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See also: [[followed by::IR 05000255/1996014]]


=Text=
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{{#Wiki_filter:consumers . Power*.*** . l'OWERIN&  
{{#Wiki_filter:consumers . Power*.*** . l'OWERIN&
llllClllliAWS  
llllClllliAWS l'IUlliRESS Palisades Nuclear Plant: 27780 Blue Star Memorlal Highway, Covert, Ml 49043 February 21, 1997 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 DOCKET 50-255 -LICENSE PPR-20 -PALISADES PLANT Thomas J. Palmisano Plant General Manager . RESPONSE TO NOTICE OF VIOLATION FOR TWO VIOLATIONS IN NRC . INTEGRATED INSPECTION REPORT NO. 50-255/96014(DRP)  
l'IUlliRESS  
-. ---NRC Inspection Report No. 50-255/96014(DRP) dated January 22,_1997, identified two Severity Level IV Violations of NRC requirements.
Palisades  
The first violation identified two examples where the plant staff did not adhere to procedures while performing outage related activities.
Nuclear Plant: 27780 Blue Star Memorlal Highway, Covert, Ml 49043 February 21, 1997 U.S. Nuclear Regulatory  
The second violation identified an example where adequate installation instructions were not provided for a temporary modification to the containment polar crane. response to these violations is in Attachment 1 . . . . . Consumers Power Company (CPCo) agrees to the violations as stated.  
Commission  
 
