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{{#Wiki_filter:- | {{#Wiki_filter:-. _. | ||
k. | k.n' ? | ||
n' ? | Director, Office of Management and Program Analysis Page 2 | ||
Director, Office of Management and Program Analysis | +- | ||
+- | De: ember 8, 1982 ATTACHMEfff I AIERAGE DAILY UNIT POWER LEVEL | ||
~ | |||
~ | |||
DOCKET NO. 50/395 UNIT v.c.5 mmer I DATE 12-08-82 COMPLETED BY G.J Tavior TELEPHONE (803) 345-5209 MONTH NOVEMBER 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net) | |||
(MWe-Ne:) | (MWe-Ne:) | ||
1 0 | 1 0 | ||
17 29 2 | |||
l 3 | 0 13, | ||
0 | n l | ||
0 | l 3 | ||
n jg iA l | |||
0 3 | |||
5 4 | |||
0 2 | |||
l 5 | |||
M | |||
( | ( | ||
0 | 0 30 6 | ||
0 | 22 0 | ||
91 l | |||
0 | 7 g | ||
O 123 8 | |||
, 24 0 | |||
115 9 | 115 9 | ||
10 | 2? | ||
0 M2 10 26 11 0 | |||
gy 143 0 | |||
170 12 28 13 0 | |||
g | 29 | ||
-156 0 | |||
0 | |||
- 14 y | |||
0 | |||
.N/A gg 3 | |||
14_ | |||
5 8301270164 821208 PDR ADOCK 05000395 R | |||
PDR g | |||
y, | |||
-r, - - - - - | |||
p 4 | |||
s | |||
.,--w | |||
Director, Office of Managemer c and Program Aialysis Page 3 December 8, 1982 | Director, Office of Managemer c and Program Aialysis Page 3 December 8, 1982 ATTACHMENT II OPERATING DATA REPORT DOCKET NO. | ||
50/395 V.C. Summer I UNIT e | |||
12-08-82 DATE G.J. Taylor ~ ~ | |||
G.J. Taylor ~ ~ | ~ | ||
COMPLETED BY | COMPLETED BY (803) 345-5209 TELEPHONE OPERATING STATUS 720 IIOVEMBER 1982 Gross HOURS IN RhPORTING PE81tOO: | ||
: 1. REPORTING PERIOD: | : 1. REPORTING PERIOD: | ||
2775 | N/A 2775 MAX. DEPEND. CAPACITY (MWerNet): | ||
: 2. CUM ENTLY AUTHORIZED POWER LEVEL (MWti: | |||
: 2. CUM ENTLY AUTHORIZED POWER LEVEL (MWti: | |||
DES! JN ELECTRICAL RATING (MWo.Neel: | DES! JN ELECTRICAL RATING (MWo.Neel: | ||
9 0 0.,,,,, | |||
N/A (50% MWt) | N/A (50% MWt) | ||
: 3. POWER LEVC.TO WHICH RESTRICTED (IF ANY) (MhNet): | : 3. POWER LEVC.TO WHICH RESTRICTED (IF ANY) (MhNet): | ||
: 4. REASONS FOR RESTRICTION llF ANYl: | : 4. REASONS FOR RESTRICTION llF ANYl: | ||
The Operating License allows operations to | The Operating License allows operations to mis MONTH YR TO DATE CUMULATIVE | ||
~~ | |||
mis MONTH YR TO DATE CUMULATIVE 50% MWt fer power operations testing. | 50% MWt fer power operations testing. | ||
: 5. NUMBER OF HOURS REACTOR VEAS CRITICAL 0 | 484.3 655.7 655.7 | ||
: 4. REACTOR RESERVE SHUTOOWr4 HOURS . . . . . . . . . . . . . . . . . . . | : 5. NUMBER OF HOURS REACTOR VEAS CRITICAL 0 | ||
192.3 | 0 0 | ||
: 7. HOURS GENER ATOR ON LINE . . . . . . . . . . . . . . . . . . . . . . . . . . | : 4. REACTOR RESERVE SHUTOOWr4 HOURS................... | ||
0 | 192.3 192.3 192.3 | ||
: 7. HOURS GENER ATOR ON LINE.......................... | |||
: 9. GROSS THERMAL ENERGY GENERATED (MWH) ............. | 0 0 | ||
30.567 | 0 S. UNIT RESERVE SHUTDOWN HOURS...................... | ||
: 10. GROSS ELECTRICAL ENERGY GENERATED (MWHI . . . . . . . . . . . . . | : 9. GROSS THERMAL ENERGY GENERATED (MWH)............. | ||
24.839 | 143.789 144,802_ | ||
: 11. NEY ELECTRICAL ENERGY GENERATID (MWH) | 144,802 30.567 30.567, 30,567 | ||
N/A | : 10. GROSS ELECTRICAL ENERGY GENERATED (MWHI............. | ||
: 12. REACTOR SERVICE F ACTOR . . . . . . . . . . . . . . . . . . . . . . . . . . . | 24.839 24.839 24,839 | ||
: 11. NEY ELECTRICAL ENERGY GENERATID (MWH) | |||
