05000366/LER-1980-155-03, /03L-0:on 801111,RHR Test Line Isolation Valve 2E11-FO24B & Condensate Drain Isolation Valve 2B21-F16 Found to Be Leaking.Cause Unknown.Investigation Underway.Valves Will Be Repaired Prior to Startup: Difference between revisions

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{{Adams
#REDIRECT [[05000366/LER-1980-155-03, Local Leak Rate Test of RHR Test Line Isolation Valve & Condensate Drain Isolation Valve Revealed Excessive Leakage.Caused by Cracking in Stellite Seating Surface.Valves Repaired]]
| number = ML19345D870
| issue date = 12/09/1980
| title = /03L-0:on 801111,RHR Test Line Isolation Valve 2E11-FO24B & Condensate Drain Isolation Valve 2B21-F16 Found to Be Leaking.Cause Unknown.Investigation Underway.Valves Will Be Repaired Prior to Startup
| author name = Coggin C
| author affiliation = GEORGIA POWER CO.
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| docket = 05000366
| license number =
| contact person =
| document report number = LER-80-155-03L, LER-80-155-3L, NUDOCS 8012170637
| package number = ML19345D864
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 2
}}
{{LER
| Title = /03L-0:on 801111,RHR Test Line Isolation Valve 2E11-FO24B & Condensate Drain Isolation Valve 2B21-F16 Found to Be Leaking.Cause Unknown.Investigation Underway.Valves Will Be Repaired Prior to Startup
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000366
| LER year = 1980
| LER number = 155
| LER revision = 3
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
{{#Wiki_filter:wwu LICENSEE EVENT REPORT n
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61 DOCKET NUVSEH 6d 69 EVENT OATE 74 75 REPOHT O ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h IO l2l l 0n 11-7-80, with Unit 2 in cold shutdown an LLRT by procedure HNP-2-3952
[ O ; 3, lwas performed on the RHR test line isolation valve.2E11-F024B and the l
l condensate drain isolation valv-2B21-F016.
On 11-11-8b, the LLRT co-l 0 4 lO lst I ordinator reviewed the tests and determined that both valves were leak-l 101s 1 I i ng in excess of specified acceptance criteria.
This is a repetitive i
10171 I occurrence - see LER 50-366/1980-154.
l 10181 L.
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CODE SUS E
COMPON ENT CODE SUS DE SU E
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s-3J 34 35 3ti 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11101 I The cause of the leakaoes is unknown at oresent.
Investiaation is un-l 1 i Iderwav: an update report will be submitted.
The valves will be ren-I ITTTl I a i re d p ri o r to s t a r t u o.
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% POWER OTHER STATUS Dis O RY DISCOVERY DESCRIPTION
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RELE ASED OF RELE ASE AMOUNT OF ACTivtTY LOCATION OF RELEASE [1] @ l 7 l@l NA l
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.7 8 9 to 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE
 
==DESCRIPTION==
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PUBLICITY NRC USE ONLY PSSUED DESCHIPT80N lllllllllllllh l
68 69 80
 
==.s enoun,n C. L. Coccin. Sunt. Plt. Enq. Serv.
psoNe: 917-367-7781
 
(
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(%J LER f:
50-366/1980-155 Licensee:
Ceorgia Power Company Facility Name:
Edwin I.
Hatch Docket #: '30-366
 
=Narrative=
Report for LER 50-366/1980-155 Gn 11-7-80, with Unit 2 it cold shutdown, a local leak rate test, per procedure HNP-2-3952, " Primary Containment Periodic performed on the RhR Type B and Type C Leakage Tests," was oest line isol,ation valve 2E11-F024B and the condensate drain isolation valve 2B21-F016.
On 11 8 0',
t h e LLRT coordinator reviewed the test data sheets and determined that both valve eriteria,, The RRR test l'eakages exceeded specified acceptance n line isolation valve 2E11-F024B leaka'ge of 6027 accci-wou1dl 3
~
i 30-da sealed water-inventory acceptance.
have caused that t oru s'y water valves specified by 10CFR50
(')
criteria for all section III.C.3 to be exceeded.
The 200 acem leakage of the condensate drain isolation valve 2B21-F016 was such that the
.009 La (544 acem) overall allowable leakage limit for bypass specified by Tech Specs 3.6.1.2.B.2 would path penetration as see LER repetitive occurrence have been exceeded.
This is a 50-366/1980-154.
There were no effects on public health or safety due to this event.
The cause of the leakages is unknown at present.
Investiga-tion is underway; an update report will be submitted.
The valves will be repaired prior to startup.
##~
v 9
}}
 
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Latest revision as of 08:40, 26 May 2025