ENS 40774: Difference between revisions
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| event date = 05/24/2004 15:00 EDT | | event date = 05/24/2004 15:00 EDT | ||
| last update date = 05/24/2004 | | last update date = 05/24/2004 | ||
| title = Degraded Condition Due | | title = Degraded Condition Due to Emergency Service Water Failure | ||
| event text = Emergency Service Water "A" (ESW ) Pump failure resulted in inoperability of all Div 1 ECCS systems at 0150 on 05/21/04 [See event notification 40767]. A plant shutdown was initiated with mode 4 [cold shutdown] achieved at 0619 on 05/23/04. During the disassembly and inspection of ESW A pump, a failed coupling on the pump shaft was found to be the cause of the failure. An Operability Determination [OD] was requested on ESW B at 1330 on 05/24/04 since both pumps had the identical coupling design and the pumps had similar run times. At 1500, the Design Engineering Manager informed the control room that engineering could not return a completed OD within the allotted time that could justify continued ESW B operability. The control room Shift Manager than declared the ESW B pump inoperable. This results in a condition that could have prevented the fulfillment of a safety function, specifically the removal of residual heat. | | event text = Emergency Service Water "A" (ESW ) Pump failure resulted in inoperability of all Div 1 ECCS systems at 0150 on 05/21/04 [See event notification 40767]. A plant shutdown was initiated with mode 4 [cold shutdown] achieved at 0619 on 05/23/04. During the disassembly and inspection of ESW A pump, a failed coupling on the pump shaft was found to be the cause of the failure. An Operability Determination [OD] was requested on ESW B at 1330 on 05/24/04 since both pumps had the identical coupling design and the pumps had similar run times. At 1500, the Design Engineering Manager informed the control room that engineering could not return a completed OD within the allotted time that could justify continued ESW B operability. The control room Shift Manager than declared the ESW B pump inoperable. This results in a condition that could have prevented the fulfillment of a safety function, specifically the removal of residual heat. | ||
The licensee notified the NRC Resident Inspector. | The licensee notified the NRC Resident Inspector. |
Latest revision as of 21:23, 1 March 2018
Where | |
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Perry Ohio (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat | |
LER: | 05000440/LER-2004-001 |
Time - Person (Reporting Time:+-1.8 h-0.075 days <br />-0.0107 weeks <br />-0.00247 months <br />) | |
Opened: | Jim Case 17:12 May 24, 2004 |
NRC Officer: | Bill Gott |
Last Updated: | May 24, 2004 |
40774 - NRC Website
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