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{{#Wiki_filter:ACCELERATED
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DOCUMENTDISTRIBUTION
DOCUMENT DISTRIBUTION
SYSTEMSUBJECT:Respondstoviolations
SYSTEM SUBJECT: Responds to violations
notedininsprepts50-315/94-06
noted in insp repts 50-315/94-06
&50-316/94-06.Corrective
&50-316/94-06.Corrective
actions:Procedure
actions:Procedure
12THP6010RPP.606revisedtoincludeWD-490invalvelineup.DISTRIBUTION
12 THP 6010 RPP.606 revised to include WD-490 in valve lineup.DISTRIBUTION
CODE:IE06DCOPIESRECEIVED:LTR
CODE: IE06D COPIES RECEIVED:LTR
ENCLSIZE:TITLE:Environ&Radiological
ENCL SIZE: TITLE: Environ&Radiological
(50DKT)-Insp
(50 DKT)-Insp Rept/Notice
Rept/Notice
of Violation Respons I D NOTES: REGULATORY
ofViolation
ResponsIDNOTES:REGULATORY
INFORMATION
INFORMATION
DISTRIBUTION
DISTRIBUTION
SYSTEM(RIDS)ACCESSION
SYSTEM (RIDS)ACCESSION NBR:9406230229
NBR:9406230229
DOC.DATE: 94/05/25 NOTARIZED:
DOC.DATE:
YES DOCKET¹,'ij FACIL:50-315
94/05/25NOTARIZED:
Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH.NAME AUTHOR AFFILIATION
YESDOCKET¹,'ijFACIL:50-315
DonaldC.CookNuclearPowerPlant,Unit1,IndianaM0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,IndianaM05000316AUTH.NAMEAUTHORAFFILIATION
FITZPATRICK,E.
FITZPATRICK,E.
IndianaMichiganPowerCo.(formerly
Indiana Michigan Power Co.(formerly Indiana&Michigan Ele R RECIP.NAME
Indiana&MichiganEleRRECIP.NAME
RECIPIENT AFFILIATION
RECIPIENT
AFFILIATION
MARTINFJ.B.
MARTINFJ.B.
DocumentControlBranch(Document
Document Control Branch (Document Control Desk)RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD/DSP NMSS/SGTB 4E4 NRR/PMAS/ILRBl2
ControlDesk)RECIPIENT
IDCODE/NAME
PD3-1PDINTERNAL:
AEOD/DSPNMSS/SGTB
4E4NRR/PMAS/ILRBl2
NUDOCS-ABSTRACT
NUDOCS-ABSTRACT
OGC/HDS2RESRGN3FILEOlTERNAL:NRCPDRCOPIESLTTRENCL11111111111111111RECIPIENT
OGC/HDS2 RES RGN3 FILE Ol TERNAL: NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME HICKMAN,J AEOD/TTC NRR/DREP/PRPB10
IDCODE/NAME
HICKMAN,J
AEOD/TTCNRR/DREP/PRPB10
NRR/PMAS/IRCB-E
NRR/PMAS/IRCB-E
OEDIRQFILE02RGNDRSS/RPBRGN4/FIPS
OE DI RQ FILE 02 RGN DRSS/RPB RGN4/FIPS NSIC COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 D D D D NOTE TO ALL"RIDS" RECIPIENTS:
NSICCOPIESLTTRENCL111122111111111111DDDDNOTETOALL"RIDS"RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.504-2065)TO ELIMINATE YOUR NAME FROM DISTRIBUTION
PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2065)
LISTS FOR DOCUMENTS YOU DON'T NEEDl D TOTAL NUMBER OF COPIES REQUIRED: LTTR 19 ENCL 19
TOELIMINATE
Indiana Michigan Power Company P.O.Box 1663 I Coiumbus, OH 43246 lNDIANA NECHlGAN POWM AEP:NRC:1212B-
YOURNAMEFROMDISTRIBUTION
10 CFR 2.201 Donald C.Cook Nuclear Plant Units 1 and 2 Docket Nos.50-315 and 50-316 License Nos.DPR-58 and DPR-74 NRC INSPECTION
LISTSFORDOCUMENTS
REPORTS NO.50-315/94006 (DRSS)AND 50-316/94006 (DRSS)REPLY TO NOTICE OF VIOLATION U.S.Nuclear Regulatory
YOUDON'TNEEDlDTOTALNUMBEROFCOPIESREQUIRED:
LTTR19ENCL19
IndianaMichiganPowerCompanyP.O.Box1663ICoiumbus,
OH43246lNDIANANECHlGANPOWMAEP:NRC:1212B-
10CFR2.201DonaldC.CookNuclearPlantUnits1and2DocketNos.50-315and50-316LicenseNos.DPR-58andDPR-74NRCINSPECTION
REPORTSNO.50-315/94006
(DRSS)AND50-316/94006
(DRSS)REPLYTONOTICEOFVIOLATION
U.S.NuclearRegulatory
Commission
Commission
DocumentControlDeskWashington,
Document Control Desk Washington, D.C.20555 Attn: Mr.J.B.Martin May 25, 1994 Dear Mr.Martin: This letter is in response to a USNRC letter dated April 29, 1994, that forwarded a Notice of Violation (NOV)to Indiana Michigan Power Company.The NOV contained one violation which was self-identified