Document Control Desk Washington, DC 20555 DOCKET 50-255 -LICENSE PPR-20 -PALISADES  
==SUMMARY==
PLANT Thomas J. Palmisano  
OF COMMITMENTS This letter contains three new commitments and no revisions to existing commitments.
Plant General Manager . RESPONSE TO NOTICE OF VIOLATION  
: 1. Periodic.activity, SPSOSO, will be revised to use the terminology of operating procedure, SOP 30, and to make the steps to align automatic transfer switch,
FOR TWO VIOLATIONS  
* YSO, an Operations responsibility with the appropriate sign offs. . . . A review of all installed modifications will be conducted to verify tha. t J . acceptable standards were used for installation. . * -r-/ 1 . .. . . __, 2. 9703030519 970221 PDR ADOCK 05000255 G PDR Ml f HD /ID/ f MIJMI /ID A CMS ENERGY COMPANY   
IN NRC . INTEGRATED  
,. ' . 3. The Temporary Modification process will be reviewed to assure that adequate . guidance is provided to the design engineer for providing . . instructions, and for verifying that the temporary modification was installed as intended by the design.
INSPECTION  
* Thomas J. Palmisano Plant General Manager CC
REPORT NO. 50-255/96014(DRP)  
* Administrator, Region Ill, USNRC Project Manager, NRR, USNRC NRC Resident.Inspector  
-. ---NRC Inspection  
-Palisades
Report No. 50-255/96014(DRP)  
dated January 22,_1997, identified  
two Severity Level IV Violations  
of NRC requirements.  
The first violation  
identified  
two examples where the plant staff did not adhere to procedures  
while performing  
outage related activities.  
The second violation  
identified  
an example where adequate installation  
instructions  
were not provided for a temporary  
modification  
to the containment  
polar crane. response to these violations  
is in Attachment 1 . . . . . Consumers  
Power Company (CPCo) agrees to the violations  
as stated. SUMMARY OF COMMITMENTS  
This letter contains three new commitments  
and no revisions  
to existing commitments.  
1. Periodic.activity, SPSOSO, will be revised to use the terminology  
of operating  
procedure, SOP 30, and to make the steps to align automatic  
transfer switch, * YSO, an Operations  
responsibility  
with the appropriate  
sign offs. . . . A review of all installed  
modifications  
will be conducted  
to verify tha. t J . acceptable  
standards  
were used for installation. . * -r-/ 1 . .. . . __, 2. 9703030519  
970221 PDR ADOCK 05000255 G PDR  
Ml f HD /ID/ f MIJMI /ID A CMS ENERGY COMPANY   
,. ' . 3. The Temporary  
Modification  
process will be reviewed to assure that adequate . guidance is provided to the design engineer for providing . . instructions, and for verifying  
that the temporary  
modification  
was installed  
as intended by the design. *  
Thomas J. Palmisano  
Plant General Manager CC * Administrator, Region Ill, USNRC Project Manager, NRR, USNRC NRC Resident.Inspector  
-Palisades  
* Attachment  
* Attachment  
* .. 2   
* .. 2   
. ATTACHMENT  
. ATTACHMENT 1 CONSUMERS POWER COMPANY . PALISADES PLANT ** DOCKET 50-255 RESPONSE TO TWO VIOLATIONS FROM NRC INSPECTION  
1 CONSUMERS  
-REPO_RT 50-255/96014 (DRP)
POWER COMPANY . PALISADES  
PLANT ** DOCKET 50-255 RESPONSE TO TWO VIOLATIONS  
FROM NRC INSPECTION  
-REPO_RT 50-255/96014 (DRP)  
JANUARY 22, 1997 10 Pages   
JANUARY 22, 1997 10 Pages   
. * RESPONSE TO-NOTICE  
.
OF VIOLATION  
* RESPONSE TO-NOTICE OF VIOLATION FROM NRC INSPECTION REPORT NO. 5'?_,-255/96014(DRP)
FROM NRC INSPECTION  
NRG VIOLATION
REPORT NO. 5'?_,-255/96014(DRP)  
: 1) 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings, 11 requires that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.
NRG VIOLATION  
* a.
1) 10 CFR 50, Appendix B, Criterion  
* Licensee procedure CPAL-RFM-002, Revision 0, Section 9.2.11, "Uncouple CROMs and Raise RackExtensions, 11 required in step C.4 that all CRDMs be mechanically' locked prior to ins*erting a reactor trip . into the protection system. . b. Work Order No. 24610226 and PPAC No. SPS050, "PM Auto Transfer Switch, 11 Step 11, required that operations return the isolation handle to . normal position prior to performing step .12, which required that operations return the bypass handle to automatic.
V, "Instructions, Procedures, and Drawings, 11 requires that activities  
Contrary to the above, a.* On November 7, 1996, the operations shift did not ensure that the . control rod drive mechanisms were mechanically locked prior to inserting a reactor trip signal, resulting in the CROM racks dropping into **the reactor vessel upper guide structure.*
affecting  
: b. 'On November 17, 1996, the operations shift did not return the isolation handle to the normal position prior to returning the bypass handle to *: automatic position *. resulting in a loss of power to instrument AC bus Y-01. This is a Severity Level IV violation (Supplement  
quality shall be prescribed  
/). 1 CONSUMERS POWER COMPANY RESPONSE *Consumers-Power Company (CPCo) agrees with the violation as stated. ,REASON FOR VIOLATION Event 1a. Several factors *Contributed to this event. First, the "C" shift Control Room Supervisor and the Control Operator were not fully knowledgeable about the status of the control rod drive mechanisms.
by documented  
Second, the shift turnover between "B" shift and "C" shift was inadequate in that it failed to identify the controlling procedure and it failed to discuss. the need to contact Refueling Services after Electrical maintenance was completed with -CRD #33. Third, the Control Room Supervisor and the Control Operator failed.to question the need for a-procedure and determine which procedure was governing the evolution.
instructions, procedures, or drawings, of a type appropriate  
* Piscussion On November 7, 1996, preparations were being made to remove thereactor vessel* head. These preparations require.
to the circumstances  
* 1) The uncoupling of the control rods from their drive mechanisms.
and shall be accomplished  
: 2) Raising the control rod drive racks 3) Mechanically locking .the control rod drive racks . 4) De.-energizing the control rod drive motors, clutches, and brakes by placing the reactor protection system in the "reactor.
in accordance  
trip" mode. On "A" shift, the Refueling Services personnel began to uncouple the control rod drives. About 1300 on "B" shift, the Refueling Ser-Vices Supervisor called the Control -Room to let the Control Room know the uncoupling was completed and Operations was requested to raise the control rod drive racks. At this time, Operations discussed the status of the uncoupling with Refueling Services and understood that the Refueling Services procedure was controlling.
with these instructions, procedures, or drawings.  
Operations then withdrew forty-four of the five control rod drive racks, but problems were*encountered with CRD #33 rack. Electrical maintenance personnel assistance was requested.
* a. * Licensee procedure  
While the plant electricians were repairing CRD #33, Operations turnover between "B" and '!C" shifts occurred.
CPAL-RFM-002, Revision 0, Section 9.2.11, "Uncouple  
During this turnover, general information concerning the control rods was . exchanged, but it was not established.that the Refueling Services procedure was controlling. "C"*shift Operations personnel did not understand that the Refueling
CROMs and Raise RackExtensions, 11 required in step C.4 that all CRDMs be mechanically'  
* Services procedure was controlling the evolution and that Refueling Services required notification to lock the control rod drive racks after CRD#33 rack was withdrawn  
locked prior to ins*erting  
a reactor trip . into the  
protection  
system. . b. Work Order No. 24610226 and PPAC No. SPS050, "PM Auto Transfer Switch, 11 Step 11, required that operations  
return the isolation  
handle to . normal position prior to performing  
step .12, which required that operations  
return the bypass handle to automatic.  
Contrary to the above, a.* On November 7, 1996, the operations  
shift did not ensure that the . control rod drive mechanisms  
were mechanically  
locked prior to inserting  
a reactor trip signal, resulting  
in the CROM racks dropping into **the reactor vessel upper guide structure.*  
b. 'On November 17, 1996, the operations  
shift did not return the isolation  
handle to the normal position prior to returning  
the bypass handle to *: automatic  
position *. resulting  
in a loss of power to instrument  
AC bus Y-01. This is a Severity Level IV violation (Supplement  
/). 1
CONSUMERS  
POWER COMPANY RESPONSE *Consumers-Power  
Company (CPCo) agrees with the violation  
as stated. ,REASON FOR VIOLATION  
Event 1a. Several factors *Contributed  
to this event. First, the "C" shift Control Room Supervisor  
and the Control Operator were not fully knowledgeable  
about the status of the control rod drive mechanisms.  
Second, the shift turnover between "B" shift and "C" shift was inadequate  
in that it failed to identify the controlling  
procedure  
and it failed to discuss. the need to contact Refueling  
Services after Electrical  
maintenance  
was completed  
with -CRD #33. Third, the Control Room Supervisor  
and the Control Operator failed.to  
question the need for a-procedure  
and determine  
which procedure  
was governing  
the evolution.  
* Piscussion  
On November 7, 1996, preparations  
were being made to remove thereactor  
vessel* head. These preparations  
require. * 1) The uncoupling  
of the control rods from their drive mechanisms.  
2) Raising the control rod drive racks 3) Mechanically  
locking .the control rod drive racks . 4) De.-energizing  
the control rod drive motors, clutches, and brakes by placing the reactor protection  
system in the "reactor.  
