ML20054G374: Difference between revisions

From kanterella
Jump to navigation Jump to search
(StriderTol Bot insert)
 
(StriderTol Bot change)
 
Line 1: Line 1:
{{Adams
#REDIRECT [[05000339/LER-1982-023]]
| number = ML20054G374
| issue date = 06/11/1982
| title = LER 82-023/03L-0:on 820516 & 17,pressure in Nitrogen Reservoir for Pressurizer Power Operated Relief Valve PCV-2455c Dropped Below Tech Spec Limit.Caused by Nitrogen Leak in Supply Sys.Sys Will Be Modified
| author name = Cartwright W
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| docket = 05000339
| license number =
| contact person =
| document report number = LER-82-023-03L-03, LER-82-23-3L-3, NUDOCS 8206210496
| package number = ML20054G368
| document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
| page count = 2
}}
 
=Text=
{{#Wiki_filter:_ _ . _ _ _ _ . . . _ _ _                  . __
s      .
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK / / / / / / / (1) (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
/0/1/          /V/A/N/A/S/2/ (2)              /0/0/-/0/0/0/0/0/-/0/0/ (3)                                  /4/1/1/1/1/ (4)          / /    / (5)
LICENSEE CODE                                LICENSE NUMBER                                LICENSE TYPE              CAT O
                ~  R
                        /L/ (6)      /0/5/0/0/0/3/3/9/                          (7)    /0/5/1/6/8/2/ (8)            /0 /6 /1/1/8 /2 / (9)
DOCKET NUMBER                                    EVENT DATE                    REPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES (10)
/0/2/      / On On May 16, 1982 and again on May 17, 1982 while in Mode 5, the pressure in the/
f0/3/      / ni-J cogen reservoir for the pressurizer PORV (PCV-2455C) dropped below the minimum /
f0/4/      / pressure required to maintain the PORV operable. Since the pressure was restored /
/0/5/      / within the time of the T.S. 3.4.9.3.a action statement and the redundant PORV                                                    /
/0/6/      / remained operable, the health and safety of the public were not affected. This /
/0/7/      / event is reportable pursuant to T.S. 6.9.1.9.b.                                                                                  /
/0/8/      /                                                                                                                                  /
SYSTEM          CAUSE          CAUSE                                                    COMP.            VALVE CODE            CODE          SUBCODE                        COMPONENT CODE            SUBCODE          SUBCODE
/0/9/          /C/J/ (11)    /B/ (12)      /A/ (13) /V/A/L/V/E/X (14) /F/ (15)                                          /B/ (16)
SEQUENTIAL                              OCCURRENCE          REPORT            REVISION LER/R0    EVENT YEAR          REPORT NO.                                  CODE              TYPE                  NO.
(17) REPORT NUMBER        /8/2/      /-/ /0/2/3/                            / /        /0/3/            /L/        /-/      /0/
(CTION        FUTURE      EFFECT      SHUTDOWN                                      ATTACHMENT NPRD-4            PRIME COMP. COMPONENT FAKEN          ACTION      ON PLANT METHOD                        HOURS            SUBMITTED FORM SUB. SUPPLIER              MANUFACTURER
[X/ (18)      /F/ (19)    /Z/ (20)    /Z/ (21) /0/0/0/0/ (22) /Y/ (23) /N/ (24) /A/ (25) /M/1/2/0/ (26)
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS (27) fl/0/      / Leakage in the PORV nitrogen supply system caused the reservoir pressure to                                                      /
/1/1/      / decrease. In addition, the curreat method for replenishing nitrogen supply is /
/1/2/      / inadequate. A design study has been completed and Jm system will be modified to /
'l/3/    / improve reliability.                                                                                                              /
'1/4/    /                                                                                                                                  /
FACILITY                                                                      METHOD OF STATUS            % POWER                                                                            DISCOVERY DESCRIPTION (32)
'l/5/    /C/ (28)        /0/0/0/ (29)      / OTilER    NA STATUS            / ( } DISCOVERY
                                                                                        /A/ (31)              / Operational Event            /
ACTIVITY          CONTENT RELEASED      OF RELEASE        AMOUNT OF ACTIVITY (35)                                      LOCATION OF RELEASE (36)
/1/6/        /Z/ (33)      /Z/ (34)    /                      NA                      /      /          NA                                /
PERSONNEL EXPOSURES NUMBER          TYPE        DESCRIPTION (39)
'l/7/ /0/0/0/ (37) /Z/ (38)            /      NA                                                                                            /
PERSONNEL INJURIES NUMBER            DESCRIPTION (41)
':/8/    /0/0/0/ (40) /                NA                                                                                                    /
LOSS OF OR DAMAGE TO FACILITY TYPE        DESCRIPTION                    (43)
'1/9/      /Z/ (42)    /          NA                                                                                                        /
PUBLICITY ISSUED        DESCRIPTION (45)                                                                          NRC USE ONLY
  /2/0/    /N/ (44)    /          NA                                                                        /////////////
NAME OF PREPARER                        W.        R. CARTWRIGHT                PHONE      (703) 894-5151        __
8206210496 820611 PDR ADOCK 05000339 q                      PDR
 
Virginia Electric and Power Company North Anna Power Station, Unit No. 2-         
 
==Attachment:==
Page 1 of 1 Docket No. 50-339 Attachment to LER 82-032/03L-0 Description of Event On May 16, 1982 and on May 17, 1982, while in Mode 5, the nitrogen supply that provides the operating medium for the pressurizer PORV decreased to below the minimum pressure required to maintain the PORV's operable. PORV operability is based on the design requirement for 120 valve cycles (1775 psig). Since the tanks were repressurized within the time frame of the Action Statement and the redundant PORV remained operable to provide overpressure protection, the health and safety of the public were not affected.
Probable Consequences of Occurrence The operability of the PORV's in cold shutdown conditions is required to ensure that the reactor coolant pressure boundary is not pressurized in the non-ductile range. The redundant PORV remained operable and there was no pressure transient. Therefore, there was no affect on the health or safety of the public.
Cause of Event The low nitrogen pressure condition was caused by excessive leakage in the nitrogen supply system and an inadequate method of replenishing nitrogen to the system. In addition, the setpoint on a relief valve within the system drifted low causing an additional leak path.
Immediate Corrective Action Additional nitrogen was supplied and thc supply tanks restored to the proper pressure. The setpoint on the relief valve was readjusted.
Scheduled Corrective Action No additional actions will be taken at this time.
Action Taken To Prevent Recurrence The nitrogen system has been reviewed to correct the operational problems. As a result, a design change is being developed. When implemented, the leakage experienced should be reduced and an adequate method for replenishing nitrogen supplies provided.
Generic Implications North Anna Units 1 and 2 have experienced excessive nitrogen system leakage since the system was installed.}}

Latest revision as of 08:12, 15 March 2020