D.C.20555Attn:Mr.J.B.MartinMay25,1994DearMr.Martin:ThisletterisinresponsetoaUSNRCletterdatedApril29,1994,thatforwarded
by the licensee and noted during a-routine radiation protection
aNoticeofViolation
(NOV)toIndianaMichiganPowerCompany.TheNOVcontained
oneviolation
whichwasself-identified
bythelicenseeandnotedduringa-routineradiation
protection
inspection
inspection
conducted
conducted by Mr.C.R.Cox from March 28 through April 1, 1994.The violation is associated
byMr.C.R.CoxfromMarch28throughApril1,1994.Theviolation
with the proceduralized
isassociated
withtheproceduralized
activities
activities
thatledtothespentresinspillinthe587'rumming
that led to the spent resin spill in the 587'rumming
roomonMarch19,1994.Inresponsetotheevent,promptactionwastakentosuspendallresintransferactivities.
room on March 19, 1994.In response to the event, prompt action was taken to suspend all resin transfer activities.
Corrective
Corrective
actions,intheformofprocedure
actions, in the form of procedure revisions, were instituted
revisions,
to prevent recurrence
wereinstituted
prior to resumption
topreventrecurrence
of such activities.
priortoresumption
Our reply to'the notice of violation is provided in the attachment
ofsuchactivities.
to this letter.This letter is submitted pursuant to 10 CFR 50'4(f)and, as such, an oath statement is attached.Sincerely, pp~pcW E.E.Fitzpatrick
Ourreplyto'thenoticeofviolation
Vice President dr 9'406230229
isprovidedintheattachment
9'40525.PDR ADOCK 05000315 9 PDR
tothisletter.Thisletterissubmitted
STATE OF OHIO)COUNTY OF FRANKLIN)E.E.Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the forgoing response to NRC INSPECTION
pursuantto10CFR50'4(f)and,assuch,anoathstatement
REPORTS NO.50-315/94006 (DRSS)AND 50-316/94006 (DRSS), REPLY TO NOTICE OF VIOLATION and knows the contents thereof;and that said contents are true to the best of his knowledge and belief.Subscribed
isattached.
and sworn to before me this~~4 day of 19 NOTAR PUBLIC-RlTA D.HE'LL NOTARY PUDuC.STATE OP OHt."  
Sincerely,
Mr.J.B.Martin 2 AEP:NRC:1212B
pp~pcWE.E.Fitzpatrick
VicePresident
dr9'406230229
9'40525.PDRADOCK050003159PDR
STATEOFOHIO)COUNTYOFFRANKLIN)
E.E.Fitzpatrick,
beingdulysworn,deposesandsaysthatheistheVicePresident
oflicenseeIndianaMichiganPowerCompany,thathehasreadtheforgoingresponsetoNRCINSPECTION
REPORTSNO.50-315/94006
(DRSS)AND50-316/94006
(DRSS),REPLYTONOTICEOFVIOLATION
andknowsthecontentsthereof;andthatsaidcontentsaretruetothebestofhisknowledge
andbelief.Subscribed
andsworntobeforemethis~~4dayof19NOTARPUBLIC-RlTAD.HE'LLNOTARYPUDuC.STATEOPOHt."  
Mr.J.B.Martin2AEP:NRC:1212B
Attachments
Attachments
CC:A.A.BlindG.CharnoffNFEMSectionChiefNRCResidentInspector
CC: A.A.Blind G.Charnoff NFEM Section Chief NRC Resident Inspector-Bridgman, MI NRC Resident Inspector-Big Rock Point Nuclear Plant J.R.Padgett W.T.Russell, NRC-Washington, D.C.  
-Bridgman,
MINRCResidentInspector
-BigRockPointNuclearPlantJ.R.PadgettW.T.Russell,NRC-Washington,
D.C.  
ATTACHMENT
ATTACHMENT
TOAEP:NRC:1212B
TO AEP:NRC:1212B
REPLYTONOTICEOFVIOLATION
REPLY TO NOTICE OF VIOLATION
ATTACHMENT
ATTACHMENT
TOAEP:NRC:1212B
TO AEP:NRC:1212B
Page1Background
Page 1 Background
Aroutineradiation
A routine radiation protection
protection
inspection
inspection
wasconducted
was conducted by Mr.C.R.Cox from March 28 through April 1, 1994.During this inspection, one item was found to be in violation.
byMr.C.R.CoxfromMarch28throughApril1,1994.Duringthisinspection,
The violation was identified
oneitemwasfoundtobeinviolation.
as inappropriateness
Theviolation
of procedures
wasidentified
with regard to the activities
asinappropriateness
