nebraska Public Power District 6- | |||
bec w/ Enclosure: | |||
PDR IE 14 | |||
.LPOR NUDOCS | |||
4 | |||
_SECY EC's: Rl, Ril, Rlli | |||
CA PA (0 2G4) | |||
EDO (017G21) OlG (T 5D28) | |||
DEDO (017G21) OE (0 7H5) | |||
OE:EAFile (0 7H5) 01 (0 3E4) | |||
OGC (015B18) OGC (015B18) | |||
NRR (012G18) NRR/ADP (012G18) | |||
. NRR PROJECT MANAGER OC/DAF (T 9E10) ~ | |||
OC/LFDCB (T 9E10) AEOD (T-4018) | |||
RA Reading File GSanborn EAFile | |||
RIV Files MIS Coordinator | |||
BHenderson, PAO CHackney, RSLO | |||
E MAIL DISTRIBUTION: | |||
OEMAIL JDyer (JED2) | |||
TPGwynn (TPG) EMerschoff | |||
WBrown (WLB) ECollins (EEC) | |||
GSanborn (GFS) GMVasquez (GMV) | |||
BHenderson (BWH) MHammond (MFH2) | |||
CHackney (CAH) DKunihiro (DMK1) | |||
AHowell (ATH) DChamberlain (DDC) | |||
KPerkins (KEP) DRP Branch Chief | |||
KBrockman (KEB) MMiller, SRI (MHM) | |||
DOCUMENT NAME: G:\EA\ DRAFT \EA97424.DFT | |||
To receive cp of document, irdcate irt box: "C" = Copy wtthout enclosures *E" = Copy wRh enclosures *N" = No copy | |||
ES ffgfig C:DRP/C D:DR1 D:DRP _f) RC L/& | |||
W PGwynn )'7 WLBro@ V | |||
w | |||
MVasquez ECollins 6Im fel AHo#(I | |||
g: | |||
JDyeN | |||
p_,, m | |||
EMersp46!V/ | |||
m | |||
JLibbernian M b | |||
1145/97 - | |||
11/ /97 N116.N97/ " | |||
OFFICIAL RECORD COPY | |||
.- . - -- - -. ,. . . . - . - . . . . - . . - - | |||
}} | |||
Revision as of 03:47, 15 December 2020
| ML20202D089 | |
| Person / Time | |
|---|---|
| Site: | Cooper |
| Issue date: | 12/01/1997 |
| From: | Merschoff E NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | Horn G NEBRASKA PUBLIC POWER DISTRICT |
| Shared Package | |
| ML20202D095 | List: |
| References | |
| 50-298-97-07, 50-298-97-12, 50-298-97-7, EA-97-424, NUDOCS 9712040142 | |
| Download: ML20202D089 (6) | |
See also: IR 05000298/1997007
Text
,
.
f* "g uNITtostatts
p I t, NUCLEAR HEGULATORY COMMISSION
,I Rt oinN av
{
% Gli RYAN PLAZA DRivt.sulT E 400
ARLINGioN.1f xAs 7f 0118064
3,***** December 1, 1997
EA 97 424
G. R. Horn, Senior Vice Precident
of Energy Supply
Nebraska Public Power District
141415th Street
Columbus, Nebraska 68001
SUBJECT: NOTICE OF VIOLATION AND PROPOSED IMPOSITION OF CIVIL PENALTY -
$ 110,000
(NRC Inspection Report Nos. 50-298/97 07 and 9712)
Dear Mr. Horn:
This refers to the inspections conducted on June 29 through August 9,1997, and July 8
through September 5,1997, at your Cooper Nuclear Station f acility. The inspections were
conducted to review the circumstances surrounding severalinstances of failures to
identify, correct, or prevent recurrence of conditions adverse to quality. These issues were
discussed with you during an exit briefing conducted on September 5,1997, and were
documented in NRC Inspectinn Report Nos. 50 298/97 07 and 9712 dated September 4,
and October 3,1997, respectively. A predecisional enforcement conference was held in
the NRC Region IV office in Arlington, Texas, on October 17,1997, to discuss apparent
violations identified during these inspections.
Based on the information developed during the inspection and the information that you
provided during the conference, the NRC has determined that violations of NRC <
requirements occurred. These violations are cited in the enclosed Notice of Violation and
Proposed imposition of Civil Penalty and the circumstances surrounding them were
described in detailin the subject inspection reports. These violations involve several
examples of failures to meet the requirements of 10 CFR Part 50, Appendix B,
Criterion XVI. The first example involves a failure to recognize and correct instances
whereby large volumes of water could cause both trains of the standby gas treatment
system to be inoperable under certain circumstances. This problom htad been identified in
1994 (reference LER 94 035 and NRC Inspection Report 90 26) when plant personnel
recognized that backflow of water from Sump Z, under design basis accident conditions,
could render both trains of the standby gas treatment system inorserabic. However, the
corrective actions taken in 1994 were ineffective and the District identified this as an issue
again in July 1997 (reference LER 97-010).