trip" mode. On "A" shift, the Refueling  
Services personnel  
began to uncouple the control rod drives. About 1300 on "B" shift, the Refueling  
Ser-Vices  
Supervisor  
called the Control -Room to let the Control Room know the uncoupling  
was completed  
and Operations  
was requested  
to raise the control rod drive racks. At this time, Operations  
discussed  
the status of the uncoupling  
with Refueling  
Services and understood  
that the Refueling  
Services procedure  
was controlling.  
Operations  
then withdrew forty-four  
of the five control rod drive racks, but problems were*encountered  
with CRD #33 rack. Electrical  
maintenance  
personnel  
assistance  
was requested.  
While the plant electricians  
were repairing  
CRD #33, Operations  
turnover between "B" and '!C" shifts occurred.  
During this turnover, general information  
concerning  
the control rods was . exchanged, but it was not established.that  
the Refueling  
Services procedure  
was controlling. "C"*shift  
Operations  
personnel  
did not understand  
that the Refueling  
* Services procedure  
was controlling  
the evolution  
and that Refueling  
Services required notification  
to lock the control rod drive racks after CRD#33 rack was withdrawn  
.. 2   
.. 2   
. '. * On "C" shift the electricians  
. '.
finished repairing  
* On "C" shift the electricians finished repairing CRD #33, withdrew the control rod drive rack and mechanically locked itin place. The Shift Supervisor, upon being notified that CRD #33 problem had been resolved and the control rod drive rack was mechanically locked, thought the next sequential step to be performed was to place the reactor protective system in the "reactor trip" mode. The Shift Supervisor did not verify the status of the control rod drive racks nor did he determine which procedure was controlling the evolution and verify that the prerequisites were met. The Shift Supervisor directed Control Room personnel to place the reactor protection system in the "reactor trip" mode. Control Room personnel observed all control rod drive racks, except CRD #33 rack, reinserting into the reactor vessel upon the reactor protection system trip initiation.
CRD #33, withdrew the control rod drive rack and mechanically  
Subsequently, it was recognized that the control rod racks had not been mechanically locked when control rod #33 rack problem was encountered.
locked itin place. The Shift Supervisor, upon being notified that CRD #33 problem had been resolved and the control rod drive rack was mechanically  
The Refueling Services procedure allowed the control rod drive racks to be l.ocked after all the racks were withdrawn.
locked, thought the next sequential  
Event 1b. The reasons for this event included inadequate understanding of the work scope, inadequate communications, inadequate work control documents and improper equipment operation.
step to be performed  
* Discussion
was to place the reactor protective  
* On November 17, 1996, the plant was in refueling shutdown conditions with shutdown cooling system in operation.
system in the "reactor trip" mode. The Shift Supervisor  
The instrument AC Bus, Y01, was being supplied from Motor Control Center 1. Y01 is critical to the operation of the shutdown cooling system as it affects shutdown cooling heat exchanger bypass and: discharge valves (CV-3006 . and CV-3025).
did not verify the status of the control rod drive racks nor did he determine  
Earlier in the day these valves were placed on their manual hand jacks to maintain their position as instrument air was isolated and tagged for another maintenance activity.
which procedure  
An electrical preventative maintenance activity (PPAC) was schedul_ed for the Y01 automatic transfer switch, YSO. This required the YSO switch to be removed .from _ service so electrical maintenance personnel could remove the switch from the cabinet and take it to the electrical shop to perform the preventative maintenance.
was controlling  
Control Room personnel reviewed the activity but focused on the impact of this activity on the operation of the shutdown cooling system. They determined that the shutdown cooling heat exchanger bypass and discharge valves would not be affected as they were manually peing operated by the valves' hand jacks. The outage schedule stated that Operations was to "Manually align Y01 to'its normal supply". However, because all *the PPAC steps were assigned to Electrical Maintenance for completion, Operations 3   
the evolution  
*
and verify that the prerequisites  
* did not obtain a copy of the procedure to review, and failed to establish the full electrical maintenance work scope ... Subsequently, Operations decided to implement a portion of SOP 30 that configured the YSO switch from automatic to normal, but did not recognize the need to place the isolation handle to "open" (see attached sketch). This configuration fulfilled only one of two alignment steps specified in the PPAC. The Control Room Supervisor (CRS) directed an Auxiliary Operator (AO) to configure Y01 onto its normal supply using SOP 30. The AO accompanied by the System Engineering Test Coordinator (SETC) performed the alignment.
were met. The Shift Supervisor  
The SETC explained to the AO that not only would Y01 have to be placed on its normal power supply but, also, YSO must be isolated by moving the isolation handle to the "open" position.
directed Control Room personnel  
At this point the AO should have contacted the.CRS for direction and permission to perform the isolation.
to place the reactor protection  
However, the AO did the isolation and then communicated the completion of the activity and the additional step taken to the Nuclear Control Operator (NCO). The NCO understood this message to mean that the activity was completed as directed by the CRS. Therefore, the CRS was not informed that YSO was isolated.
system in the "reactor trip" mode. Control Room personnel  
After the electrical mainter:iance activity was completed, the Electrician informed the Work Control Center Lead SRO that maintenance was completed and that the Electrician*
observed all control rod drive racks, except CRD #33 rack, reinserting  
needed to be present when Operations restored the switch in order to sign. the work order steps. Also, the SETC contacted the Work Control Center and * . reque$ted that he be notified prior to the restoration activity; however, neither were contacted.
into the reactor vessel upon the reactor protection  
If either the Eiectrician or the SETC had been at the work site.during restoration, or if the work activity been written to have Operations sign off for . . restoration, Operations would have understood the desired position of YSO. \ . . . Work Control Center notified the Shift Lead SRO that YSO could be restored.
system trip initiation.  
The Shift Lead SRO conferred with the CRS on restoring YSO, and they decided to proceed. The CRS assigned a different AO to restore YSO, informed the AO and Shift Lead SRO of the. steps he had directed the previous AO to perform, and identified the steps of SOP 30 to restore YSO.. * * * * * *
Subsequently, it was recognized  
* The Shift Lead SRO and the AO went to perform the alignment of YSO. They observed the isolation handle, the source light indication and the switch's physical position, but they did not recognize their indications were different than expected.
that the control rod racks had not been mechanically  
The AO placed the YSO bypass handle from normal to automatic.
locked when control rod #33 rack problem was encountered.  
Because the isolation handle had not been restored to the "close" position, YSO failed to transfer and Y01 was de-energized.  
The Refueling  
Services procedure  
allowed the control rod drive racks to be l.ocked after all the racks were withdrawn.  
Event 1b. The reasons for this event included inadequate  
understanding  
of the work scope, inadequate  
communications, inadequate  
work control documents  
and improper equipment  
operation.  
* Discussion  
* On November 17, 1996, the plant was in refueling  
shutdown conditions  
with shutdown cooling system in operation.  
The instrument  
AC Bus, Y01, was being supplied from Motor Control Center 1. Y01 is critical to the operation  
of the shutdown cooling system as it affects shutdown cooling heat exchanger  
bypass and: discharge  
valves (CV-3006 . and CV-3025).  
Earlier in the day these valves were placed on their manual hand jacks to maintain their position as instrument  
air was isolated and tagged for another maintenance  
activity.  
An electrical  
preventative  
maintenance  
activity (PPAC) was schedul_ed  
for the Y01 automatic  
transfer switch, YSO. This required the YSO switch to be removed .from _ service so electrical  
maintenance  
personnel  
could remove the switch from the cabinet and take it to the electrical  
shop to perform the preventative  
maintenance.  
Control Room personnel  
reviewed the activity but focused on the impact of this activity on the operation  
of the shutdown cooling system. They determined  
that the shutdown cooling heat exchanger  
bypass and discharge  
valves would not be affected as they were manually peing operated by the valves' hand jacks. The outage schedule stated that Operations  
was to "Manually  
align Y01 to'its normal supply". However, because all *the PPAC steps were assigned to Electrical  
Maintenance  
for completion, Operations  
3   
* * did not obtain a copy of the procedure  
to review, and failed to establish  
the full electrical  
maintenance  
work scope ... Subsequently, Operations  
decided to implement  
a portion of SOP 30 that configured  
the YSO switch from automatic  
to normal, but did not recognize  