that led to the spent resin spill in the 587 drumming room on March 19, 1994.This violation was set forth in a letter containing
ofprocedures
the notice of violation, dated April 29, 1994, from Mr.John A.Grobe, Acting Chief, Reactors Support Programs Branch.The letter was received May 10, 1994.Our response to the notice of violation is contained within this document.NRC Violation I"10 CFR 50, Appendix B, Criterion V,"Instructions, Procedures, and Drawings," requires that activities
withregardtotheactivities
affecting quality be prescribed
thatledtothespentresinspillinthe587drummingroomonMarch19,1994.Thisviolation
by a procedure of a type appropriate
wassetforthinalettercontaining
to the circumstances
thenoticeofviolation,
and shall be accomplished
datedApril29,1994,fromMr.JohnA.Grobe,ActingChief,ReactorsSupportProgramsBranch.TheletterwasreceivedMay10,1994.Ourresponsetothenoticeofviolation
in accordance
iscontained
with these procedures.
withinthisdocument.
Contrary to the above: On March 18, 1994, Procedure 12 THP 6010 RPP.606,"Operation
NRCViolation
of the Radi.oactive
I"10CFR50,AppendixB,Criterion
Waste Water Demineralizer
V,"Instructions,
System (RWDS)," was inappropriate
Procedures,
to the circumstances
andDrawings,"
in that the valve lineup failed to identify a valve required to be opened for the evolution to be completed successfully.
requiresthatactivities
2.On March 19, 1994, Procedure 02 OHP 4021.007.002,"Reactor Coolant Demineralizer
affecting
Resin Sluicing and Replacement," was inappropriate
qualitybeprescribed
to the circumstances
byaprocedure
in that the procedure failed to identify alternative
ofatypeappropriate
flow paths and the valves whose positions needed to be verified to prevent those alternative
tothecircumstances
flow paths.This is a Severity Level IV violation (Supplement
andshallbeaccomplished
inaccordance
withtheseprocedures.
Contrarytotheabove:OnMarch18,1994,Procedure
12THP6010RPP.606,"Operation
oftheRadi.oactive
WasteWaterDemineralizer
System(RWDS),"wasinappropriate
tothecircumstances
inthatthevalvelineupfailedtoidentifyavalverequiredtobeopenedfortheevolution
tobecompleted
successfully.
2.OnMarch19,1994,Procedure
02OHP4021.007.002,
"ReactorCoolantDemineralizer
ResinSluicingandReplacement,"
wasinappropriate
tothecircumstances
inthattheprocedure
failedtoidentifyalternative
flowpathsandthevalveswhosepositions
neededtobeverifiedtopreventthosealternative
flowpaths.ThisisaSeverityLevelIVviolation
(Supplement
I)."  
I)."  
ATTACHMENT
ATTACHMENT
TOAEP,:NRC:1212B
TO AEP,:NRC:1212B
Page2ResponsetoViolation
Page 2 Response to Violation Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
Admission
2.Reasons for the Violation The valve lineup for procedure 12 THP 6010 RPP.606,"Operation
orDenialoftheAlleedViolation
of the Radioactive
IndianaMichiganPowerCompanyadmitstotheviolation
Waste Water Demineralizer
ascitedintheNRCnoticeofviolation.
System (RWDS)," failed to identify WD-490 due to the procedure author's misinterpretation
2.ReasonsfortheViolation
of valve information
Thevalvelineupforprocedure
when transitioning
12THP6010RPP.606,"Operation
from one flow print to another.The author incorrectly
oftheRadioactive
assumed that WD-498 was identified
WasteWaterDemineralizer
on two prints when in fact WD-498 was on one print and WD-490 was on the other.Subsequent
System(RWDS),"failedtoidentifyWD-490duetotheprocedure
procedure reviews performed prior to the procedure approval failed to identify the original error.Procedure 02 OHP 4021.007.002,"Reactor Coolant Demineralizer
author'smisinterpretation
Resin Sluicing and Replacement," failed to identify alternative
ofvalveinformation
