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{{#Wiki_filter:_ _ - | {{#Wiki_filter:_ _ - | ||
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Ent gy Oper:tions, Inc. | Ent gy Oper:tions, Inc. | ||
Killona, LA 70006 Tel 504 739 6242 C. Ewing,111 at Safety & Regulatory Affairs W3F1-98-0146 A4.05 PR October 14,1998 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 | Killona, LA 70006 Tel 504 739 6242 C. Ewing,111 at Safety & Regulatory Affairs W3F1-98-0146 A4.05 PR October 14,1998 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555 | ||
==Subject:== | ==Subject:== | ||
Waterford 3 SES Docket No. 50-382 License No. NPF-38 | Waterford 3 SES Docket No. 50-382 License No. NPF-38 Monthly Operating Report Gentlemen: | ||
Attached is the subject monthly report which covers the operating statistics for the month of September,1998. This report is submitted per Section 6.9.1.6 of the Waterford 3 Technical Specifications for Facility Operating License No. NPF-38. | Attached is the subject monthly report which covers the operating statistics for the month of September,1998. This report is submitted per Section 6.9.1.6 of the Waterford 3 Technical Specifications for Facility Operating License No. NPF-38. | ||
Should you have any questions regarding the above, please contact me at (504) 739-6242 or C.C. Hayes at (504) 739-6662. | Should you have any questions regarding the above, please contact me at (504) 739-6242 or C.C. Hayes at (504) 739-6662. | ||
Very truly yours, | Very truly yours, e | ||
\\ | |||
l | l 1 | ||
/ | |||
\\ | |||
Director Nuclear Safety & Regulatory Affairs ECE/ALL/ssf Attachment | l E.C. Ewing | ||
cc: | / | ||
Director Nuclear Safety & Regulatory Affairs ECE/ALL/ssf Attachment cc: | |||
E.W. Merschoff (NRC Region IV), C.P. Patel (NRC-NRR), | |||
J. Smith, N.S. Reynolds, B. Lewis (Utility Data Institute, Inc.), | J. Smith, N.S. Reynolds, B. Lewis (Utility Data Institute, Inc.), | ||
J.T. Wheelock (INPO Records Center), | |||
1 | 1 O | ||
NRC Resident inspectors Office 9810160102 980930 PDR ADOCK 05000302-R PCR j | |||
NRC MONTHLY OPERATING REPORT | |||
==SUMMARY== | ==SUMMARY== | ||
OF OPERATIONS | OF OPERATIONS WATERFORD 3 for September,1998 i | ||
For the month of September, the unit was shutdown on 2 separate occasions and operated l | |||
for several days at a reduced power level. This resulted in an average reactor power level of 42.2% for the month. | |||
l l | l l | ||
1 l | 1 l | ||
l 10/1 & 98 | l 10/1 & 98 Page : I of 6 | ||
l | l 4 | ||
PRESSURIZER SAFETY VALVE FAILURES AND CHALLENGES WATERFORD 3 l | |||
for September,1998 I | |||
l l | l l | ||
There were no pressurizer safety valve failures or challenges experienced during the month. | There were no pressurizer safety valve failures or challenges experienced during the month. | ||
However a conservative decision was made to shut-down the plant to replace the valves due to leak rate projections. | However a conservative decision was made to shut-down the plant to replace the valves due to leak rate projections. | ||
l l | l l | ||
l | l j$)h$$ | ||
j$)h$$ | N4 | ||
OPERATING DATA REPORT DOCKET NUMBER : | |||
: 1. Reporting Period | 50-382 UNIT NAME : WATERFORD 3 DATE OF REPORT : | ||
: 2. Currently Authorized Power Level (MWt) | October 12,1998 COMPLETED BY : | ||
