ENS 45029: Difference between revisions

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| event date = 04/28/2009 21:59 EDT
| event date = 04/28/2009 21:59 EDT
| last update date = 04/29/2009
| last update date = 04/29/2009
| title = Manual Reactor Trip Initiated As A Result Of A Loss Of Condensate Flow
| title = Manual Reactor Trip Initiated as a Result of a Loss of Condensate Flow
| event text = At 2159 Sequoyah Unit 1 was manually tripped from 18% reactor power. The manual trip was in response to automatic isolation of all intermediate pressure feedwater heater strings resulting in a loss of all condensate flow. The feedwater heater strings isolated following a manual trip of the main turbine. The main turbine was manually tripped in response to a failed open moisture separator reheater relief valve. At the time of the event Sequoyah Unit 1 was raising power following a refueling outage.
| event text = At 2159 Sequoyah Unit 1 was manually tripped from 18% reactor power. The manual trip was in response to automatic isolation of all intermediate pressure feedwater heater strings resulting in a loss of all condensate flow. The feedwater heater strings isolated following a manual trip of the main turbine. The main turbine was manually tripped in response to a failed open moisture separator reheater relief valve. At the time of the event Sequoyah Unit 1 was raising power following a refueling outage.
Following the reactor trip, all safety-related equipment operated as designed. Auxiliary feedwater automatically actuated as expected on loss of the operating main feedwater pump.
Following the reactor trip, all safety-related equipment operated as designed. Auxiliary feedwater automatically actuated as expected on loss of the operating main feedwater pump.

Latest revision as of 22:12, 1 March 2018

ENS 45029 +/-
Where
Sequoyah Tennessee Valley Authority icon.png
Tennessee (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-2.15 h-0.0896 days <br />-0.0128 weeks <br />-0.00295 months <br />)
Opened: James W. Fuller
23:50 Apr 28, 2009
NRC Officer: Joe O'Hara
Last Updated: Apr 29, 2009
45029 - NRC Website
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