: 13. REACTOR AVAILABIllTY F ACTOR . . . . . . . . . . . . . . . . . . . . . . . | N/A N/A N/A | ||
N/A | : 12. REACTOR SERVICE F ACTOR........................... | ||
: 14. UNIT SERVICE F ACTOR . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . | *N/A. | ||
N/A | N/A N/A | ||
: 15. UNIT AVAILABILITY F ACTOR . . . . . . . . . . . . . . . . . . . . . . . . . . | : 13. REACTOR AVAILABIllTY F ACTOR....................... | ||
N/A | N/A N/A N/A | ||
: 16. UNIT CAPACITY FACTOR (using MDC) 7. . . . . . . . . . . . . . . . . . . . | : 14. UNIT SERVICE F ACTOR.............................. | ||
N/A | N/A N/A N/A | ||
: 17. UNIT CAPACITY FACTOR (Using Design MWel . . . . . . . . . . . . . . . . . | : 15. UNIT AVAILABILITY F ACTOR.......................... | ||
N/A N/A N/A | |||
: 16. UNIT CAPACITY FACTOR (using MDC) 7.................... | |||
N/A N/A N/A | |||
: 17. UNIT CAPACITY FACTOR (Using Design MWel................. | |||
N/A | N/A | ||
~ | |||
N/A | N/A N/A | ||
: 18. UNIT FORCED OUTAGE R ATE . . . . . . . . . . . . . . . . . . . . . . . . . . | : 18. UNIT FORCED OUTAGE R ATE.......................... | ||
: 19. SHUTDOWN 4 SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACHl: | : 19. SHUTDOWN 4 SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACHl: | ||
( | ( | ||
D-3 Steam Cenerator Modification -- March 1983, through May,1983 | i D-3 Steam Cenerator Modification -- March 1983, through May,1983 M/A | ||
: 20. iF SHUT DOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARTUP: | : 20. iF SHUT DOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARTUP: | ||
: 21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPGRATION): | : 21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPGRATION): | ||
FORECAST ACHIEVED 10-20-82 10-22-82 INITIAL CRITICALITY l1-l7-82_ 11-16-82 INITIAL ELECTRICITY I | |||
COMMERCIAL OPERATION l | COMMERCIAL OPERATION l | ||
Director, Office of Management and Program Analysis | Director, Office of Management and Program Analysis ATTACHMENT III DOCKET NO. 50/395 Page 4 December 8, 1982 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME V. c. S u==ar i I) ATE 19 nn n? | ||
Page 4 | COMPLETED BY _G J. Tavlor REPORT MONTil NOVEMBER 1982 TELEPHONE (803) m-mo METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR GR NO. | ||
December 8, 1982 | DATE S: SCHEDULED (HOURS) | ||
COMPLETED BY _G | REASON (1) | ||
REDUCING POWER (2) | |||
N/A | CORRECTIVE ACTION 0mENTS | ||
4 | ~ | ||
2 | N/A 821116 S | ||
3 | 382.0 H | ||
4 | 4 Initial Plant Start-up Testing I' | ||
18.5 | 82?l17 F | ||
6 | 54.7 G | ||
3 | |||
: 1) Reactor trip due to low-low level in Steam Generator "B". | |||
2 d21119 S | |||
14.0 H | |||
2 | |||
: 2) Tripped reactor while performing control room evacuation test. | |||
3 (821120 F | |||
19.3 G | |||
3 | |||
: 3) Reactor trip due to low-low la"al. it all Steam Generators. | |||
4 821121 S | |||
12.3 H | |||
4 | |||
: 4) Tripped reactor while performing Station Blackout Test. | |||
5 821122 F | |||
18.5 C | |||
3 | |||
: 5) Reactor trip due to low level in Deaerator tank, caused main feen-water pumps to trip causing turbine to trip, in turn tripping reactor. | |||
6 821129 F | |||
26.9 G | |||
3 | |||
: 6) Reactor trip due to low-low level in g | |||
B Steam Generator while performing i | |||
Steam Generator level test. | |||
