ML15236A356: Difference between revisions

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{{Adams
#REDIRECT [[DCL-15-102, 10 CFR 71.95 Report Regarding Energy Solutions' Model 8-120B Shipping Cask]]
| number = ML15236A356
| issue date = 08/24/2015
| title = 10 CFR 71.95 Report Regarding Energy Solutions' Model 8-120B Shipping Cask
| author name = Allen B S
| author affiliation = Pacific Gas & Electric Co
| addressee name = Lombard M
| addressee affiliation = NRC/Document Control Desk, NRC/NMSS/DSFM
| docket = 05000275, 05000323, 07109168
| license number = DPR-080, DPR-082
| contact person =
| case reference number = DCL-15-102
| document type = Letter, Report, Miscellaneous
| page count = 14
}}
 
=Text=
{{#Wiki_filter:Pacific Gas and Electric Company August 24, 2015 PG&E Letter DCL-15-102 Barry S. Allen Vice President, Nuclear Services Diablo Canyon Power Plant Mail Code 104/6 P. 0. Box 56 Avila Beach; CA 93424 805.545.4888 Internal:
691.4888 Fax: 805.545.6445 Mr. Mark Lombard, Director 10 CFR 71.95 Division of Spent Fuel Storage and Transportation Office of Nuclear Material Safety and Safeguards U.S. Nuclear Regulatory Commission Washington DC ATTN: Document Control Desk Docket No. 50-275, OL-DPR-80 Docket No. 50-323, OL-DPR-82 Diablo Canyon, Units 1 and 2 Diablo Canyon Power Plant 10 CFR 71.95 Report Regarding Energy Solutions' Model 8-1208 Shipping Cask
 