the need to place the isolation  
handle to "open" (see attached sketch). This configuration  
fulfilled  
only one of two alignment  
steps specified  
in the PPAC. The Control Room Supervisor (CRS) directed an Auxiliary  
Operator (AO) to configure  
Y01 onto its normal supply using SOP 30. The AO accompanied  
by the System Engineering  
Test Coordinator (SETC) performed  
the alignment.  
The SETC explained  
to the AO that not only would Y01 have to be placed on its normal power supply but, also, YSO must be isolated by moving the isolation  
handle to the "open" position.  
At this point the AO should have contacted  
the.CRS for direction  
and permission  
to perform the isolation.  
However, the AO did the isolation  
and then communicated  
the completion  
of the activity and the additional  
step taken to the Nuclear Control Operator (NCO). The NCO understood  
this message to mean that the activity was completed  
as directed by the CRS. Therefore, the CRS was not informed that YSO was isolated.  
After the electrical  
mainter:iance  
activity was completed, the Electrician  
informed the Work Control Center Lead SRO that maintenance  
was completed  
and that the Electrician*  
needed to be present when Operations  
restored the switch in order to sign. the work order steps. Also, the SETC contacted  
the Work Control Center and * . reque$ted  
that he be notified prior to the restoration  
activity;  
however, neither were contacted.  
If either the Eiectrician  
or the SETC had been at the work site.during  
restoration, or if the work activity been written to have Operations  
sign off for . . restoration, Operations  
would have understood  
the desired position of YSO. \ . . . Work Control Center notified the Shift Lead SRO that YSO could be restored.  
The Shift Lead SRO conferred  
with the CRS on restoring  
YSO, and they decided to proceed. The CRS assigned a different  
AO to restore YSO, informed the AO and Shift Lead SRO of the. steps he had directed the previous AO to perform, and identified  
the steps of SOP 30  
to restore YSO.. * * * * * * * The Shift Lead SRO and the AO went to perform the alignment  
of YSO. They observed the isolation  
handle, the source light indication  
and the switch's physical position, but they did not recognize  
their indications  
were different  
than expected.  
The AO placed the YSO bypass handle from normal to automatic.  
Because the isolation  
handle had not been restored to the "close" position, YSO failed to transfer and Y01 was de-energized.  
' l 4   
' l 4   
,. CORRECTIVE  
,. CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED The following actions were taken. _ Event 1a. 1. Refueling and Maintenance outage activities were temporarily suspended on November 18, 1996 to review and reinforce nuclear, radiation, and industrial/personnel safety concerns with all work groups on site. This event and several other events from the first two weeks of the outage were reviewed with all crews. A common theme running among the identified issues is the lack communications between work groups and alignment among workers. *
ACTIONS TAKEN AND RESULTS ACHIEVED The following  
* 2. Three specific responsibilities were reinforced at the Operations Department stand down meetings.
actions were taken. _ Event 1a. 1. Refueling  
These were: . " Shift Supervisors, are to identify Operations activities from the outage schedule with an understanding of the relationship between these . and others. It is intended that this understanding will contribute to well-informed decision making the Operations organization.  
and Maintenance  
* . Work Control Center Senior Reactor Operators are to direct work activities
outage activities  
* having Operations involvement to Control Room personnel for authorization . .
were temporarily  
* This is to provide interfacing work documents physically to the individual.s . who will be performing the activity, better communications between Operations and other. work discipline*
suspended  
personnel, and improve the information flow to those individuals who will be directing the activity>
on November 18, 1996 to review and reinforce  
* Control. Room personnel are to assure they have a complete understanding
nuclear, radiation, and industrial/personnel  
* of activities requested of them and that proper alignments have been made. . . 3. . . The control rod drive blades and racks were inspected for damage due the trip occurring with a reduced water level. No damage was observed on any of the control rod drive blades or racks. *
safety concerns with all work groups on site. This event and several other events from the first two weeks of the outage were reviewed with all crews. A common theme running among the identified  
* Event 1b. In addition to actions 1 and 2 from above, the following actions were taken. 1. Shift Supervisor, CRS, Lead SRO, AO and other Operations personnel involved discussed this event and the barriers that could have prevented it. The 5   
issues is the lack communications  
.. . . -discussion included responsibilities for proper communications, pre-job briefings, equipment operation, self checking and other aspects of operator ccmduct. 2. Shift Operations Supervisor has briefed the Shift Supervisors and SROs on the need to identify and conduct pre-job briefings.
between work groups and alignment  
The expectation to conduct . . --. job briefings whenever coordination between two or more work groups is required has been re-established.
among workers. * * 2. Three specific responsibilities  
* 3.
were reinforced  
* Maintenance and Construction Manager reinforced pre-job briefing expectations with maintenance and construction supervision personnel using this event as an example where a collective pre-job briefing may have prevented the event. CORRECTIVE ACTIONS REMAINING TO BE TAKEN TO AVOID FURTHER VIOLATIONS . Periodic activity, SPS050, will be revised to use the terminology of operating ,
at the Operations  
* procedure, SOP 30, and to make the steps to align automatic transfer switch, YSO, an Operations responsibility with the appropriate sign offs. DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED
Department  
* CPCo is now in full compliance.
stand down meetings.  
6 Y-50 AUTOMATIC TRANSFER SWITCH I I I ! i _! -i ' I I I I I i i I .
These were: . " Shift Supervisors, are to identify Operations  
* EMERGENCY BYPASS HANDLE. CE ... AUTOMATIC  
activities  
* * . OfEN . *NORMAL T a.£ROENCY TCJL..IU:XX NORMAL m FAm SWITOf SOURa (KM!Nl'ARY)
from the outage schedule with an understanding  
SOURCE
of the relationship  
* AVAJl...&BIE  
between these . and others. It is intended that this understanding  
will contribute  
to well-informed decision making  
the Operations  
organization.  
* . Work Control Center Senior Reactor Operators  
are to direct work activities  
* having Operations  
involvement  
to Control Room personnel  
for authorization . . * This is to provide interfacing  
work documents  
physically  
to the individual.s . who will be performing  
the activity, better communications  
between Operations  
and other. work discipline*  
personnel, and improve the information  
flow to those individuals  
who will be directing  
the activity>  
* Control. Room personnel  
are to assure they have a complete understanding  
* of activities  
requested  
of them and that proper alignments  
have been made. . . 3. . . The control rod drive blades and racks were inspected  
for damage due the trip occurring  
with a reduced water level. No damage was observed on any of the control rod drive blades or racks. * * Event 1b. In addition to actions 1 and 2 from above, the following  
actions were taken. 1. Shift Supervisor, CRS, Lead SRO, AO and other Operations  
personnel  
involved discussed  
this event and the barriers that could have prevented  
it. The 5   
.. . . -discussion  
included responsibilities  
for proper communications, pre-job briefings, equipment  
operation, self checking and other aspects of operator ccmduct. 2. Shift Operations  
Supervisor  
has briefed the Shift Supervisors  
and SROs on the need to identify and conduct pre-job briefings.  
The expectation  
to conduct . . --. job briefings  
whenever coordination  
between two or more work groups is required has been re-established.  
* 3. * Maintenance  
and Construction  
Manager reinforced  
pre-job briefing expectations  
with maintenance  
and construction  
supervision  
personnel  
using this event as an example where a collective  
pre-job briefing may have prevented  
the event. CORRECTIVE  
ACTIONS REMAINING  
TO BE TAKEN TO AVOID FURTHER VIOLATIONS . Periodic activity, SPS050, will be revised to use the terminology  
of operating , * procedure, SOP 30, and to make the steps to align automatic  
transfer switch, YSO, an Operations  
responsibility  
with the appropriate  
sign offs. DATE WHEN FULL COMPLIANCE  
WILL BE ACHIEVED * CPCo is now in full compliance.  
6
Y-50 AUTOMATIC  
TRANSFER SWITCH I I I ! i _! -i ' I I I I I i i I . * EMERGENCY  
BYPASS HANDLE. CE ... AUTOMATIC  
* * . OfEN . *NORMAL T a.£ROENCY  
TCJL..IU:XX  
NORMAL m FAm SWITOf SOURa (KM!Nl'ARY)  
SOURCE * AVAJl...&BIE  
...... AVAILABIP  
...... AVAILABIP  
* .. 0 11tANSFER . TE$t' LOAD (])NNECJE)  
* .. 0 11tANSFER . TE$t' LOAD (])NNECJE)
TO NORMAL * . 1t1SI' .. NORMAL  
TO NORMAL * . 1t1SI' .. NORMAL  
.* *1MCC#2! l , RESET ro* MCC # 1 I* I NORMAL 1*  
.* *1MCC#2! l , RESET ro* MCC # 1 I* I NORMAL 1*
7 . . .   
7 . . .   
*. * NRC VIOLATION  
*.
.2.) 10 CFR 50, Appendix B, Criterion  
* NRC VIOLATION  
Ill, Design Control, requires, in part," that . design control measures " ... shall include provisions  