The second example involves a failure to identify and correct significant blockage of
Residual Heat Removal (RHR) Heat Exchanger B which reduced the heat transfer capability
- below design requirements. After questioning by an NRC inspector, the District opened a
condition adverse to qt,ality tracking number (CAO 97-0742) regardin0 the issue of mud ,
found in the heat exchanger. The CAO was closed after concluding that the heat
^ 1
' 97 204 142 97 201
G PDR hh k,
_.
,
.
Nebraska Public Power District 2-
exchanger had been operable, that the condition was not reportable, and (of concern to the
NRC) that na condition adverse to nuclear safety or unexpected condition existed. Attor
significant involvement from the NRC expressing concerns about the District's conclusion
that the condition was not adverse to nuclear safety, several months later, the
CAO 07 0742 and related CAQs were reopened to more thoroughly review the issues.
The remaining seven violations also involve situations in which the District inadequately
identified or corrected conditions adverse to quality. These violations occurred during
similar timeframes and had similar causes.
During the conference, your staff discussed severaiinitiatives that the District has
implemented to improve its safety focus, especially in the area of problem identification
and resolution. The District noted that an alert radwaste operator identified the issue
involving the standby gas treatment system (the first example in the Notice). The NRC
recognizes that the District identified this issue, but notes that this condition could have
resulted in a common modo failure for a safety system, and was not corrected for over
2 years. There also were prior missed opportunities to identify this problem. The situation
involving RHR Heat Exchanger B (the second example in the Notice) is significant because
your staff did not recognize a significant condition adverse to quality on a safety system,
even af ter significant NRC involvement. The circumstances surrounding these two
violations, as well as the other seven, indica'.e contemporary weaknesses in your staff's
ability to recognize and correct problems. Therefore, these violations are classified in the
aggregate in accordance with the " General Statement of Policy and Procedure for NRC
Enforcement Actions" (Enforcement Policy), NUREG 1600, as a Severity Level lli problem.
In accordance with the Enforcement Policy, a base civil penalty in the amount of $55,000 ;
is considered for a Severity Level lll problem. Because your f acility has been the subject of
escalated enforcement actions within the last 2 years,' the NRC considered whether credit
was warranted for /dentification and Conective Action in accordance with the civil penalty
assessment process in Section VI.B.2 of the Enforcement Policy. Given the circumstances
surrounding the identification of the violation involving RHR Heat Exchanger 8, and the fact
that NRC identified most of the violations, the NRC has determined that the District is not
deserving of Identification credit. in evaluating whether credit is warranted for the
Conectivo Action factor, the NRC considered whether the District's corrective actions will
prevent recurrence of the specific violations, and are sufficiently comprehensive, given the
significance and complexity of the violations, to prevent recurrence of violations with
similar root causes. The District has been undertaking actions to improve personnel
performance in problem identification and resolution. Examples of the District's actions
include evaluating self identification rates, focusing on engineering teamwork, better
' A Notice of Violation and Exercise of Discretion (EA97-017) was isst ed on June 25.1997 involving a
Severity level til probletn telated to failurn to update the USAR and to perform adequate safety evaluations in
accordance with 10 CFR $0.$9. The NRC exerdsed discretion and did not propose a civil penalty.
.. _-
_. - __ __
,
.
!
i 1
i Nebraska Public Power District 3- -
!
focusing on conservative decision-making, emphasizing fundamentals such as procedure
use and adherence, reducing challenges in the control room, enhancing training,
conducting self assessments, and improving the tracking and trending of prngrams such as .
CAQ/SCAQ. Many of these actiont were ongoing at the time of the violations, and little !
information was provided at the conference relative to additional actions, timetables, etc.,
that would result in improved performance. Given the District's past performance as well
as the circumstances surrounding the violations, the NHC was unable to justify giving the-
District credit for time Correct /va Act/on factor.
Therefore, to emphasize the importance of prompt identification and comprehensive
correction of violations, and in recognition of your previous escalated enforcement actions,
I have been authorized, after consultation with the Director, Office of Enforcement, to
issue the enclosed Notice of Violation and Proposed Imposition of Civil Penalty (Notice)in
the amount of $110,000 for the Severity Levellli problem,
it should be noted that, on the basis of information provided to the NRC during the~
conference, the apparent violation related to the Automatic Depressurization System relief
valve accumulator low pressure alarm was not a violation. As such, this issue was not
cited in the encinse.1 Notice.