==Dear Mr. Lombard:==
Pacific Gas and Electric Company (PG&E) hereby submits the enclosed report pursuant to 10 CFR 71.95(a)(3) regarding instances in which the conditions of approval in Certificate of Compliance Number 9168, for the EnergySo/utions' Model 8-1208 shipping cask, were not met when making radwaste shipments from the Diablo Canyon Power Plant. Enclosure 1 contains the 10 CFR 71.95 Report, prepared by PG&E, regarding the EnergySolutions' Model 8-1208 Shipping Cask. Enclosure 2 contains a copy of the Customer Notification letter and associated 10 CFR 71.95 Report, provided by Energy Solutions, regarding the Energy Solutions' Model 8-1208 Shipping Cask. PG&E makes no new or revised regulatory commitments (as defined by NEI 99-04) in this report. PG&E will implement corrective actions in accordance with the site Corrective Action Program. If you have any questions concerning this submittal, please contact Mr. Hossein Hamzehee at 805-545-4720, or Mr. Timothy Irving at 805-545-3015.
Sincerely, Barry S. "'en A member of the STARS (Strategic Teaming and Resource Sharing) Alliance
* Comanche Peak
* Diablo Canyon
* Palo Verde
* Wolf Creek m Document Control Desk August 24, 2015 Page 2 dqmg/6192/50708969 Enclosures cc/enc: . Marc L. Dapas, Regional Administrator Mark Lewis, EnergySolutions LLC Siva Lingam, NRC Project Manager PG&E Letter DCL-15-102 John P. Reynoso, Acting Senior Resident Inspector IN PO Diablo Distribution 2
Diablo Canyon Power Plant 10 CFR 71.95 Report Regarding Enclosure 1 PG&E Letter DCL-15-1 02 Energy Solutions' Model 8-1208 Shipping Cask 1. Abstract:
This report provides information required by 10 CFR 71.95, "Reports," for instances in which the conditions of approval in Certificate of Compliance (CoC) Number 9168, issued to EnergySolutions, LLC (EnergySo/utions), for its Model 8-1208 shipping cask, were not observed in making radioactive waste shipments.
The circumstances described in this report apply specifically to Pacific Gas and Electric Company's (PG&E's) Diablo Canyon Power Plant (DCPP). On June 24, 2015, DCPP identified 4 shipments that failed to comply with the recently interpreted, vent port leak test requirements associated with the subject CoC. Between 2013 and 2015, DCPP made 4 Type-8 shipments with this cask and removed the cask vent port plug each time. After replacing the vent port plug, DCPP leak tested the vent port in accordance with PG&E's Maintenance Procedure (MP) M-50.23, "Loading Pre-Loaded Liners Into The Chem-Nuclear CNS 8-1208 Radioactive Waste Shipping Cask," and the vendor's cask procedure.
There were no components or system failures that contributed to this event. 2. Narrative Description of Event The Model 8-1208 shipping cask is a cylindrical, carbon steel, lead-shielded package designed for the transport of radioactive waste containers.
The cask has both a opening primary lid and a smaller, inner-secondary lid. Test ports for leak testing these package lids are located between the twin 0-ring seals for both the primary and secondary lids. Each package has a vent and optional drain port which can be used to inert the cask cavity with nitrogen, or vent pressure within the containment cavity which may be generated during transport, prior to lid removal. The vent hole in the primary lid is sealed with a removable plug and silicone gasket. There are no complex operational requirements associated with the package. An air test rig with a pressure gauge is engaged above each of the test ports or vent hole to pressurize the cavity. During leak testing, the air supply is isolated and the gauge is monitored to ensure a pressure drop of no more than 0.05 pounds-per-square-inch over the 15 minute test period. DCPP procedure MP M-50.23, "Loading Pre-Loaded Liners into EnergySo/utions' 8-1208 Radwaste Shipping Cask," specified a 15-minute hold time for the pre-shipment leak test of the cask vent port, which was successfully completed for all 4 shipments.
However, DCPP now recognizes the test manifold gasket may have reduced test sensitivity below the value required for the vent port plug. Therefore, the conditions of approval in the CoC were not met when making these shipments.
This failure was identified on June 24, 2015, by a letter from Energy Solutions. 
: i. Status of inoperable components or systems Enclosure 1 PG&E Letter DCL-15-1 02 Not applicable.
None of the components or systems were inoperable.
ii. Dates and approximate times of occurrences The testing for these 4 shipments occurred between July 2014 and April2015.
iii. Cause of Error Test manifold gasket blocked the full air pressure on the vent port plug. iv. Failure Mode, Mechanism, and Effects Not applicable.
: v. Systems or Secondary Functions Affected Not applicable.
vi. Method of Discovery of the Error During an industry audit of Energy Solutions, a concern was raised that the test manifold gasket could reduce the preshipment leak test sensitivity below the require value for the vent port plug. vii. Discussion of Cause The test manifold gasket, when compressed, may deform and cover the vent port plug reducing the sensitivity of the leak test. viii. Manufacturer and Model Number Manufacturer:
EnergySolutions, LLC Model Number: 8-1208 ix. Quantities and chemical and physical form(s) of the package contents These shipments were all Physical/Chemical form Solid/Oxides on resin and their quantities are as shown in the table below. Date Quantity (Curies) RWS-14-001 07/16/14 49.7 2 Date RWS-14-002 07/25/14 RWS-15-002 03/25/15 RWS-15-003 04/01/15 3. Assessment of Safety Consequences Enclosure 1 PG&E Letter DCL-15-1 02 Quantity (Curies) 48.2 82.5 28.5 Based on the safety evaluation conducted by Energy Solutions, there is no safety consequence of performing the preshipment leak test of the Model 8-120B cask vent port plug. 4. Corrective Actions PG&E is reviewing the need to use this cask in the future. If used in the future, DCPP will revise DCPP procedure MP M-50.23, "Loading Pre-Loaded Liners into EnergySolutions' 8-120B Radwaste Shipping Cask," prior to using it. EnergySo/utions revised Procedure TR-TP-002 to replace the test manifold gasket with a different type. 5. Previous Similar Events In 2013, PG&E submitted a report on an inadequate leak test time for the vent port plug on this model cask (PG&E Letter DCL-13-094, "Diablo Canyon Power Plant and Humboldt Bay Power Plant 10 CFR 71.95 Reports Regarding Energy Solutions' Model 8-120B Shipping Cask," dated September 30, 2013). 6. Contact for Additional Information Clint Miller, DCPP Radwaste Engineer, 805-545-4582.
: 7. Extent of Exposure of Individuals to Radiation or Radioactive Materials The vent port was adequately sealed, and there was no additional exposure of individuals to radiation or radioactive material as the result of the deficient leak test. 3 Enclosure 2 PG&E Letter DCL-15-1 02 Copy of Energy Solutions Customer Notification Letter and 10 CFR 71.95 Report on the 8-1208 Cask June 24, 2015 ES-CD-0-2015-002
 