: 3. Power Level to which Restricted (if any)(Net MWe) | D. S. Freeman TELEPHONE: | ||
(504) 739-6575 OPERATING STATUS | |||
: 1. Reporting Period September,1998 Gross Hours in Reporting Period 720 | |||
: 2. Currently Authorized Power Level (MWt) 3,390 Maximum Dependable Capacity (Net MWe) : | |||
1,07s Design Electrical Rating (Net MWe) 1,104 | |||
: 3. Power Level to which Restricted (if any)(Net MWe) | |||
N/A | N/A | ||
: 4. Reason for Restriction (if any) | : 4. Reason for Restriction (if any) | ||
: 5. Number of Hours Reactor was Critical | N/A THIS YEAR TO MONTH DATE CUMULATIVE | ||
: 6. Reactor Reserve Shutdown Hours | : 5. Number of Hours Reactor was Critical 40s.2 s,197.0 98,739.7 | ||
: 7. Hours Generator was On-line | : 6. Reactor Reserve Shutdown Hours o.0 0.0 0.0 | ||
: 8. Unit Reserve Shutdown Hours | : 7. Hours Generator was On-line 357.6 s,138.7 95,822.s | ||
: 9. Gross Thermal Energy Generated | : 8. Unit Reserve Shutdown Hours o.o 0.0 0.0 | ||
: 10. Gross Electrical Energy Generated (MWH) | : 9. Gross Thermal Energy Generated (MWH) 1,029,804 20,s26,386 317,507,977 | ||
: 11. Net Electrical Energy Generated (MWH) | : 10. Gross Electrical Energy Generated (MWH) 324,327 s,941,232 10s,161,270 | ||
: 12. Reactor Service Factor | : 11. Net Electrical Energy Generated (MWH) 295,959 s,636,s8s 101,289,923 | ||
94.s | : 12. Reactor Service Factor 58.4 94.s 84.8 | ||
: 13. Reactor Availability Factor | : 13. Reactor Availability Factor ss.4 94.s 84.8 | ||
: 14. Unit Service Factor | : 14. Unit Service Factor 49 93.7 83.8 | ||
: 15. Unit Availability Factor | : 15. Unit Availability Factor 49.7 93.7 83.8 | ||
: 16. Unit Capacity Factor (using MDC) | : 16. Unit Capacity Factor (using MDC) 38.2 94.2 82.s | ||
: 17. Unit Capacity Factor (using DER) | : 17. Unit Capacity Factor (using DER) 37.2 91.8 80.4 | ||
-18. Unit Forced Outage Rate 46.8 s.s 3.s lW1498 Page ; 3 of 6 | |||
~ | |||
OPERATING DATA REPORT DOCKET NUMBER : 50-382 UNIT NAME : WATERFORD 3 DATE OF REPORT : October 12,1998 COMPLETED BY : D. S. Freeman TELEPHONE: (504) 739-6575 OPERATING STATUS (Cont.) | OPERATING DATA REPORT DOCKET NUMBER : 50-382 UNIT NAME : WATERFORD 3 DATE OF REPORT : | ||
October 12,1998 COMPLETED BY : | |||
D. S. Freeman TELEPHONE: | |||
(504) 739-6575 OPERATING STATUS (Cont.) | |||
: 19. Shutdowns Scheduled over next 6 months (type, date and duration of each) : | : 19. Shutdowns Scheduled over next 6 months (type, date and duration of each) : | ||
REFUEL OUTAGE #9 - commencing on February 5,1999 - 40 day outage | REFUEL OUTAGE #9 - commencing on February 5,1999 - 40 day outage | ||
: 20. If Shutdown at end of report period, estimated date of startup : | : 20. If Shutdown at end of report period, estimated date of startup : | ||
10/1/98 | |||
: 21. Unit is in Commercial Operation. | : 21. Unit is in Commercial Operation. | ||
THIS | THIS YEAR TO MONTH DATE CUMULATIVE i | ||
1 | 1 | ||
: 22. Hours in Reporting Period | : 22. Hours in Reporting Period 720 e,ssi 114,120 | ||
: 23. Unit Forced Outage Hours | : 23. Unit Forced Outage Hours 314.8 ass.7 3,s85.7 | ||
: 24. Nameplate Rating | : 24. Nameplate Rating (Gross MWe) 1,200 Max. Dependable Capacity (Gross MWe) 1,120 | ||
