ML20004D635: Difference between revisions
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lY l@ lYl@ lLl@ l G l 2 l 1 l 0 l( | lY l@ lYl@ lLl@ l G l 2 l 1 l 0 l( | ||
33 14 J5 40 di 42 43 44 47 CAUSC DESCRIPTION AND CORRECTIVE ACTIONS h I i I o ! LOverpressurization of the tube side of the HPCI stland seal condenser caused the l | 33 14 J5 40 di 42 43 44 47 CAUSC DESCRIPTION AND CORRECTIVE ACTIONS h I i I o ! LOverpressurization of the tube side of the HPCI stland seal condenser caused the l | ||
((_TJ Lgaskets to stretch out of place. Caskets were replaced. Graham Manufacturine I | |||
,,i j l Company neoprene gasket; pressure class, 150 psi (design); normal operating pressure, I i,i q l 60 psi. Special test will be initiated to monitor piping pressures to determine 1 liiil l cause of overpressurization. I H ) 80 T li ' POWER | ,,i j l Company neoprene gasket; pressure class, 150 psi (design); normal operating pressure, I i,i q l 60 psi. Special test will be initiated to monitor piping pressures to determine 1 liiil l cause of overpressurization. I H ) 80 T li ' POWER | ||
. O THE R STA TUS ISCO Rv DISCOVERY CESCRePTION NA i Operator observed l | . O THE R STA TUS ISCO Rv DISCOVERY CESCRePTION NA i Operator observed l | ||
Revision as of 15:28, 15 March 2020
| ML20004D635 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 06/05/1981 |
| From: | TENNESSEE VALLEY AUTHORITY |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| Shared Package | |
| ML20004D626 | List: |
| References | |
| LER-81-019-03L, LER-81-19-3L, NUDOCS 8106090601 | |
| Download: ML20004D635 (2) | |
Text
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UPDATE REPORT--PRE 7IOUS REPORT DATE 5/15/81 LICENSEE EVENT REPORT w
CON IllOL ItLOCK. l l f l (PLEASE PRINT oR TYPE ALL REoutRED INFORMATioNI
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T D ATE 15 0 6VEN T DESCRIPTION AND PROB ABLE CONSEQUENCES h
[n1.'l l During automatic reactor shutdown, when the HPCI system was initiated. the unoer I gg l and lower HPCI gland seal condenser head gaskets were blown. The HPCI was removed I i n I .i l l from service to replace the gaskets. There was no danger to the health or safety i I
g o j ., i l of the public. Redundant systems were operable. Previous similar events: B FRO l l g l 260/74016W, 74017W, 74024W, and 74028W. I PEI I
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33 14 J5 40 di 42 43 44 47 CAUSC DESCRIPTION AND CORRECTIVE ACTIONS h I i I o ! LOverpressurization of the tube side of the HPCI stland seal condenser caused the l
((_TJ Lgaskets to stretch out of place. Caskets were replaced. Graham Manufacturine I
,,i j l Company neoprene gasket; pressure class, 150 psi (design); normal operating pressure, I i,i q l 60 psi. Special test will be initiated to monitor piping pressures to determine 1 liiil l cause of overpressurization. I H ) 80 T li ' POWER
. O THE R STA TUS ISCO Rv DISCOVERY CESCRePTION NA i Operator observed l
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Tennessee Valley Authority Form BF-17 Erowns Ferry Nuclear Plant BF 15.2 3/24/81 LER SUPPLEMENTAL INFORMATION BFRO 296 / 81019 R1 Technical Specification Involved 3.5.E.l(2)
Reported Under Technical Specification 6.7.2.b.2 Date of Occurrence 4/23/81 Time of Occurrence 0830 Unit 3 Identification and Description of Occurrence:
Unit 3 HPCI inoperable to replace gland seal condenser gaskets.
Conditiens Prior to Occurrence:
Unit i refueling outage Unit 2 at 99%
Unit 3 scram due to low reactor water level.
Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment. Describe.
Requirements of T.S. 3.5.E.1(2) were met.
l t pparent Cause of Occurrence:
Overpressurizing gland seal condenser (tube side).
Analysis of Occurrence:
l There was no danger to the health or safety of the public, no release of activity.
l no damage to the plant or equipment, and no resulting significant chain of events.
l l Corrective Action:
Replaced head gaskets. Instrumentation will be installed to monitor piping pressures to determine cause of overpressurization.
Failure Data:
BFRO-50-260/74016W, 74017W, 74024W, and 74028W.
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- Retention : Period - Lifetime; Responsibility - Document Control Supervisor
- Revision : t
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