ML20133P628: Difference between revisions

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{{Adams
#REDIRECT [[IR 05000524/2006028]]
| number = ML20133P628
| issue date = 07/22/1985
| title = Notice of Violation from Insp on 850524-0628
| author name =
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee name =
| addressee affiliation =
| docket = 05000321, 05000366
| license number =
| contact person =
| document report number = 50-366-85-18, NUDOCS 8508140399
| package number = ML20133P623
| document type = NOTICE OF VIOLATION OF A REGULATION, TEXT-INSPECTION & AUDIT & I&E CIRCULARS
| page count = 1
}}
See also: [[see also::IR 05000524/2006028]]
 
=Text=
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    ,
                                                ENCLOSURE
                                          NOTICE OF VIOLATION
                                                                                                    l
                                                                                                    '
        Georgia Power Company                                          Docket No.  50-366
        Hatch 2                                                        License No. NPF-5
        The following violation was identified during an inspection conducted on
        May 24 - June 28, 1985. The Severity Level was assigned in accordance with the
        NRC Enforcement Policy (10 CFR Part 2, Appendix C).
              Technical Specification 6.8.1 requires that procedures shall be established,
              implemented and maintained covering safety-related activities.
              Contrary to the above, Procedure HNP-2-1500, Primary Containment Atmospheric
              Control System, was not properly implemented in that on May 24, 1985, two
              nitrogen makeup valves were found out of the position required by Data
              Package 1 of HNP-2-1500. The position of these valves, being shut instead
              of open, caused a SCRAM when the air was secured to the Main Steam Isolation
              valves in preparation for inerting the drywell.
              This is a Seversty Level IV violation (Supplement I).
        Pursuant to 10 CFR 2.201, you are required to submit to this office within 30
        days of the date of this Notice, a written statement or explanation in reply,
        including: (1) admission or denial of the alleged violation; (2) the reasons
        for the violation if admitted; (3) the corrective steps which have been taken
        and the results achieved; (4) corrective steps which will be taken to avoid
        further violations; and (5) the date when full compliance will be achieved.
        Security or safeguards information should be submitted as an enclosure to
'
        facilitate withholding it from public disclosure as required by 10 CFR 2.790(d)
        or 10 CFR 73.21.
        Date:    M
                                  8508140399 850722
                                  PDR    ADOCK 05000321
                                  O                  PDR
                                ._    _                  _          _
                                                                                            ._.
}}

Latest revision as of 20:48, 25 September 2020