.2.) 10 CFR 50, Appendix B, Criterion Ill, Design Control, requires, in part," that . design control measures " ... shall include provisions to assure that appropriate quality standards are specified and included in design documents  
to assure that appropriate  
... ," and that " ... design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of .. design reviews. Design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design ... " Palisades Administrative Procedure 9.31, "Temporary Modification Control," Revision *12, Paragraph 7.1.8, required that a technical review be conducted to verify that instructions for installation were correct .. Contrary to the On November 6, 1996, Temporary Modification (TM) 96-050 to the containment polar came did not contain correct installation instructions for replacement of a single solenoid with two solenoids.
quality standards  
The original solenoid was*hard mounted and was provided with adequate ventilation to prevent premature failure. As the result of inadequate preparation and review, TM 96-050 did not provide instructions for mounting the second of the two replacement solenoids.
are specified  
The* second solenoid was installed utilizing duct tape and "tie-wtaps" in a manner which resulted in overheating and failure of the solenoid coil, and a subsequent .
and included in design documents  
* electrical fire .. This is a Severity IV violation (Supplement 1 ). CONSUMERS POWER COMPANY RESPONSE Consumers Power Company (CPCo) agrees with the violation as stated. REASON FOR THE VIOLATION . Based on the inspection data from the failed coils, the most likely cause of the failure on the trolley crane brake coils is the manner which the coils were mounted. This *inadequate mounting design was caused by the failure of design personnel to.identify soler:ioid heat dissipation as critical characteristic during the design process . 8 . -
... ," and that " ... design control measures shall provide for verifying  
* Discussion . A temporary modification was required to the containment Polar Crane due to a failure of the existing 460VAC solenoid on the trolley brake actuator.
or checking the adequacy of design, such as by the performance  
No replacement 460VAC solenoid was available.
of .. design reviews. Design changes, including  
When this solenoid is energized, the actuator releases the braking mechanism on the crane trolley motor. ) The modification involved the replacement of the original 460VAC coil with 230VAC coils. One of the 230V coils would be installed in the position of the original coil and the second would be used as a dummy load to provide a voltage drop across it. This would result in a voltage dividing circuit which would divide the 460 volts from the circuit supply in half thus applying 230 volts across each coil. To ensure that the impedance w<ifs matched a spare plunger was inserted into the dummy coil and fixed in the inserted position using duct tape. The dummy coil was then tye-wrapped to a . support bar and additional tape was wrapped around it. The temporary modification to substitute the 230VAC coils for the 460VAC was an acceptable design. However, the dummy coil mounting design was focused on making sure the coil did not come loose and fall into the debris free zone inside containment.  
field changes, shall be subject to design control measures commensurate  
* . Potential overheating of the dummy coil was not considered in the design. The Polar Crane was in service with the temporary modification in place for approximately 60 hours before failure occurred.
with those applied to the original design ... " Palisades  
With high usage of the Polar Crane. and repeated starts and stops on the trolley crane motor, the additional layers of tape on the dummy coil caused chronic overheating of the dummy coil. The epoxy insulating material became hot enough to melt and the dummy coil wires shorted togetheL This allowed the full 460 volts to be applied across the 230VAC working coil, causing its failure. The smoke and. arcing observed was the result of the dummy coil overheating, causing the duct tape to catch fire and burn. No evidence of arcing to the support structure was found around either coil. CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED 1.
Administrative  
* The two 230 volt coils were replaced with a new. 460 volt coil. It has been in use *without incident since it was installed  
Procedure  
.. 2. This event was reviewed as a lessons learned with all Design Engineering at a department stand down meeting. Discussions covered conditions leading to the event, and the need for Design Engineering to consider all operating characteristics in design . 9 CORRECTIVE ACTIONS REMAINING TO BE TAKEN TO AVOID FURTHER VIOLATIONS
9.31, "Temporary  
: 1. A review of all installed temporary modifications will be conducted to verify that acceptable standards were used for installation.
Modification  
2.* The Temporary Modification process will be reviewed to assure that adequate guidance is provided to the design engineer for providing installation instructions, arid for verifying that the temporary modification was installed as intended by the design. DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED CPCo is in full compliance. .
Control," Revision *12, Paragraph  
* 10}}
7.1.8, required that a technical  
review be conducted  
to verify that instructions  
for installation  
were correct .. Contrary to the  
On November 6, 1996, Temporary  
Modification (TM) 96-050 to the containment  
polar came did not contain correct installation  
instructions  
for replacement  
of a single solenoid with two solenoids.  
The original solenoid was*hard mounted and was provided with adequate ventilation  
to prevent premature  
failure. As the result of inadequate  
preparation  
and review, TM 96-050 did not provide instructions  
for mounting the second of the two replacement  
solenoids.  
The* second solenoid was installed  
utilizing  
duct tape and "tie-wtaps" in a manner which resulted in overheating  
and failure of the solenoid coil, and a subsequent . * electrical  
fire .. This is a Severity  
IV violation (Supplement  
1 ). CONSUMERS  
POWER COMPANY RESPONSE Consumers  
Power Company (CPCo) agrees with the violation  
as stated. REASON FOR THE VIOLATION . Based on the inspection  
data from the failed coils, the most likely cause of the failure on the trolley crane brake coils is the manner which the coils were mounted. This *inadequate  
mounting design was caused by the failure of design personnel  
to.identify  
soler:ioid  
heat dissipation  
as critical characteristic  
during the design process . 8 . -  
* Discussion . A temporary  
modification  
was required to the containment  
Polar Crane due to a failure of the existing 460VAC solenoid on the trolley brake actuator.  
No replacement  
460VAC solenoid was available.  
When this solenoid is energized, the actuator releases the braking mechanism  
on the crane trolley motor. ) The modification  
involved the replacement  
of the original 460VAC coil with 230VAC coils. One of the 230V coils would be installed  
in the position of the original coil and the second would be used as a dummy load to provide a voltage drop across it. This would result in a voltage dividing circuit which would divide the 460 volts from the circuit supply in half thus applying 230 volts across each coil. To ensure that the impedance  
w<ifs matched a spare plunger was inserted into the dummy coil and fixed in the inserted position using duct tape. The dummy coil was then tye-wrapped  
to a . support bar and additional  
tape was wrapped around it. The temporary  
modification  
to substitute  
the 230VAC coils for the 460VAC was an acceptable  
design. However, the dummy coil mounting design was focused on making sure the coil did not come loose and fall into the debris free zone inside containment.  
* . Potential  
overheating  
of the dummy coil was not considered  
in the design. The Polar Crane was in service with the temporary  
modification  
in place for approximately  
60 hours before failure occurred.  
With high usage of the Polar Crane. and repeated starts and stops on the trolley crane motor, the additional  
layers of tape on the dummy coil caused chronic overheating  
of the dummy coil. The epoxy insulating  
material became hot enough to melt and the dummy coil wires shorted togetheL This allowed the full 460 volts to be applied across the 230VAC working coil, causing its failure. The smoke and. arcing observed was the result of the dummy coil overheating, causing the duct tape to catch fire and burn. No evidence of arcing to the support structure  
was found around either coil. CORRECTIVE  
ACTIONS TAKEN AND RESULTS ACHIEVED 1. * The two 230 volt coils were replaced with a new. 460 volt coil. It has been in use *without incident since it was installed  
.. 2. This event was reviewed as a lessons learned with all Design Engineering  
at a department  
stand down meeting. Discussions  
covered conditions  
leading to the event, and the need for Design Engineering  
to consider all operating  
characteristics  
in design . 9
CORRECTIVE  
ACTIONS REMAINING  
TO BE TAKEN TO AVOID FURTHER VIOLATIONS  
1. A review of all installed  
temporary  
modifications  
will be conducted  
to verify that acceptable  
standards  
were used for installation.  
2.* The Temporary  
Modification  
process will be reviewed to assure that adequate guidance is provided to the design engineer  
for providing  
installation  
instructions, arid for verifying  
that the temporary  
modification  
was installed  
as intended by the design. DATE WHEN FULL COMPLIANCE  
WILL BE ACHIEVED CPCo is in full compliance. . * 10
}}