==Dear Valued Customer:==
 
On Monday June 1, 2015, an 8-1208 cask user identified a concern that the neoprene gasket could potentially affect the integrity of the vent port seal pre-shipment leak test. In response, EnergySolutions performed a series of tests that confirmed that the neoprene gasket can constrict on the head of the vent port plug cap screw when it is compressed by the manifold, resulting in a reduction of the test sensitivity.
The amount of reduction of the test sensitivity cannot be determined for any particular shipment due to several reasons. It is uncertain whether, or by how much, the sensitivity of the vent port pre-shipment leak tests was reduced because: 1) Use of the gasket was optional-the gasket may," or may not have been in place for the tests, and 2) The force with which the gasket was compressed during testing is unknown, so it is uncertain if it caused the gasket to constrict onto the head of the vent port cap screw. The gasket may have been used on as many as 100 shipments by EnergySo!utions or its customers with Energy Solutions as the licensee from September 2013 through June 2015. It was September 2013 when newly designed lids were installed.
The condition was determined not to have significant safety consequence becavse the seals receive periodic helium leak testing as required by the SAR, the vent ports are rarely opened, there is a margin of conservatism of approximately a factor of 9 on the prescribed vent port leak rate test, and there have been no observations of contamination around the vent port openings that would suggest leakage. There will be no further tests made using the gaskets since EnergySolutions has replaced all of the subject gaskets with a modified version that does not have the to reduce the test sensitivity.
Energy Solutions filed the attached report with the NRC containing the information required by 10 CFR 71.95 on June 24, 2015. In the report, EnergySolutions describes the cause of the discrepancy and provides information that supports that there is no safety significance.
We expect that the information required for individual users to make their own notifications is contained in this report. Reference to this report in individual user reports would be appropriate if you so choose. We sincerely apologize for any inconvenience this issue may have caused within in your organization.
Our corrective actions as a result of this issue are intended to prevent recurrence of similar issues and to ensure the highest quality of products and services that we provide. For additional details, please contact Aleksandr Gelfand at axgelfond@energysolutions.com or 803-591-9074. Sincerely, MarkS. Lewis General Manager, Cask Logistics Logistics, Processing and Disposal EnergySo!utions, LLC
 
==Attachment:==
 
Letter and Report to NRC on 8-1208 Cask cc: Dan Shum Aleksandr Gelfand 740 Osborn Road. Barnwell, South Carolina 29812 803.259.1781.
Fax 803.259.1477 I I l I l I t I I l I I f I f f I I r I I I I i i ! I I I l-i i I I t r I I I l I l l I ' i ! l l I t 
 
June 24, 2015 Mark .Lorn bard, Director Division of Spent Fuel*Management Office of Nuclear Material Safety and Safeguards U.S. Nuclear Regulatory Commission Washington DC 20555-0001 A1TN: Document Control Desk
 
==Subject:==
10 CFR 71.95 Report on the Cask \
 
==Dear Mr. Lombard:==
CD15-0149 EnefgySo!utions hereby submits the attached report providing the information required by 10 CFR 71.95(a)(3) for instances in which the conditions of approval in the Certificate of
* Compliance for the 8-120B Cask (Certificate of Compliance
#91.68) may not have been observed in making certain shipments.
The circumstances desc.dbed in this report are applicable to approximately 235 shipments made by BnergySolutions as a licensee and user of the 8-120B cask over a 21 month period. If you have any questions regarding this please contact me at 801-649-2109.
Daniel B. Shrum Senior Vice President, Regulatory Affairs EnergySolutions LLC Dan Shrum Jun 24 2015 2:58PM Attachment; Fa:ilure to Obse.rVe Certificate of Compliance Conditions for the 8-120B Vent Port Leak Pre-Shipment Leak Test cc: Michele Sampson, Chief Spent Fuel Licensing Branch Pierre M. Saverot Licensing Branch 299 So.uth Main Street, Suite 1700 *Salt Lake City, Utah 84ii1 (801} 649*2000
* Fax: (801) 880-2879
* www.energysolutions;com l r j l I I f 1 I I I I I ! I i I I ! I I I I i ;--1 I l t I i r J I l ! l I l I L l I 1 l t I r 
 