: 25. If changes occur in capacity ratings (Items 2 and 24) since the last report, give the reasons : | : 25. If changes occur in capacity ratings (Items 2 and 24) since the last report, give the reasons : | ||
N/A 1&l498 | N/A 1&l498 Page 4 of 6 | ||
.._______.m__._ | |||
~ | |||
AVERAGE DAILY UNIT POWER LEVEL l | AVERAGE DAILY UNIT POWER LEVEL l | ||
[ | [ | ||
Reporting Period : | DOCKET NUMBER : F0-382 l | ||
l DAY Avg. Power Level | UNIT NAME : | ||
WATERFORD 3 l | |||
DATE OF REPORT : | |||
October 12,1998 COMPLETED BY : | |||
D. S. Freeman TELEPHONE: (504) 739-6575 l | |||
Reporting Period : | |||
September,1998 | |||
( NET MWe ) | |||
l DAY Avg. Power Level DAY Avg. Power Level 1 | |||
1,086 16 542 2 | |||
1,087 17 468 3 | |||
1,087 18 (30) 4 1,087 19 (22) 5 1,088 20 (17) 6 1,088 21 (17) 7 1,089 22 (18) 8 1,088 23 (21) 9 1,070 24 (30) 10 5 | |||
25 (43) 11 (42) 26 (44) 12 350 27 (38) 13 537 28 (30) 14 541 29 (30) 15 540 30 (39) | |||
INSTRUCTIONS : | INSTRUCTIONS : | ||
.On this form, list the average daily unit power level in MWe-Net for each l | |||
day in the reporting month. Compute to the nearest whole megawatt. | |||
l I | l I | ||
10/14N8 | 10/14N8 Page ' 5 of 6 | ||
..O UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NUMBER : | |||
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NUMBER : | 50-382 UNIT NAME : WATERFORD 3 DATE OF REPORT : October 12,1998 COMPLETED BY : | ||
D. S. Freeman TELEPHONE: | |||
Return to power was delayed by 4% days due to the threat by Hurricane Georges | (504) 739-6575 REPORTING PERIOD : September,1998 Outage Date Duration Shutdown Cause, Comments and Number (yymmdd) Type (Hours) Reason Method Corrective Actions 98-04 980910 S | ||
47.6 A | |||
S - Scheduled | 1 Anomalies were discovered in the oil of Main Transformer B, predicating future failure of the transformer. A controlled shutdown of the unit was performed to disconnect the transformer. The plant then operated at a reduced power level with the remaining Main Transformer while the damaged one was swapped out with a spare. (see CR-98-1179) 98-05 980917 F | ||
D - Regulatory Restriction l | 314.8 A | ||
1 Elevated levels of leakage were l | |||
being experienced from the Pressurizer Code Safety Valves. The unit was conservatively shut down due to leak-rate projections. Both Safety Valves were replaced. (see CR-98-1195) | |||
Return to power was delayed by 4% days due to the threat by Hurricane Georges and requirements to receive NRC and FEMA approval for post-hurricane restart. | |||
i hk TYPE REASON F - Forced A - Equipment Failure (explain) | |||
S - Scheduled B - Maintenance or Test C - Refueling i | |||
D - Regulatory Restriction l | |||
E - Operator Training and METHOD License Examination l | |||
1 - Manual F - Administrative l | |||
2 - Manual Scram G - Operational Error (explain) i 3 - Automatic Scram H - Other (explain) 4 - Continuation from Previous Period 5 - Power Reduction 6 - Other (explain) 10/1494 Page ' 6 of 6}} | |||
Latest revision as of 01:20, 11 December 2024
| ML20154K080 | |
| Person / Time | |
|---|---|
| Site: | Waterford |
| Issue date: | 09/30/1998 |
| From: | Ewing E, Freeman D ENTERGY OPERATIONS, INC. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| W3F1-98-0146, W3F1-98-146, NUDOCS 9810160102 | |
| Download: ML20154K080 (7) | |
Text
_ _ -
_.. - ~
Ent gy Oper:tions, Inc.