Revision as of 23:05, 16 August 2019

Responds to NRC 970122 Ltr Re Violations Noted in Insp Rept 50-255/96-14.Corrective actions:SPS050 Revised to Use Terminology of Operating Procedure SOP 30
ML18066A892
Person / Time
Site: Palisades 
Issue date: 02/21/1997
From: Thomas J. Palmisano
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9703030519
Download: ML18066A892 (13)


Text

consumers . Power*.*** . l'OWERIN&

llllClllliAWS l'IUlliRESS Palisades Nuclear Plant: 27780 Blue Star Memorlal Highway, Covert, Ml 49043 February 21, 1997 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 DOCKET 50-255 -LICENSE PPR-20 -PALISADES PLANT Thomas J. Palmisano Plant General Manager . RESPONSE TO NOTICE OF VIOLATION FOR TWO VIOLATIONS IN NRC . INTEGRATED INSPECTION REPORT NO. 50-255/96014(DRP)

-. ---NRC Inspection Report No. 50-255/96014(DRP) dated January 22,_1997, identified two Severity Level IV Violations of NRC requirements.

The first violation identified two examples where the plant staff did not adhere to procedures while performing outage related activities.

The second violation identified an example where adequate installation instructions were not provided for a temporary modification to the containment polar crane. response to these violations is in Attachment 1 . . . . . Consumers Power Company (CPCo) agrees to the violations as stated.

SUMMARY

OF COMMITMENTS This letter contains three new commitments and no revisions to existing commitments.

1. Periodic.activity, SPSOSO, will be revised to use the terminology of operating procedure, SOP 30, and to make the steps to align automatic transfer switch,
  • YSO, an Operations responsibility with the appropriate sign offs. . . . A review of all installed modifications will be conducted to verify tha. t J . acceptable standards were used for installation. . * -r-/ 1 . .. . . __, 2. 9703030519 970221 PDR ADOCK 05000255 G PDR Ml f HD /ID/ f MIJMI /ID A CMS ENERGY COMPANY

,. ' . 3. The Temporary Modification process will be reviewed to assure that adequate . guidance is provided to the design engineer for providing . . instructions, and for verifying that the temporary modification was installed as intended by the design.

  • Thomas J. Palmisano Plant General Manager CC
  • Administrator, Region Ill, USNRC Project Manager, NRR, USNRC NRC Resident.Inspector

-Palisades

  • Attachment
  • .. 2

. ATTACHMENT 1 CONSUMERS POWER COMPANY . PALISADES PLANT ** DOCKET 50-255 RESPONSE TO TWO VIOLATIONS FROM NRC INSPECTION

-REPO_RT 50-255/96014 (DRP)

JANUARY 22, 1997 10 Pages

.

  • RESPONSE TO-NOTICE OF VIOLATION FROM NRC INSPECTION REPORT NO. 5'?_,-255/96014(DRP)

NRG VIOLATION

1) 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings, 11 requires that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.
  • a.
  • Licensee procedure CPAL-RFM-002, Revision 0, Section 9.2.11, "Uncouple CROMs and Raise RackExtensions, 11 required in step C.4 that all CRDMs be mechanically' locked prior to ins*erting a reactor trip . into the protection system. . b. Work Order No. 24610226 and PPAC No. SPS050, "PM Auto Transfer Switch, 11 Step 11, required that operations return the isolation handle to . normal position prior to performing step .12, which required that operations return the bypass handle to automatic.

