ML19275A222: Difference between revisions

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| number = ML19275A231
| number = ML19275A231
| issue date = 09/27/1979
| issue date = 09/27/1979
| title = Forwards LERs 79-100/03L-0 & 79-105/03L-0
| title = LER 79-105/03L-0:on 790828,during Testing of Containment Particulate Monitor,Power Fuses Blew When Sample Pump Was Placed in Stop Position Causing Particulate & Gas Monitor to Be Inoperable.Caused by Shorted Valve K5
| author name = Cartwright W
| author name = Cartwright W
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
Line 21: Line 21:
| number = ML19275A227
| number = ML19275A227
| issue date = 09/27/1979
| issue date = 09/27/1979
| title = Forwards LERs 79-100/03L-0 & 79-105/03L-0
| title = LER 79-100/03L-0:on 790903,during Steady State Operation, Greater than 12-step Disagreement Was Noted Between Rod Position Indicator D-10 & Group Demand Indication.Caused by Voltage Drift in Signal Conditioning Card
| author name = Cartwright W
| author name = Cartwright W
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)

Latest revision as of 07:33, 23 January 2020

Forwards LERs 79-100/03L-0 & 79-105/03L-0
Date released: 10/16/2019 Download: ML19275A222


LER 79-105/03L-0:on 790828,during Testing of Containment Particulate Monitor,Power Fuses Blew When Sample Pump Was Placed in Stop Position Causing Particulate & Gas Monitor to Be Inoperable.Caused by Shorted Valve K5
ML19275A231
Person / Time
Site: North Anna Dominion icon.png
Issue date: 09/27/1979
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
Download: ML19275A231 (2)
LER 79-100/03L-0:on 790903,during Steady State Operation, Greater than 12-step Disagreement Was Noted Between Rod Position Indicator D-10 & Group Demand Indication.Caused by Voltage Drift in Signal Conditioning Card
ML19275A227
Person / Time
Site: North Anna Dominion icon.png
Issue date: 09/27/1979
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
Download: ML19275A227 (2)
Forwards LERs 79-100/03L-0 & 79-105/03L-0
ML19275A221
Person / Time
Site: North Anna Dominion icon.png
Issue date: 09/27/1979
From: Stallings C
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To: OREILLY J P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
Download: ML19275A221 (1)