flow paths""and the valves whose positions needed to be verified closed to prevent those paths from being used.This was due to the basic assumption
whentransitioning
that the subject valves are normally maintained
fromoneflowprinttoanother.Theauthorincorrectly
in the closed position and, therefore, a check was not necessary.
assumedthatWD-498wasidentified
ontwoprintswheninfactWD-498wasononeprintandWD-490wasontheother.Subsequent
procedure
reviewsperformed
priortotheprocedure
approvalfailedtoidentifytheoriginalerror.Procedure
02OHP4021.007.002,
"ReactorCoolantDemineralizer
ResinSluicingandReplacement,"
failedtoidentifyalternative
flowpaths""andthevalveswhosepositions
neededtobeverifiedclosedtopreventthosepathsfrombeingused.Thiswasduetothebasicassumption
thatthesubjectvalvesarenormallymaintained
intheclosedpositionand,therefore,
acheckwasnotnecessary.
Corrective
Corrective
ActionsTakenandResultsAchievedOnMarch18,1994,procedure
Actions Taken and Results Achieved On March 18, 1994, procedure 12 THP 6010 RPP.606,"Operation
12THP6010RPP.606,"Operation
of the Radioactive
oftheRadioactive
Waste Water Demineralizer
WasteWaterDemineralizer
System (RWDS)," was revised to include WD-490 in the valve lineup.On March 25, 1994, procedure 02 OHP 4021.007.002,"Reactor Coolant Demineralizer
System(RWDS),"wasrevisedtoincludeWD-490inthevalvelineup.OnMarch25,1994,procedure
Resin Sluicing and Replacement," was revised-to include verification
02OHP4021.007.002,
of the subject alternate flow paths and the associated
"ReactorCoolantDemineralizer
valves which positions needed to be verified.Corrective
ResinSluicingandReplacement,"
Actions Taken to Avoid Further Violations
wasrevised-toincludeverification
The procedure used by the radiation protection
ofthesubjectalternate
flowpathsandtheassociated
valveswhichpositions
neededtobeverified.
Corrective
ActionsTakentoAvoidFurtherViolations
Theprocedure
usedbytheradiation
protection
department
department
forprocedure
for procedure preparation, review and maintenance
preparation,
will be revised to enhance reviews performed to ensure procedure accuracy.This revision will be completed prior to July 1, 1994.  
reviewandmaintenance
willberevisedtoenhancereviewsperformed
toensureprocedure
accuracy.
Thisrevisionwillbecompleted
priortoJuly1,1994.  
ATTACHMENT
ATTACHMENT
TOAEP:NRC:1212B
TO AEP:NRC:1212B
Page3Inthecoverlettertothesubjectnoticeofviolation/inspection
Page 3 In the cover letter to the subject notice of violation/inspection
'eport,itwasrequested
'eport, it was requested that our response include a review of similar evolutions
thatourresponseincludeareviewofsimilarevolutions
that'require coordination
that'requirecoordination
between different groups and the steps taken to improve the coordination
betweendifferent
and communications
groupsandthestepstakentoimprovethecoordination
between such groups.Review and assessment
andcommunications
of coordination
betweensuchgroups.Reviewandassessment
and communication
ofcoordination
between different groups is an integral part of our corrective
andcommunication
action program.Previous assessment
betweendifferent
lead to the initiation
groupsisanintegralpartofourcorrective
of a comprehensive
actionprogram.Previousassessment
leadtotheinitiation
ofacomprehensive
improvement
improvement
planwithintheChemistry
plan within the Chemistry Department.
Department.
Similarly, a self assessment
Similarly,
of recent events related to coordination
aselfassessment
and communication
ofrecenteventsrelatedtocoordination
within the Operations
andcommunication
withintheOperations
Department
Department
hasresultedintheinitiation
has resulted in the initiation