Contrary to the above, a.* On November 7, 1996, the operations shift did not ensure that the . control rod drive mechanisms were mechanically locked prior to inserting a reactor trip signal, resulting in the CROM racks dropping into **the reactor vessel upper guide structure.*

b. 'On November 17, 1996, the operations shift did not return the isolation handle to the normal position prior to returning the bypass handle to *: automatic position *. resulting in a loss of power to instrument AC bus Y-01. This is a Severity Level IV violation (Supplement

/). 1 CONSUMERS POWER COMPANY RESPONSE *Consumers-Power Company (CPCo) agrees with the violation as stated. ,REASON FOR VIOLATION Event 1a. Several factors *Contributed to this event. First, the "C" shift Control Room Supervisor and the Control Operator were not fully knowledgeable about the status of the control rod drive mechanisms.

Second, the shift turnover between "B" shift and "C" shift was inadequate in that it failed to identify the controlling procedure and it failed to discuss. the need to contact Refueling Services after Electrical maintenance was completed with -CRD #33. Third, the Control Room Supervisor and the Control Operator failed.to question the need for a-procedure and determine which procedure was governing the evolution.

  • Piscussion On November 7, 1996, preparations were being made to remove thereactor vessel* head. These preparations require.
  • 1) The uncoupling of the control rods from their drive mechanisms.
2) Raising the control rod drive racks 3) Mechanically locking .the control rod drive racks . 4) De.-energizing the control rod drive motors, clutches, and brakes by placing the reactor protection system in the "reactor.

trip" mode. On "A" shift, the Refueling Services personnel began to uncouple the control rod drives. About 1300 on "B" shift, the Refueling Ser-Vices Supervisor called the Control -Room to let the Control Room know the uncoupling was completed and Operations was requested to raise the control rod drive racks. At this time, Operations discussed the status of the uncoupling with Refueling Services and understood that the Refueling Services procedure was controlling.

Operations then withdrew forty-four of the five control rod drive racks, but problems were*encountered with CRD #33 rack. Electrical maintenance personnel assistance was requested.

While the plant electricians were repairing CRD #33, Operations turnover between "B" and '!C" shifts occurred.

During this turnover, general information concerning the control rods was . exchanged, but it was not established.that the Refueling Services procedure was controlling. "C"*shift Operations personnel did not understand that the Refueling

  • Services procedure was controlling the evolution and that Refueling Services required notification to lock the control rod drive racks after CRD#33 rack was withdrawn

.. 2

. '.

  • On "C" shift the electricians finished repairing CRD #33, withdrew the control rod drive rack and mechanically locked itin place. The Shift Supervisor, upon being notified that CRD #33 problem had been resolved and the control rod drive rack was mechanically locked, thought the next sequential step to be performed was to place the reactor protective system in the "reactor trip" mode. The Shift Supervisor did not verify the status of the control rod drive racks nor did he determine which procedure was controlling the evolution and verify that the prerequisites were met. The Shift Supervisor directed Control Room personnel to place the reactor protection system in the "reactor trip" mode. Control Room personnel observed all control rod drive racks, except CRD #33 rack, reinserting into the reactor vessel upon the reactor protection system trip initiation.

Subsequently, it was recognized that the control rod racks had not been mechanically locked when control rod #33 rack problem was encountered.

The Refueling Services procedure allowed the control rod drive racks to be l.ocked after all the racks were withdrawn.

Event 1b. The reasons for this event included inadequate understanding of the work scope, inadequate communications, inadequate work control documents and improper equipment operation.

  • Discussion
  • On November 17, 1996, the plant was in refueling shutdown conditions with shutdown cooling system in operation.

The instrument AC Bus, Y01, was being supplied from Motor Control Center 1. Y01 is critical to the operation of the shutdown cooling system as it affects shutdown cooling heat exchanger bypass and: discharge valves (CV-3006 . and CV-3025).

Earlier in the day these valves were placed on their manual hand jacks to maintain their position as instrument air was isolated and tagged for another maintenance activity.

An electrical preventative maintenance activity (PPAC) was schedul_ed for the Y01 automatic transfer switch, YSO. This required the YSO switch to be removed .from _ service so electrical maintenance personnel could remove the switch from the cabinet and take it to the electrical shop to perform the preventative maintenance.

Control Room personnel reviewed the activity but focused on the impact of this activity on the operation of the shutdown cooling system. They determined that the shutdown cooling heat exchanger bypass and discharge valves would not be affected as they were manually peing operated by the valves' hand jacks. The outage schedule stated that Operations was to "Manually align Y01 to'its normal supply". However, because all *the PPAC steps were assigned to Electrical Maintenance for completion, Operations 3

  • did not obtain a copy of the procedure to review, and failed to establish the full electrical maintenance work scope ... Subsequently, Operations decided to implement a portion of SOP 30 that configured the YSO switch from automatic to normal, but did not recognize the need to place the isolation handle to "open" (see attached sketch). This configuration fulfilled only one of two alignment steps specified in the PPAC. The Control Room Supervisor (CRS) directed an Auxiliary Operator (AO) to configure Y01 onto its normal supply using SOP 30. The AO accompanied by the System Engineering Test Coordinator (SETC) performed the alignment.

The SETC explained to the AO that not only would Y01 have to be placed on its normal power supply but, also, YSO must be isolated by moving the isolation handle to the "open" position.

At this point the AO should have contacted the.CRS for direction and permission to perform the isolation.

However, the AO did the isolation and then communicated the completion of the activity and the additional step taken to the Nuclear Control Operator (NCO). The NCO understood this message to mean that the activity was completed as directed by the CRS. Therefore, the CRS was not informed that YSO was isolated.

After the electrical mainter:iance activity was completed, the Electrician informed the Work Control Center Lead SRO that maintenance was completed and that the Electrician*

needed to be present when Operations restored the switch in order to sign. the work order steps. Also, the SETC contacted the Work Control Center and * . reque$ted that he be notified prior to the restoration activity; however, neither were contacted.

If either the Eiectrician or the SETC had been at the work site.during restoration, or if the work activity been written to have Operations sign off for . . restoration, Operations would have understood the desired position of YSO. \ . . . Work Control Center notified the Shift Lead SRO that YSO could be restored.

The Shift Lead SRO conferred with the CRS on restoring YSO, and they decided to proceed. The CRS assigned a different AO to restore YSO, informed the AO and Shift Lead SRO of the. steps he had directed the previous AO to perform, and identified the steps of SOP 30 to restore YSO.. * * * * * *

  • The Shift Lead SRO and the AO went to perform the alignment of YSO. They observed the isolation handle, the source light indication and the switch's physical position, but they did not recognize their indications were different than expected.

The AO placed the YSO bypass handle from normal to automatic.

Because the isolation handle had not been restored to the "close" position, YSO failed to transfer and Y01 was de-energized.