t | t | ||
n l' | n l' | ||
Director, Office ~ofcManagement and-Program Analysiv Page15 | Director, Office ~ofcManagement and-Program Analysiv Page15 December 8, 1982 ATTACHMENT IV NARRATIVE | ||
December 8, 1982 ATTACHMENT IV NARRATIVE | |||
==SUMMARY== | ==SUMMARY== | ||
OF OPERATING EXPERIENCE 4 | OF OPERATING EXPERIENCE 4 | ||
1The Nuclear Regulatory Commission granted Virgil C. Summer Nuclear Station Unit No. 1 permission to allow teating and operations to a 50% MWth power level at 1821 hours November 12, 1982. Immediately thereaf ter, commencement of the power ascension. testing program took ' place. At 2200 hours November 16, 1982, Virgil ~C. Summer Nuclear Station was syncronized to the grid at a 10%. power level and produced its first electricity. | 1The Nuclear Regulatory Commission granted Virgil C. | ||
Summer Nuclear Station Unit No. 1 permission to allow teating and operations to a 50% MWth power level at 1821 hours November 12, 1982. | |||
Immediately thereaf ter, commencement of the power ascension. testing program took ' place. | |||
At 2200 hours November 16, 1982, Virgil ~C. | |||
Summer Nuclear Station was syncronized to the grid at a 10%. power level and produced its first electricity. | |||
A reactor trip occurred ' at 0420 hours' November 4,1982, from 0% | A reactor trip occurred ' at 0420 hours' November 4,1982, from 0% | ||
power. The trip was due to a low-low- level in Steam Generator "B" while-in manual control. | power. | ||
The trip was due to a low-low-level in Steam Generator "B" while-in manual control. | |||
On. November 11, 1982-at 1100 hours, problems were encountered in | On. November 11, 1982-at 1100 hours, problems were encountered in | ||
'the. operation-of Main Feedwater Isolation Valve "A". | |||
Then the Plant was-subsequently shut down for corrective action.. It was | |||
Plant was-subsequently shut down for corrective action. . It was determined later that a redundant solenoid was faulty. -It was replaced, and th'e valve was put back into service. | ~ | ||
determined later that a redundant solenoid was faulty. -It was replaced, and th'e valve was put back into service. | |||
The valve was considered to have been Technical Specification operable during the duration of -this condition. | |||
c A reactor - trip occurred Iat 0315 hours November 13,1982, Efran 2% | c A reactor - trip occurred Iat 0315 hours November 13,1982, Efran 2% | ||
power. The trip was due to low feedwater flow to "C" Steam Generator. This occurred due to a. steam flow noise spike on Steam Generator "C" steam flow instrumentation, while testing N-41 Nuclear Instrumentation. | power. | ||
The trip was due to low feedwater flow to "C" Steam Generator. | |||
This occurred due to a. steam flow noise spike on Steam Generator "C" steam flow instrumentation, while testing N-41 Nuclear Instrumentation. | |||
A reactor trip occurred at 2011 hours November 13,1982, from 2% | A reactor trip occurred at 2011 hours November 13,1982, from 2% | ||
power. This trip was due to low-low level in Steam Generator "C". Feedwater was in manual control, and feedwater was isolated due to-high flow through the feedwater bypass valve. Steam Generator level decreased before operator could recover. | power. | ||
i | This trip was due to low-low level in Steam Generator "C". | ||