ofsignificant
of significant
changeswithinthisdepartment.
changes within this department.
ThelatestanalysisofourCorrective
The latest analysis of our Corrective
ActionProgramDataBaserevealedthatcommunications
Action Program Data Base revealed that communications
remainachallenge.
remain a challenge.
Thisinformation
This information
hasbeenprovidedtotheappropriate
has been provided to the appropriate
management
management
personnel.
personnel.
Wewillcontinuetomonitorperformance
We will continue to monitor performance
intheseareasandprovidefeedbackrelativetotheeffectiveness
in these areas and provide feedback relative to the effectiveness
ofperformance
of performance
improvement
improvement
initiatives.
initiatives.
TeamworkandCommunication
Teamwork and Communication
arecriticaltothesuccessofanyoperation
are critical to the success of any operation and the, importance
andthe,importance
of each has consistently
ofeachhasconsistently
been emphasized
beenemphasized
during State of the"Plant Sessions conducted by the Vice President-Plant
duringStateofthe"Plant
Manager and attended by plant and contract personnel.
Sessionsconducted
In addition, the AEP Nuclear Organization
bytheVicePresident-Plant
has initiated an integrated
Managerandattendedbyplantandcontractpersonnel.
Team Building process.This integrated
Inaddition,
Team Building process was initiated by Senior Management
theAEPNuclearOrganization
and is designed to enhance teamwork, coordination
hasinitiated
and communication
anintegrated
TeamBuildingprocess.Thisintegrated
TeamBuildingprocesswasinitiated
bySeniorManagement
andisdesignedtoenhanceteamwork,
coordination
andcommunication
throughout
throughout
thewholeorganization.
the whole organization.
Also,theradiation
Also, the radiation protection
protection
department
department
willreviewsimilarprocedural
will review similar procedural
evolutions
evolutions
thatrequirecoordination
that require coordination
betweendifferent
between different groups and will delineate within these procedures
groupsandwilldelineate
withintheseprocedures
individual
individual
responsibilities
responsibilities
forcommandandcontroloftheactivityfrombothanintradepartment
for command and control of the activity from both an intradepartment
andinterdepartment
and interdepartment
coordination
coordination
perspective.
perspective.
Thisreviewwillbecompleted
This review will be completed prior to July 1, 1994.Procedure changes required as a result of this review will be completed prior to May 1, 1995.In addition, the operations
priortoJuly1,1994.Procedure
changesrequiredasaresultofthisreviewwillbecompleted
priortoMay1,1995.Inaddition,
theoperations
department
department
willreviewthiseventwiththeoperations
will review this event with the operations
procedure
procedure group and will determine if changes are necessary to the current procedure development
groupandwilldetermine
process.This review will be completed prior to July 1, 1994.Process changes required as a result of this review wi13.be completed prior to May 1, 1995.Date When Full Com lienee Vill Be Achieved Full compliance
ifchangesarenecessary
was achieved on March 25, 1994, with the revision to Procedure 02 OHP 4021.007.002,"Reactor Coolant Demineralizer
tothecurrentprocedure
Resin'Sluicing and Replacement".
development
process.Thisreviewwillbecompleted
priortoJuly1,1994.Processchangesrequiredasaresultofthisreviewwi13.becompleted
priortoMay1,1995.DateWhenFullComlieneeVillBeAchievedFullcompliance
wasachievedonMarch25,1994,withtherevisiontoProcedure
02OHP4021.007.002,
"ReactorCoolantDemineralizer
Resin'Sluicing
andReplacement".
}}
}}