Failure to Observe Certificate of Compliance Conditions for the 8-120B Vent Port Pre-Shipment Leak Test June 24, 2015 1) Abstract Durfug the vent port seal pre-shipment leak rate test, a neoprene gasket that was added under the test manifold may have reduced the test sensitivity below the requ.ired value. The test manifold and gasket are not licensed packaging components.
The gasket was added to the test manifold on some or all shipments to more reliably seal the manifold, saving test time and reducing personnel exposures. The amount of reduction ofthe test sensitivity cannot be determined for any particular shipment due to several reasons as discussed below. The gasket may have been used on as many as 100 shipments by EnergySolutions as the licensee :fi*om September 2013 through June 2015. The condition was detennined not to have significant safety consequence because the seals receive periodic helium leak testing as required by the SAR, the vent ports are only opened rarely, there is a margin of conservatism of approximately a factor of 9 on the prescribed vent port leak rate test, and there have been no observations of contamination around the vent port openings that would suggest leakage. There will be no further tests made using the gaskets since EnergySolutions has replaced all of the subject gaskets with a modified version that does not have the potential to reduce the test sensitivity.
It is uncertain whether, or by how much, the sensitivity
.ofthe vent p01t pre-shipment leak tests was reduced because: 1) Use of the gasket was optional-the gasket may, or may not have been in place for the tests, and 2) The force with which the gasket was compressed during testing is unknown, so it is uncertain if caused the gasket to constrict onto the head of the vent p01t cap screw. 2) Narrative Description of the Event a) Status of Component$
All of the 8-120B packaging components are operating normally.
The neoprene gaskets that caused the event have all be removed from service and replaced with a new manifold gasket, as discussed in (4) below. b) Dates of Occurrences From September 2013, when pre-shipment leak tests were first performed using the neoprene gasket, to approximately 1 00 shipments were made by EnergySolutions as the licensee.
Most of these shipments used the neoprene gasket to perfo1m the pre-. shipment leak rate test of the vent port.
* 2 
---------------ENERGYSOLUTIONs-----------------
c) Cau.se of Error New 8-120B lids went into service in September 2013. It was found that the manifold sometimes had problems sealing w*ith the vent port on these new lids.
personnel found that adding an extra neoprene gasket helped to reduce the false test failures.
Since the pre-shipment leak rate test is performed in a radiation environment, false fallures are undesirable because they increase the persoimel exposure.
The pers_onnel did not realize that the gaskets had the to reduce test sensitivity.
Attachment 1 has a detailed description of the test configuration.
d) Failure Mode, Mechanism, and Effects The neoprene gasket can constrict on the head of the vent port plug cap screw when it is compressed by the bottom end of the test manifold stinger, which could reduce the sensitivity of the pre-shipment ieak test. Consequently, the vent port pre-shipment leak tests perfonned using the neoprene gasket may not have provided the required test sensitivity of lx 1 o-3 ref-cm 3 I sec. e) Systems or Secondary Functions Affected Not applicable.
f) Method ofDiscovery of the Error On Monday June 1, 2015, an 8-120B cask user identified a concern that the neoprene gasket could potentially affect the integrity of the vent port seal pre-shipment leak test. Later that week EnergySolutions performed a bench test that confirmed that the neoprene gasket can constrict on the head of the vent port plug cap screw when it is compressed by the manifold, resulting in a reduction of the test sensitivjty.
_3) Assessment of Safety Consequences
* Pre-shipment leak tests of all containment seals, includip.g the vent port, were performed prior to every shipment in accordance with the requirements of Chapter 7 of the SAR. In addition, periodic and maintenance leak tests of the containment seals) using helium as the test gas, were performed after maintenance, repair, Or replacement of the containment Sya}s ID accordance with therequirements of Chapter 8 oft)J.eSAR.
The 8-120B preshipment leak rate test criteria Were sized for the large primary lid. Since the vent port has a much sn1aller test volume, the test specification is conservative.
Calculations
* show that the test specified in the SARis a factor of 9 more sensitive than the lxl o-3 required by Chapter 8 of the SAR. However; due to the uncertainties in the effects ofthe gasket, and the behavior of seaLs in series, it is not possible to c*onfum whether the reduction ill sensitivity is offset by the test criteria conservatism.
/
There has been no indication of any leakage from the vent poti from any shipment, and therefore>
no exposure of individuals to radiation or radioactive materials due to the gaskets. It is also noted that it is unusual for the vent pmt seal to be opened during cask operations, in which case the previous helium leak test of the vent port seal provides added assurance of seal integrity.
Therefore, it is concluded that there has been no safety consequence from performing vent port pre-shipment leak tests that may not have provided the requited test sensitivity of lxl0-3 ref-cm 3 /sec. 4) Planned Corrective Actions EnergySolutions has taken corrective actions to assure that use of the old neoprene gasket design for the vent port pre-shipment leak test is immediately discontinued. -* EnergySolutions notified all 8-120B cask users with upcoming shipments to require use of a new procedure, in conjunction with the new manifold gasket design, for shipment leak testing of the vent port seal on all future shipments.
* EnergySolutions designed and tested new manifold gasket design that does not constrict onto the head of the vent port plus screw when compressed, and therefore it does not reduce the test sensitivity. The new gaskets have been distributed to all upcoming shipment users. The new manifold gasket design is shown in Attachment
: 1. The dTawing for the 8-120B air drop manifold have been revised to include the new gasket and the air pressure drop test procedure TR-TP-002 has been revised to incorporate the new pre-shipment leak test procedure for the vent port. Use of the new procedure and the new manifold gasket will assure that the pre-shipment leak test satisfies the required test sensitivity and that the manifold gasket is removed from the test port after cmnpleting the pre-shipment leak test. 5) Previous Similar Events Involving the 8-120B No previous slinilar events have been identified. 6) Contact for Additional Information Dan Shrum EnergySolutions Senior Vice President, Regulatory Affairs (801) 649-2109 7) Extent of Exposure oflndividuals to Radiation or Radioactive Materials None. 4 
 