Feedwater was in manual control, and feedwater was isolated due to-high flow through the feedwater bypass valve. | |||
Steam Generator level decreased before operator could recover. | |||
A reactor trip occurred at 2138 hours November 17,1982, from 35 power. The trip was due to low-low level in Steam Generator "A". | i A reactor trip occurred at 1444 hours November 17, 1982, from 2% | ||
. power. | |||
The trip was due,to low-low level in Steam Generator "B" | |||
. hile transferring emergency feedwater flow to main feedwater w | |||
flow. | |||
A reactor trip occurred at 2138 hours November 17,1982, from 35 power. | |||
The trip was due to low-low level in Steam Generator "A". | |||
A reac. tor trip' occurred at 0030 hours November 19,1982, from 6% | A reac. tor trip' occurred at 0030 hours November 19,1982, from 6% | ||
. power. | |||
The trip was due to low-low level in Steam Generator "C". | |||
l | l | ||
;,v; <,-. | |||
- Director, Office - of. Management and Program Anal'ysis-Page 6 December'8, 1982/ | |||
ATTACHMENT IV Continued At.2315 hours November 19, 1982, a control room evacuation test. | ATTACHMENT IV Continued At.2315 hours November 19, 1982, a control room evacuation test. | ||
was conducted which resulted in a manual trip of . the plant.- | was conducted which resulted in a manual trip of. the plant.- | ||
' Control.of-the - plant was satisfactorily maintained while away | |||
~ | |||
from the Control Room. | from the Control Room. | ||
A reactor trip occurred at 0450 hours November 20,1982, 'from 2% | A reactor trip occurred at 0450 hours November 20,1982, 'from 2% | ||
power. The trip, which was due to Steam Generator Low-Low Level, | power. | ||
The trip, which was due to Steam Generator Low-Low Level, | |||
. occurred.while ettempting to transfer feedwater flow from emergency to main feedwater flow. | |||
? | |||
A ' reactor trip occurredLat 1626 hours November 20,1982, from 12% | A ' reactor trip occurredLat 1626 hours November 20,1982, from 12% | ||
~ | |||
power. The trip was_due to low-low level in all steam generators. Feedwater Isolation Valves A, B, and C tripped when feedwater temperature dropped belor: 225 F. | power. | ||
The trip was_due to low-low level in all steam generators. | |||
Feedwater Isolation Valves A, B, and C tripped when feedwater temperature dropped belor: 225 F. | |||
The feedwater temperature decrease was due to a flow transient in the deaerator tank which caused a cooldown in feedwater. | |||
A reactor trip occurred at 0457 hours November 21,1982, from 1% | A reactor trip occurred at 0457 hours November 21,1982, from 1% | ||
power. The trip, .which was due to Steam Generator Low-Low Level, | power. | ||
The trip,.which was due to Steam Generator Low-Low Level, | |||
At 1419 hours November 21, 1982, a Station Blackout Test was conducted which resulted in a plant trip. | . occurred while warming up main feedwater lines and transferring feedwater flow ' f rom emergency to main feedwater flow. | ||
At 1419 hours November 21, 1982, a Station Blackout Test was conducted which resulted in a plant trip. | |||
The plant performed as expected, and the test was satisfactorily completed. | |||
F A reactor trip occurred at 1059 hours November 22, 1982, from 21% | F A reactor trip occurred at 1059 hours November 22, 1982, from 21% | ||