Revision as of 07:19, 6 July 2018

Responds to Violations Noted in Insp Repts 50-315/94-06 & 50-316/94-06.Corrective Actions:Procedure 12 Thp 6010 RPP.606 Revised to Include WD-490 in Valve Lineup
ML17331B440
Person / Time
Site: Cook  
Issue date: 05/25/1994
From: FITZPATRICK E
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: MARTIN J B
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1212B, NUDOCS 9406230229
Download: ML17331B440 (8)


See also: IR 05000315/1994006

Text

ACCELERATED

DOCUMENT DISTRIBUTION

SYSTEM SUBJECT: Responds to violations

noted in insp repts 50-315/94-06

&50-316/94-06.Corrective

actions:Procedure

12 THP 6010 RPP.606 revised to include WD-490 in valve lineup.DISTRIBUTION

CODE: IE06D COPIES RECEIVED:LTR

ENCL SIZE: TITLE: Environ&Radiological

(50 DKT)-Insp Rept/Notice

of Violation Respons I D NOTES: REGULATORY

INFORMATION

DISTRIBUTION

SYSTEM (RIDS)ACCESSION NBR:9406230229

DOC.DATE: 94/05/25 NOTARIZED:

YES DOCKET¹,'ij FACIL:50-315

Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH.NAME AUTHOR AFFILIATION

FITZPATRICK,E.

Indiana Michigan Power Co.(formerly Indiana&Michigan Ele R RECIP.NAME

RECIPIENT AFFILIATION

MARTINFJ.B.

Document Control Branch (Document Control Desk)RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD/DSP NMSS/SGTB 4E4 NRR/PMAS/ILRBl2

NUDOCS-ABSTRACT

OGC/HDS2 RES RGN3 FILE Ol TERNAL: NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME HICKMAN,J AEOD/TTC NRR/DREP/PRPB10

NRR/PMAS/IRCB-E

OE DI RQ FILE 02 RGN DRSS/RPB RGN4/FIPS NSIC COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 D D D D NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.504-2065)TO ELIMINATE YOUR NAME FROM DISTRIBUTION