You are required to respond to this letter and should follow the instructions specified in the
encloted Notice when preparing your response, in your response, you should document
the specific actions taken and any additional actions you plan to prevent recurrence. The
NRC will use your response, in part, to determine whether further enforcement action is
necessary to ensure compliance with regulatory requirements,
in accordance with 10 CFR 2,790 of the NRC's " Rules of Practice," a copy of this letter, e
its enclosure, and your response will be placed in the NRC Public Document Room.
Sincerely,
Ellis W. Merse f
Regional Ad , fiistrator
Docket No. 50 298
License No. DPR-4G
Enclosure: Notice of Violation and
Proposed imposition of Civil Penalty
cc w! Enclosure: (see next page)
. _ .
- . - . _. . .
_ _ .
,
, t
)
,
g
f
f
r
' i
Nebraska Public Power District - 4I i
i
l.
i
!
cc w/ Enclosure:~ ,
"
-John R. McPhail, General Counsel '
Nebraska Public Power District i
P.O. Box 499
Columbus, Nebraska 68602 0499
,
P. D. Graham, Vice President of :
Nuclear Energy - 1
Nebraska Public Power District
- P.O. Box 98
Brownville, Nebraska 68321 l
!
~
B. L. Houston, Nuclear Licensing
and Safety Manager l
Nebraska Public Power District
P.O. Box 98
.
Brownville, Nebraska 68321 *
i
Dr. William D. Leech
MidAmerican Energy t
4
007 Walnut Street !
P.O. Box 657 -
Des Moines, Iowa 50303 0657 l
1
Mrz Hon Stoddr d
Lincoln Electric Gystem '
i 11th'and O Streets
Lincoln, Nebraska 68508 i
Randolph Wood, LJt ector
Nebraska Departmt at of Environmental '
Ouality
P.O. Box 98922
-Lincoln, Nebraska 68509 8922. !
Chairman.-
!
Nemaha County Board of Commissioners !
Nemaha County Courthouse *
1824 N Street ' i
Auburn, Nebraska 68305 ~
!
E
I
i
,
4
- -a
yy dyv~ f y g A -4 p -- y -- me. .-4+ fW-p s ah p ,,e v --g,. y- py pg.-- ,.9.,,q.9.q.spe=gew.-,_wgge--sty--g+4 --y-e w-.w-- -..-g m ---y.ep erw--*,r-,-,.i -uw- -- -- 7 v me n s +: mw-
L s s ,- s u - +s .
,
!
Nebraska Public Power District -
5
Chery! Ro0ers, LLRW Program Manager
Environmental Protection Section
flebraska Department of Health
301 Centennial Mall, South
P.O. Box 95007
Lincoln, Nebraska 08509 5007
R. A. Kucera, Department Director
of intergovernmental Ccoperation
'
Department of Natutal Resources
P.O. Box 170
Jefferson City, Missouri 05102
Kantas Radiation Cortrol Program Director
)
^
- [ i
os
3/
lY
Nebraska Public Power District 6-
bec w/ Enclosure:
.LPOR NUDOCS
4
_SECY EC's: Rl, Ril, Rlli
CA PA (0 2G4)
EDO (017G21) OlG (T 5D28)
DEDO (017G21) OE (0 7H5)
OE:EAFile (0 7H5) 01 (0 3E4)
NRR (012G18) NRR/ADP (012G18)
. NRR PROJECT MANAGER OC/DAF (T 9E10) ~
OC/LFDCB (T 9E10) AEOD (T-4018)
RA Reading File GSanborn EAFile
RIV Files MIS Coordinator
BHenderson, PAO CHackney, RSLO
E MAIL DISTRIBUTION:
OEMAIL JDyer (JED2)
TPGwynn (TPG) EMerschoff
WBrown (WLB) ECollins (EEC)
GSanborn (GFS) GMVasquez (GMV)
BHenderson (BWH) MHammond (MFH2)
CHackney (CAH) DKunihiro (DMK1)
AHowell (ATH) DChamberlain (DDC)
KPerkins (KEP) DRP Branch Chief
KBrockman (KEB) MMiller, SRI (MHM)
DOCUMENT NAME: G:\EA\ DRAFT \EA97424.DFT
To receive cp of document, irdcate irt box: "C" = Copy wtthout enclosures *E" = Copy wRh enclosures *N" = No copy
ES ffgfig C:DRP/C D:DR1 D:DRP _f) RC L/&
W PGwynn )'7 WLBro@ V
w
MVasquez ECollins 6Im fel AHo#(I
g:
JDyeN
p_,, m
EMersp46!V/
m
JLibbernian M b
1145/97 -
11/ /97 N116.N97/ "
OFFICIAL RECORD COPY
.- . - -- - -. ,. . . . - . - . . . . - . . - -