power. .The trip was a result of a feedwater pump trip due to low-low deaerator tank level, while attempting to transfer to main feedwater valves. The feedwater booster pump and feedwater | power..The trip was a result of a feedwater pump trip due to low-low deaerator tank level, while attempting to transfer to main feedwater valves. | ||
pumps tripped from low level in the deaerator storage tank. This caused the main turbine to trip, subsequently causing the reactor to trip' when power level is greater than 10%. | The feedwater booster pump and feedwater pumps tripped from low level in the deaerator storage tank. | ||
This i | |||
caused the main turbine to trip, subsequently causing the reactor to trip' when power level is greater than 10%. | |||
A reactor trip occurred at 2008 hours November 29,1982, from 30% | A reactor trip occurred at 2008 hours November 29,1982, from 30% | ||
' power. | |||
The trip was due tp low-low level in Steam Generator "b". | |||
The trip occurred while pefforming a Steam Generator level test due to a sticking feedwater regulator valve. | The trip occurred while pefforming a Steam Generator level test due to a sticking feedwater regulator valve. | ||
Virgil C. Summer Nuclear Station is presently continuing power ascension testing to a 50% MWth powcr level. | Virgil C. | ||
Summer Nuclear Station is presently continuing power ascension testing to a 50% MWth powcr level. | |||
__,}} | __,}} | ||
Latest revision as of 09:14, 16 December 2024
| ML20070Q770 | |
| Person / Time | |
|---|---|
| Site: | Summer |
| Issue date: | 12/08/1982 |
| From: | Gabe Taylor SOUTH CAROLINA ELECTRIC & GAS CO. |
| To: | |
| Shared Package | |
| ML20070Q749 | List: |
| References | |
| NUDOCS 8301270164 | |
| Download: ML20070Q770 (5) | |
Text
-. _.
k.n' ?
Director, Office of Management and Program Analysis Page 2
+-
De: ember 8, 1982 ATTACHMEfff I AIERAGE DAILY UNIT POWER LEVEL
~
~
DOCKET NO. 50/395 UNIT v.c.5 mmer I DATE 12-08-82 COMPLETED BY G.J Tavior TELEPHONE (803) 345-5209 MONTH NOVEMBER 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Ne:)
1 0
17 29 2
0 13,
n l
l 3
n jg iA l
0 3
5 4
0 2
l 5
M
(
0 30 6
22 0
91 l
7 g
O 123 8
, 24 0
115 9
2?
0 M2 10 26 11 0
gy 143 0
170 12 28 13 0
29
-156 0
0
- 14 y
0
.N/A gg 3
14_
5 8301270164 821208 PDR ADOCK 05000395 R
PDR g
y,
-r, - - - - -
p 4
s
.,--w
Director, Office of Managemer c and Program Aialysis Page 3 December 8, 1982 ATTACHMENT II OPERATING DATA REPORT DOCKET NO.
50/395 V.C. Summer I UNIT e
12-08-82 DATE G.J. Taylor ~ ~
~
COMPLETED BY (803) 345-5209 TELEPHONE OPERATING STATUS 720 IIOVEMBER 1982 Gross HOURS IN RhPORTING PE81tOO:
- 1. REPORTING PERIOD:
N/A 2775 MAX. DEPEND. CAPACITY (MWerNet):
- 2. CUM ENTLY AUTHORIZED POWER LEVEL (MWti:
DES! JN ELECTRICAL RATING (MWo.Neel:
9 0 0.,,,,,
N/A (50% MWt)
- 3. POWER LEVC.TO WHICH RESTRICTED (IF ANY) (MhNet):
- 4. REASONS FOR RESTRICTION llF ANYl:
The Operating License allows operations to mis MONTH YR TO DATE CUMULATIVE
~~
50% MWt fer power operations testing.
484.3 655.7 655.7
- 5. NUMBER OF HOURS REACTOR VEAS CRITICAL 0
0 0
- 4. REACTOR RESERVE SHUTOOWr4 HOURS...................
192.3 192.3 192.3
- 7. HOURS GENER ATOR ON LINE..........................
0 0
0 S. UNIT RESERVE SHUTDOWN HOURS......................
- 9. GROSS THERMAL ENERGY GENERATED (MWH).............