' l 4

,. CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED The following actions were taken. _ Event 1a. 1. Refueling and Maintenance outage activities were temporarily suspended on November 18, 1996 to review and reinforce nuclear, radiation, and industrial/personnel safety concerns with all work groups on site. This event and several other events from the first two weeks of the outage were reviewed with all crews. A common theme running among the identified issues is the lack communications between work groups and alignment among workers. *

  • 2. Three specific responsibilities were reinforced at the Operations Department stand down meetings.

These were: . " Shift Supervisors, are to identify Operations activities from the outage schedule with an understanding of the relationship between these . and others. It is intended that this understanding will contribute to well-informed decision making the Operations organization.

  • . Work Control Center Senior Reactor Operators are to direct work activities
  • having Operations involvement to Control Room personnel for authorization . .
  • This is to provide interfacing work documents physically to the individual.s . who will be performing the activity, better communications between Operations and other. work discipline*

personnel, and improve the information flow to those individuals who will be directing the activity>

  • Control. Room personnel are to assure they have a complete understanding
  • of activities requested of them and that proper alignments have been made. . . 3. . . The control rod drive blades and racks were inspected for damage due the trip occurring with a reduced water level. No damage was observed on any of the control rod drive blades or racks. *
  • Event 1b. In addition to actions 1 and 2 from above, the following actions were taken. 1. Shift Supervisor, CRS, Lead SRO, AO and other Operations personnel involved discussed this event and the barriers that could have prevented it. The 5

.. . . -discussion included responsibilities for proper communications, pre-job briefings, equipment operation, self checking and other aspects of operator ccmduct. 2. Shift Operations Supervisor has briefed the Shift Supervisors and SROs on the need to identify and conduct pre-job briefings.

The expectation to conduct . . --. job briefings whenever coordination between two or more work groups is required has been re-established.

  • 3.
  • Maintenance and Construction Manager reinforced pre-job briefing expectations with maintenance and construction supervision personnel using this event as an example where a collective pre-job briefing may have prevented the event. CORRECTIVE ACTIONS REMAINING TO BE TAKEN TO AVOID FURTHER VIOLATIONS . Periodic activity, SPS050, will be revised to use the terminology of operating ,
  • procedure, SOP 30, and to make the steps to align automatic transfer switch, YSO, an Operations responsibility with the appropriate sign offs. DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED
  • CPCo is now in full compliance.

6 Y-50 AUTOMATIC TRANSFER SWITCH I I I ! i _! -i ' I I I I I i i I .

  • EMERGENCY BYPASS HANDLE. CE ... AUTOMATIC
  • * . OfEN . *NORMAL T a.£ROENCY TCJL..IU:XX NORMAL m FAm SWITOf SOURa (KM!Nl'ARY)

SOURCE

  • AVAJl...&BIE

...... AVAILABIP

  • .. 0 11tANSFER . TE$t' LOAD (])NNECJE)

TO NORMAL * . 1t1SI' .. NORMAL

.* *1MCC#2! l , RESET ro* MCC # 1 I* I NORMAL 1*

7 . . .

  • .
  • NRC VIOLATION

.2.) 10 CFR 50, Appendix B, Criterion Ill, Design Control, requires, in part," that . design control measures " ... shall include provisions to assure that appropriate quality standards are specified and included in design documents

... ," and that " ... design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of .. design reviews. Design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design ... " Palisades Administrative Procedure 9.31, "Temporary Modification Control," Revision *12, Paragraph 7.1.8, required that a technical review be conducted to verify that instructions for installation were correct .. Contrary to the On November 6, 1996, Temporary Modification (TM)96-050 to the containment polar came did not contain correct installation instructions for replacement of a single solenoid with two solenoids.

The original solenoid was*hard mounted and was provided with adequate ventilation to prevent premature failure. As the result of inadequate preparation and review, TM 96-050 did not provide instructions for mounting the second of the two replacement solenoids.

The* second solenoid was installed utilizing duct tape and "tie-wtaps" in a manner which resulted in overheating and failure of the solenoid coil, and a subsequent .

  • electrical fire .. This is a Severity IV violation (Supplement 1 ). CONSUMERS POWER COMPANY RESPONSE Consumers Power Company (CPCo) agrees with the violation as stated. REASON FOR THE VIOLATION . Based on the inspection data from the failed coils, the most likely cause of the failure on the trolley crane brake coils is the manner which the coils were mounted. This *inadequate mounting design was caused by the failure of design personnel to.identify soler:ioid heat dissipation as critical characteristic during the design process . 8 . -
  • Discussion . A temporary modification was required to the containment Polar Crane due to a failure of the existing 460VAC solenoid on the trolley brake actuator.

No replacement 460VAC solenoid was available.

When this solenoid is energized, the actuator releases the braking mechanism on the crane trolley motor. ) The modification involved the replacement of the original 460VAC coil with 230VAC coils. One of the 230V coils would be installed in the position of the original coil and the second would be used as a dummy load to provide a voltage drop across it. This would result in a voltage dividing circuit which would divide the 460 volts from the circuit supply in half thus applying 230 volts across each coil. To ensure that the impedance w<ifs matched a spare plunger was inserted into the dummy coil and fixed in the inserted position using duct tape. The dummy coil was then tye-wrapped to a . support bar and additional tape was wrapped around it. The temporary modification to substitute the 230VAC coils for the 460VAC was an acceptable design. However, the dummy coil mounting design was focused on making sure the coil did not come loose and fall into the debris free zone inside containment.

  • . Potential overheating of the dummy coil was not considered in the design. The Polar Crane was in service with the temporary modification in place for approximately 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> before failure occurred.

With high usage of the Polar Crane. and repeated starts and stops on the trolley crane motor, the additional layers of tape on the dummy coil caused chronic overheating of the dummy coil. The epoxy insulating material became hot enough to melt and the dummy coil wires shorted togetheL This allowed the full 460 volts to be applied across the 230VAC working coil, causing its failure. The smoke and. arcing observed was the result of the dummy coil overheating, causing the duct tape to catch fire and burn. No evidence of arcing to the support structure was found around either coil. CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED 1.

  • The two 230 volt coils were replaced with a new. 460 volt coil. It has been in use *without incident since it was installed

.. 2. This event was reviewed as a lessons learned with all Design Engineering at a department stand down meeting. Discussions covered conditions leading to the event, and the need for Design Engineering to consider all operating characteristics in design . 9 CORRECTIVE ACTIONS REMAINING TO BE TAKEN TO AVOID FURTHER VIOLATIONS

1. A review of all installed temporary modifications will be conducted to verify that acceptable standards were used for installation.

2.* The Temporary Modification process will be reviewed to assure that adequate guidance is provided to the design engineer for providing installation instructions, arid for verifying that the temporary modification was installed as intended by the design. DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED CPCo is in full compliance. .

  • 10