LISTS FOR DOCUMENTS YOU DON'T NEEDl D TOTAL NUMBER OF COPIES REQUIRED: LTTR 19 ENCL 19

Indiana Michigan Power Company P.O.Box 1663 I Coiumbus, OH 43246 lNDIANA NECHlGAN POWM AEP:NRC:1212B-

10 CFR 2.201 Donald C.Cook Nuclear Plant Units 1 and 2 Docket Nos.50-315 and 50-316 License Nos.DPR-58 and DPR-74 NRC INSPECTION

REPORTS NO.50-315/94006 (DRSS)AND 50-316/94006 (DRSS)REPLY TO NOTICE OF VIOLATION U.S.Nuclear Regulatory

Commission

Document Control Desk Washington, D.C.20555 Attn: Mr.J.B.Martin May 25, 1994 Dear Mr.Martin: This letter is in response to a USNRC letter dated April 29, 1994, that forwarded a Notice of Violation (NOV)to Indiana Michigan Power Company.The NOV contained one violation which was self-identified

by the licensee and noted during a-routine radiation protection

inspection

conducted by Mr.C.R.Cox from March 28 through April 1, 1994.The violation is associated

with the proceduralized

activities

that led to the spent resin spill in the 587'rumming

room on March 19, 1994.In response to the event, prompt action was taken to suspend all resin transfer activities.

Corrective

actions, in the form of procedure revisions, were instituted

to prevent recurrence

prior to resumption

of such activities.

Our reply to'the notice of violation is provided in the attachment

to this letter.This letter is submitted pursuant to 10 CFR 50'4(f)and, as such, an oath statement is attached.Sincerely, pp~pcW E.E.Fitzpatrick

Vice President dr 9'406230229

9'40525.PDR ADOCK 05000315 9 PDR

STATE OF OHIO)COUNTY OF FRANKLIN)E.E.Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the forgoing response to NRC INSPECTION

REPORTS NO.50-315/94006 (DRSS)AND 50-316/94006 (DRSS), REPLY TO NOTICE OF VIOLATION and knows the contents thereof;and that said contents are true to the best of his knowledge and belief.Subscribed

and sworn to before me this~~4 day of 19 NOTAR PUBLIC-RlTA D.HE'LL NOTARY PUDuC.STATE OP OHt."

Mr.J.B.Martin 2 AEP:NRC:1212B

Attachments

CC: A.A.Blind G.Charnoff NFEM Section Chief NRC Resident Inspector-Bridgman, MI NRC Resident Inspector-Big Rock Point Nuclear Plant J.R.Padgett W.T.Russell, NRC-Washington, D.C.

ATTACHMENT

TO AEP:NRC:1212B

REPLY TO NOTICE OF VIOLATION

ATTACHMENT

TO AEP:NRC:1212B

Page 1 Background

A routine radiation protection

inspection

was conducted by Mr.C.R.Cox from March 28 through April 1, 1994.During this inspection, one item was found to be in violation.

The violation was identified

as inappropriateness

of procedures

with regard to the activities

that led to the spent resin spill in the 587 drumming room on March 19, 1994.This violation was set forth in a letter containing

the notice of violation, dated April 29, 1994, from Mr.John A.Grobe, Acting Chief, Reactors Support Programs Branch.The letter was received May 10, 1994.Our response to the notice of violation is contained within this document.NRC Violation I"10 CFR 50, Appendix B, Criterion V,"Instructions, Procedures, and Drawings," requires that activities

affecting quality be prescribed

by a procedure of a type appropriate

to the circumstances

and shall be accomplished

in accordance

with these procedures.

Contrary to the above: On March 18, 1994, Procedure 12 THP 6010 RPP.606,"Operation

of the Radi.oactive

Waste Water Demineralizer

System (RWDS)," was inappropriate

to the circumstances

in that the valve lineup failed to identify a valve required to be opened for the evolution to be completed successfully.