143.789 144,802_
144,802 30.567 30.567, 30,567
- 10. GROSS ELECTRICAL ENERGY GENERATED (MWHI.............
24.839 24.839 24,839
- 11. NEY ELECTRICAL ENERGY GENERATID (MWH)
N/A N/A N/A
- 12. REACTOR SERVICE F ACTOR...........................
- N/A.
N/A N/A
- 13. REACTOR AVAILABIllTY F ACTOR.......................
N/A N/A N/A
- 14. UNIT SERVICE F ACTOR..............................
N/A N/A N/A
- 15. UNIT AVAILABILITY F ACTOR..........................
N/A N/A N/A
- 16. UNIT CAPACITY FACTOR (using MDC) 7....................
N/A N/A N/A
- 17. UNIT CAPACITY FACTOR (Using Design MWel.................
N/A
~
N/A N/A
- 18. UNIT FORCED OUTAGE R ATE..........................
- 19. SHUTDOWN 4 SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACHl:
(
i D-3 Steam Cenerator Modification -- March 1983, through May,1983 M/A
- 20. iF SHUT DOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARTUP:
- 21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPGRATION):
FORECAST ACHIEVED 10-20-82 10-22-82 INITIAL CRITICALITY l1-l7-82_ 11-16-82 INITIAL ELECTRICITY I
COMMERCIAL OPERATION l
Director, Office of Management and Program Analysis ATTACHMENT III DOCKET NO. 50/395 Page 4 December 8, 1982 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME V. c. S u==ar i I) ATE 19 nn n?
COMPLETED BY _G J. Tavlor REPORT MONTil NOVEMBER 1982 TELEPHONE (803) m-mo METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR GR NO.
DATE S: SCHEDULED (HOURS)
REASON (1)
REDUCING POWER (2)
CORRECTIVE ACTION 0mENTS
~
N/A 821116 S
382.0 H
4 Initial Plant Start-up Testing I'
82?l17 F
54.7 G
3
- 1) Reactor trip due to low-low level in Steam Generator "B".
2 d21119 S
14.0 H
2
- 2) Tripped reactor while performing control room evacuation test.
3 (821120 F
19.3 G
3
- 3) Reactor trip due to low-low la"al. it all Steam Generators.
4 821121 S
12.3 H
4
- 4) Tripped reactor while performing Station Blackout Test.
5 821122 F
18.5 C
3
- 5) Reactor trip due to low level in Deaerator tank, caused main feen-water pumps to trip causing turbine to trip, in turn tripping reactor.
6 821129 F
26.9 G
3
- 6) Reactor trip due to low-low level in g
B Steam Generator while performing i
Steam Generator level test.
t
n l'
Director, Office ~ofcManagement and-Program Analysiv Page15 December 8, 1982 ATTACHMENT IV NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE 4
1The Nuclear Regulatory Commission granted Virgil C.
Summer Nuclear Station Unit No. 1 permission to allow teating and operations to a 50% MWth power level at 1821 hours0.0211 days <br />0.506 hours <br />0.00301 weeks <br />6.928905e-4 months <br /> November 12, 1982.
Immediately thereaf ter, commencement of the power ascension. testing program took ' place.
At 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> November 16, 1982, Virgil ~C.
Summer Nuclear Station was syncronized to the grid at a 10%. power level and produced its first electricity.
A reactor trip occurred ' at 0420 hours0.00486 days <br />0.117 hours <br />6.944444e-4 weeks <br />1.5981e-4 months <br />' November 4,1982, from 0%
power.
The trip was due to a low-low-level in Steam Generator "B" while-in manual control.
On. November 11, 1982-at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />, problems were encountered in
'the. operation-of Main Feedwater Isolation Valve "A".
Then the Plant was-subsequently shut down for corrective action.. It was
~
determined later that a redundant solenoid was faulty. -It was replaced, and th'e valve was put back into service.
The valve was considered to have been Technical Specification operable during the duration of -this condition.
c A reactor - trip occurred Iat 0315 hours0.00365 days <br />0.0875 hours <br />5.208333e-4 weeks <br />1.198575e-4 months <br /> November 13,1982, Efran 2%
power.
