05000346/LER-1980-061-03, /03L-0:on 800812,during Calibr & Maint Records Check,Personnel Found Valve SV5005 Installed on 760826 for Temporary Use Was Not Replaced.Caused by Inadequate Administrative Control.Replacement for SV5005 Requested: Difference between revisions

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{{Adams
#REDIRECT [[05000346/LER-1980-061-03, /03L-1:on 800812,valve SV5005 Installed 760826 for Temporary Use Was Never Replaced.Caused by Inadequate Implementation of Administrative Control.Valve Secured in Closed Position & Facility Change Request Implemented]]
| number = ML19344F061
| issue date = 09/10/1980
| title = /03L-0:on 800812,during Calibr & Maint Records Check,Personnel Found Valve SV5005 Installed on 760826 for Temporary Use Was Not Replaced.Caused by Inadequate Administrative Control.Replacement for SV5005 Requested
| author name = Isley T
| author affiliation = TOLEDO EDISON CO.
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
| docket = 05000346
| license number =
| contact person =
| document report number = LER-80-061-03L, LER-80-61-3L, TAC-42508, NUDOCS 8009120356
| package number = ML19344F058
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 3
| project = TAC:42508
| stage = Other
}}
{{LER
| Title = /03L-0:on 800812,during Calibr & Maint Records Check,Personnel Found Valve SV5005 Installed on 760826 for Temporary Use Was Not Replaced.Caused by Inadequate Administrative Control.Replacement for SV5005 Requested
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000346
| LER year = 1980
| LER number = 61
| LER revision = 3
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
{{#Wiki_filter:NRC FORM Q U.S. NUCL EAR RE JULATORY COMr.iiSSION (7 77)
LICENSEE EVENT REPORT CONTROL BLOCK: l l
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8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT D ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h ITTTI I (NP-33-80-73) On 8/12/80 at 0900 hours, I&C personnel were checking their calibration l g lcnd maintenance records and discovered that valve SV5005 was instal.i.ed on 8/26/76 for l l temporary use and never replaced. This valve controls the contr.inment purge isolation l o 4 lo i s i l damper CV5005 and was not qualified for nuclear; service.
Being a Safety Features l
lo is I l Actuation System level 1 valve, it must be operable in all modes.
Therefore the l
jol7lletation entered the action statement of T.S. 3.3.2.1.
There was no danger to the l
l o t a l l public or station personnel. The installed valve functioned properly since installed.l 80 7
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CODE S BC E COMPONENT CODE SUSC dE S
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9 10 11 12 13 18 19 20 MQUENTIAL OCCURRENCE REPORT REVISION LER EVENT YEAR REPORT NO.
CODE TYPE N O.
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l0l0l0lDl [YJ Q l N l g l Zl g lZ l9 l9 l9 lg 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h li l o l l The cause was an inadequate implementation of an administrative control.
SV5005 was l
1 i l originally installed for temporary use. however there are no records to indicate anv I
i 2 l followup. When SV5005 was determined unqualified, CV5005 was declared inoperable and I i 3 l secured in its closed position.
Facility Change Request 80-206 has been written to l
l replace SV5005 with a nuclear service grade valve.
l i 4 7
8 9 80 STt
% POWER oTHER STATUS IS O RY DISCOVERY DESCRIPTION [A_j@ l 0 l 0 l 0 l@l NA l
lBl@jComparisonofbadvalvewithknowngoodfne 1 5 A TlVITY CO TENT r.ELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION oF RELE ASE NA l
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7 8 9 10 80 ISSUE OESCniPTION
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8 9 10 68 69 80 g DVR 80-133 Thomas Isley PHONE:
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NAME OF PREPARER i
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:- TOLEDO EDISON COMPANY
.iDAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-80-73 2
'DATE OF EVENT: August 12, 1980, FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:.'Non-Qualified ~ Solenoid Valve Operator Installed on Containment Purge Valve Conditions Prior to Occurrence: The unit was 'in Mode 5 with Poser (MWT) = 0 and Load (Gross MRE) w 0.
Description of Occurrence: On August 12, 1980 at 0900 hours, Inscrument and Controls (I&C) personnel were comparing a suspected bad solenoid valve with a known good one, SV5005.- This good valve,-.SV5005, controls the Containment Purge Inlet Isolation Damper CV5005.- A check of I&C calibration and maintenance records showed that SV5005 was installed August 26, 1976 for temporary use and was never replaced with the proper valve. -This temporary valve is not qualified for nuclear service and is not accepta-ble in this application.
Therefore, CV5005 was declared inoperable and secured in its closed position.
Being a Safety Features Actuation System (SFAS) incident icyc1 1 valve, CV5005 must be operable in all modes, and therefore, the station entered the action statement of Tech-nical Specification 3.3.2.1.
This action statement required the valve to be secured in its safety position, closed.
Designation of Apparent Cause of Occurrence: The cause was an inadequate implementation of an administrative control during the initial plant testing and system turnover. At -
the time.the valve was installed, it was known that it wat for temporary use. I&C's Instrument Information Sheet shows that at the time of the installation, it was known that this solenoid-valve was installed for temporary use until a proper valve -was received. The installation of this temporary valve without proper documentation was not in complianceDwith the administrative requirements of AD 1844.00, " Maintenance".
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. The installed valve did function properly in all testing since it was installed.
 
==Corrective Action==
An ongoing review of I&C records is being conducted to verify that there.had been no other maintenance activities conducted during initial startup and testing that'were completed without conforming to the administrative requirements
~
ofLAD~1844.00. No additional discrepancies have been found.
On: August 12,;1980 when it was determined that the installed SV5005 solenoid valve i
. as not qualified for its application, CV5005 was declared inoperable and secured
~
w in.its closed position'.- The valve will remain closed until a suitable replacement is installed. Nonconformance Report 292-80 was-issued to ensure a qualified solenoid LER 180-061 q
m
 
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...i- }
' TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER' STATION UNIT ONE PAGE 2 SUPPLEMENTAL INFORMATION FOR LER NP-33-80-73
: valve is used. ' Facility Change Request 80-206 has been written to replace SV5005-
.with-an available nuclear service grade solenoid valve.
Failure Data: There have L$en no previous reports of this type damper being declared' inoperable due.to the installation of a non-qualified solenoid valve.
LER #80-061 4
w a
}}
 
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Latest revision as of 11:40, 25 December 2024