Attachment 1 Details of the 8-120B Vent Port Leak Rate Test Setup The 8-120B CoC requires the package to be prepared for shipment and operated in accordance with Chapter 7 of the SAR, and* tested and maintained in accordance with Chapter 8 of the SAR. Step 7 .1.14 of the SAR requires a pre-shipment leak test of the primary lid) secondary lid> and vent port seals to be performed in accordance with Section 83.2.2 prior to every shipment to assure that the containment system is properly f!Ssembled.
Per Table 8-2 ofthe SAR, the shipment leak test of the vent port is performed by connecting a test manifold to the vent port, pressuriZing the seal and head ofthe vent pmt cap screw to 18 psig with dry air or nitrogen, and monitoring the pressure for at least '15 minutes to assure that it does not drop by more than 0.1 psig. The pre-shipment leaktest of the vent port is a pressure drop test performed using a dedicated test manifold.
The test manifold is not a part ofthe licensed package. It includes a stinger (shown below), an 0-ring seal that contacts the* stinger and the bottom of the vent port hole, and a sleeve nut to compress the 0-ring seal. The test manifold was designed so that it the vent port cap screw, leaving a small gap between itself and the vent port cap screw. The 8-120B caskfleet began to ship with a new lid design in September 2013, and operations staff noted more frequent difficulty getting the manifold to seal. It became desirable to find a better way to seal the. bottom of the manifold in order to minimize operator exposure.
They found that adding a neoprene ga,sket (also not part of the licensed package) under the base of the stinger as shown below helped reduce testing time and exposure.
5 j I l !* f ! t l-1 l ! t I I ! I r I i l f. i I 
 
PRIMARY LID VENT PORT CAP SCREW 6 MANIFOLD STINGER MANIFOLD SLEEVE NUT MANIFOLD 0-RING SEAL (NOT LICENSED EQUIPMENT)
NEOPRENE GAS.KET-SHOWN UNCOMPRESSED (NOT LICENSED EQUIPMENT) t I l f l j } I I l i ! I I I ! I t ! ,. j I I ! I I ! l l l f-\fWRG.
TTT'Tf'fi\TCf---------. .\ ,D K -.<;.01 .1 .LVl Y0 Corrective Action.-Modified Test Seal The new manifold gasket design, shown below, replaces the manifold 0-ring seal and neoprene gasket previously used with a neoprene gasket that fits within the notch at the base of the manifold stinger. VENT PORT SEAL VENT PORT CAP SCREW 7 \ \ \ .. "\, \ \ NEW MANIFOLD GASKET (SHOWN UNCOMPRESSED)
I ! l I I l l I I t l l I ! I i ! I I t I i i I 1 i l 1 I r I-I i-l i ! ; j t r I ! i i i ! l l l l l I l i r I}}

Latest revision as of 08:40, 7 April 2019