The trip was due to low feedwater flow to "C" Steam Generator.
This occurred due to a. steam flow noise spike on Steam Generator "C" steam flow instrumentation, while testing N-41 Nuclear Instrumentation.
A reactor trip occurred at 2011 hours0.0233 days <br />0.559 hours <br />0.00333 weeks <br />7.651855e-4 months <br /> November 13,1982, from 2%
power.
This trip was due to low-low level in Steam Generator "C".
Feedwater was in manual control, and feedwater was isolated due to-high flow through the feedwater bypass valve.
Steam Generator level decreased before operator could recover.
i A reactor trip occurred at 1444 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.49442e-4 months <br /> November 17, 1982, from 2%
. power.
The trip was due,to low-low level in Steam Generator "B"
. hile transferring emergency feedwater flow to main feedwater w
flow.
A reactor trip occurred at 2138 hours0.0247 days <br />0.594 hours <br />0.00354 weeks <br />8.13509e-4 months <br /> November 17,1982, from 35 power.
The trip was due to low-low level in Steam Generator "A".
A reac. tor trip' occurred at 0030 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> November 19,1982, from 6%
. power.
The trip was due to low-low level in Steam Generator "C".
l
- ,v; <,-.
- Director, Office - of. Management and Program Anal'ysis-Page 6 December'8, 1982/
ATTACHMENT IV Continued At.2315 hours0.0268 days <br />0.643 hours <br />0.00383 weeks <br />8.808575e-4 months <br /> November 19, 1982, a control room evacuation test.
was conducted which resulted in a manual trip of. the plant.-
' Control.of-the - plant was satisfactorily maintained while away
~
from the Control Room.
A reactor trip occurred at 0450 hours0.00521 days <br />0.125 hours <br />7.440476e-4 weeks <br />1.71225e-4 months <br /> November 20,1982, 'from 2%
power.
The trip, which was due to Steam Generator Low-Low Level,
. occurred.while ettempting to transfer feedwater flow from emergency to main feedwater flow.
?
A ' reactor trip occurredLat 1626 hours0.0188 days <br />0.452 hours <br />0.00269 weeks <br />6.18693e-4 months <br /> November 20,1982, from 12%
~
power.
The trip was_due to low-low level in all steam generators.
Feedwater Isolation Valves A, B, and C tripped when feedwater temperature dropped belor: 225 F.
The feedwater temperature decrease was due to a flow transient in the deaerator tank which caused a cooldown in feedwater.
A reactor trip occurred at 0457 hours0.00529 days <br />0.127 hours <br />7.556217e-4 weeks <br />1.738885e-4 months <br /> November 21,1982, from 1%
power.
The trip,.which was due to Steam Generator Low-Low Level,
. occurred while warming up main feedwater lines and transferring feedwater flow ' f rom emergency to main feedwater flow.
At 1419 hours0.0164 days <br />0.394 hours <br />0.00235 weeks <br />5.399295e-4 months <br /> November 21, 1982, a Station Blackout Test was conducted which resulted in a plant trip.
The plant performed as expected, and the test was satisfactorily completed.
F A reactor trip occurred at 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br /> November 22, 1982, from 21%
power..The trip was a result of a feedwater pump trip due to low-low deaerator tank level, while attempting to transfer to main feedwater valves.
The feedwater booster pump and feedwater pumps tripped from low level in the deaerator storage tank.
This i
caused the main turbine to trip, subsequently causing the reactor to trip' when power level is greater than 10%.
A reactor trip occurred at 2008 hours0.0232 days <br />0.558 hours <br />0.00332 weeks <br />7.64044e-4 months <br /> November 29,1982, from 30%
' power.
The trip was due tp low-low level in Steam Generator "b".
The trip occurred while pefforming a Steam Generator level test due to a sticking feedwater regulator valve.
Virgil C.
Summer Nuclear Station is presently continuing power ascension testing to a 50% MWth powcr level.
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