Killona, LA 70006 Tel 504 739 6242 C. Ewing,111 at Safety & Regulatory Affairs W3F1-98-0146 A4.05 PR October 14,1998 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555
Subject:
Waterford 3 SES Docket No. 50-382 License No. NPF-38 Monthly Operating Report Gentlemen:
Attached is the subject monthly report which covers the operating statistics for the month of September,1998. This report is submitted per Section 6.9.1.6 of the Waterford 3 Technical Specifications for Facility Operating License No. NPF-38.
Should you have any questions regarding the above, please contact me at (504) 739-6242 or C.C. Hayes at (504) 739-6662.
Very truly yours, e
\\
l 1
/
\\
l E.C. Ewing
/
Director Nuclear Safety & Regulatory Affairs ECE/ALL/ssf Attachment cc:
E.W. Merschoff (NRC Region IV), C.P. Patel (NRC-NRR),
J. Smith, N.S. Reynolds, B. Lewis (Utility Data Institute, Inc.),
J.T. Wheelock (INPO Records Center),
1 O
NRC Resident inspectors Office 9810160102 980930 PDR ADOCK 05000302-R PCR j
NRC MONTHLY OPERATING REPORT
SUMMARY
OF OPERATIONS WATERFORD 3 for September,1998 i
For the month of September, the unit was shutdown on 2 separate occasions and operated l
for several days at a reduced power level. This resulted in an average reactor power level of 42.2% for the month.
l l
1 l
l 10/1 & 98 Page : I of 6
l 4
PRESSURIZER SAFETY VALVE FAILURES AND CHALLENGES WATERFORD 3 l
for September,1998 I
l l
There were no pressurizer safety valve failures or challenges experienced during the month.
However a conservative decision was made to shut-down the plant to replace the valves due to leak rate projections.
l l
l j$)h$$
N4
OPERATING DATA REPORT DOCKET NUMBER :
50-382 UNIT NAME : WATERFORD 3 DATE OF REPORT :
October 12,1998 COMPLETED BY :
D. S. Freeman TELEPHONE:
(504) 739-6575 OPERATING STATUS
- 1. Reporting Period September,1998 Gross Hours in Reporting Period 720
- 2. Currently Authorized Power Level (MWt) 3,390 Maximum Dependable Capacity (Net MWe) :
1,07s Design Electrical Rating (Net MWe) 1,104
- 3. Power Level to which Restricted (if any)(Net MWe)
N/A
- 4. Reason for Restriction (if any)
N/A THIS YEAR TO MONTH DATE CUMULATIVE
- 5. Number of Hours Reactor was Critical 40s.2 s,197.0 98,739.7
- 6. Reactor Reserve Shutdown Hours o.0 0.0 0.0
- 7. Hours Generator was On-line 357.6 s,138.7 95,822.s
- 8. Unit Reserve Shutdown Hours o.o 0.0 0.0
- 9. Gross Thermal Energy Generated (MWH) 1,029,804 20,s26,386 317,507,977
- 10. Gross Electrical Energy Generated (MWH) 324,327 s,941,232 10s,161,270
- 11. Net Electrical Energy Generated (MWH) 295,959 s,636,s8s 101,289,923
- 12. Reactor Service Factor 58.4 94.s 84.8
- 13. Reactor Availability Factor ss.4 94.s 84.8
- 14. Unit Service Factor 49 93.7 83.8
- 15. Unit Availability Factor 49.7 93.7 83.8
- 16. Unit Capacity Factor (using MDC) 38.2 94.2 82.s
- 17. Unit Capacity Factor (using DER) 37.2 91.8 80.4
-18. Unit Forced Outage Rate 46.8 s.s 3.s lW1498 Page ; 3 of 6
~
OPERATING DATA REPORT DOCKET NUMBER : 50-382 UNIT NAME : WATERFORD 3 DATE OF REPORT :
October 12,1998 COMPLETED BY :
D. S. Freeman TELEPHONE:
(504) 739-6575 OPERATING STATUS (Cont.)