2.On March 19, 1994, Procedure 02 OHP 4021.007.002,"Reactor Coolant Demineralizer

Resin Sluicing and Replacement," was inappropriate

to the circumstances

in that the procedure failed to identify alternative

flow paths and the valves whose positions needed to be verified to prevent those alternative

flow paths.This is a Severity Level IV violation (Supplement

I)."

ATTACHMENT

TO AEP,:NRC:1212B

Page 2 Response to Violation Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.

2.Reasons for the Violation The valve lineup for procedure 12 THP 6010 RPP.606,"Operation

of the Radioactive

Waste Water Demineralizer

System (RWDS)," failed to identify WD-490 due to the procedure author's misinterpretation

of valve information

when transitioning

from one flow print to another.The author incorrectly

assumed that WD-498 was identified

on two prints when in fact WD-498 was on one print and WD-490 was on the other.Subsequent

procedure reviews performed prior to the procedure approval failed to identify the original error.Procedure 02 OHP 4021.007.002,"Reactor Coolant Demineralizer

Resin Sluicing and Replacement," failed to identify alternative

flow paths""and the valves whose positions needed to be verified closed to prevent those paths from being used.This was due to the basic assumption

that the subject valves are normally maintained

in the closed position and, therefore, a check was not necessary.

Corrective

Actions Taken and Results Achieved On March 18, 1994, procedure 12 THP 6010 RPP.606,"Operation

of the Radioactive

Waste Water Demineralizer

System (RWDS)," was revised to include WD-490 in the valve lineup.On March 25, 1994, procedure 02 OHP 4021.007.002,"Reactor Coolant Demineralizer

Resin Sluicing and Replacement," was revised-to include verification

of the subject alternate flow paths and the associated

valves which positions needed to be verified.Corrective

Actions Taken to Avoid Further Violations

The procedure used by the radiation protection

department

for procedure preparation, review and maintenance

will be revised to enhance reviews performed to ensure procedure accuracy.This revision will be completed prior to July 1, 1994.

ATTACHMENT

TO AEP:NRC:1212B

Page 3 In the cover letter to the subject notice of violation/inspection

'eport, it was requested that our response include a review of similar evolutions

that'require coordination

between different groups and the steps taken to improve the coordination

and communications

between such groups.Review and assessment

of coordination

and communication

between different groups is an integral part of our corrective

action program.Previous assessment

lead to the initiation

of a comprehensive

improvement

plan within the Chemistry Department.

Similarly, a self assessment

of recent events related to coordination

and communication

within the Operations

Department

has resulted in the initiation

of significant

changes within this department.

The latest analysis of our Corrective

Action Program Data Base revealed that communications

remain a challenge.

This information

has been provided to the appropriate

management

personnel.

We will continue to monitor performance

in these areas and provide feedback relative to the effectiveness

of performance

improvement

initiatives.

Teamwork and Communication

are critical to the success of any operation and the, importance

of each has consistently

been emphasized

during State of the"Plant Sessions conducted by the Vice President-Plant

Manager and attended by plant and contract personnel.

In addition, the AEP Nuclear Organization

has initiated an integrated

Team Building process.This integrated

Team Building process was initiated by Senior Management

and is designed to enhance teamwork, coordination

and communication

throughout

the whole organization.

Also, the radiation protection

department

will review similar procedural

evolutions

that require coordination

between different groups and will delineate within these procedures

individual

responsibilities

for command and control of the activity from both an intradepartment

and interdepartment

coordination

perspective.

This review will be completed prior to July 1, 1994.Procedure changes required as a result of this review will be completed prior to May 1, 1995.In addition, the operations

department

will review this event with the operations

procedure group and will determine if changes are necessary to the current procedure development

process.This review will be completed prior to July 1, 1994.Process changes required as a result of this review wi13.be completed prior to May 1, 1995.Date When Full Com lienee Vill Be Achieved Full compliance

was achieved on March 25, 1994, with the revision to Procedure 02 OHP 4021.007.002,"Reactor Coolant Demineralizer

Resin'Sluicing and Replacement".