- 19. Shutdowns Scheduled over next 6 months (type, date and duration of each) :
REFUEL OUTAGE #9 - commencing on February 5,1999 - 40 day outage
- 20. If Shutdown at end of report period, estimated date of startup :
10/1/98
- 21. Unit is in Commercial Operation.
THIS YEAR TO MONTH DATE CUMULATIVE i
1
- 22. Hours in Reporting Period 720 e,ssi 114,120
- 23. Unit Forced Outage Hours 314.8 ass.7 3,s85.7
- 24. Nameplate Rating (Gross MWe) 1,200 Max. Dependable Capacity (Gross MWe) 1,120
- 25. If changes occur in capacity ratings (Items 2 and 24) since the last report, give the reasons :
N/A 1&l498 Page 4 of 6
.._______.m__._
~
AVERAGE DAILY UNIT POWER LEVEL l
[
DOCKET NUMBER : F0-382 l
UNIT NAME :
WATERFORD 3 l
DATE OF REPORT :
October 12,1998 COMPLETED BY :
D. S. Freeman TELEPHONE: (504) 739-6575 l
Reporting Period :
September,1998
( NET MWe )
l DAY Avg. Power Level DAY Avg. Power Level 1
1,086 16 542 2
1,087 17 468 3
1,087 18 (30) 4 1,087 19 (22) 5 1,088 20 (17) 6 1,088 21 (17) 7 1,089 22 (18) 8 1,088 23 (21) 9 1,070 24 (30) 10 5
25 (43) 11 (42) 26 (44) 12 350 27 (38) 13 537 28 (30) 14 541 29 (30) 15 540 30 (39)
INSTRUCTIONS :
.On this form, list the average daily unit power level in MWe-Net for each l
day in the reporting month. Compute to the nearest whole megawatt.
l I
10/14N8 Page ' 5 of 6
..O UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NUMBER :
50-382 UNIT NAME : WATERFORD 3 DATE OF REPORT : October 12,1998 COMPLETED BY :
D. S. Freeman TELEPHONE:
(504) 739-6575 REPORTING PERIOD : September,1998 Outage Date Duration Shutdown Cause, Comments and Number (yymmdd) Type (Hours) Reason Method Corrective Actions 98-04 980910 S
47.6 A
1 Anomalies were discovered in the oil of Main Transformer B, predicating future failure of the transformer. A controlled shutdown of the unit was performed to disconnect the transformer. The plant then operated at a reduced power level with the remaining Main Transformer while the damaged one was swapped out with a spare. (see CR-98-1179) 98-05 980917 F
314.8 A
1 Elevated levels of leakage were l
being experienced from the Pressurizer Code Safety Valves. The unit was conservatively shut down due to leak-rate projections. Both Safety Valves were replaced. (see CR-98-1195)
Return to power was delayed by 4% days due to the threat by Hurricane Georges and requirements to receive NRC and FEMA approval for post-hurricane restart.
i hk TYPE REASON F - Forced A - Equipment Failure (explain)
S - Scheduled B - Maintenance or Test C - Refueling i
D - Regulatory Restriction l
E - Operator Training and METHOD License Examination l
1 - Manual F - Administrative l
2 - Manual Scram G - Operational Error (explain) i 3 - Automatic Scram H - Other (explain) 4 - Continuation from Previous Period 5 - Power Reduction 6 - Other (explain) 10/1494 Page ' 6 of 6