ENS 48689: Difference between revisions

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| event date = 01/22/2013 01:13 EST
| event date = 01/22/2013 01:13 EST
| last update date = 01/22/2013
| last update date = 01/22/2013
| title = Secondary Containment Pressure Positive For 12 Seconds
| title = Secondary Containment Pressure Positive for 12 Seconds
| event text = On 01/22/2013 at 00:30 Reactor building HVAC tripped due to low outside air temperature and Standby Gas Treatment system was manually started and maintained Reactor Building differential pressure negative. At 01:13 secondary containment pressure went positive during restart of the Center Reactor Building HVAC Train. This is a loss of secondary containment function. In a 12 second time span secondary containment pressure went above 0 inches WC [Water Column] to +0.17 inches WC and then decreased to < 0 inches WC remaining stable during the Reactor Building HVAC restart. The Center Reactor Building HVAC Exhaust Fan Discharge Damper opened after the Supply Fan discharge damper; this condition would produce the indications noted.
| event text = On 01/22/2013 at 00:30 Reactor building HVAC tripped due to low outside air temperature and Standby Gas Treatment system was manually started and maintained Reactor Building differential pressure negative. At 01:13 secondary containment pressure went positive during restart of the Center Reactor Building HVAC Train. This is a loss of secondary containment function. In a 12 second time span secondary containment pressure went above 0 inches WC [Water Column] to +0.17 inches WC and then decreased to < 0 inches WC remaining stable during the Reactor Building HVAC restart. The Center Reactor Building HVAC Exhaust Fan Discharge Damper opened after the Supply Fan discharge damper; this condition would produce the indications noted.
The System was returned to normal with two Reactor Building HVAC trains running and the Standby Gas Treatment System shutdown and in standby. Reactor building pressure is stable with differential pressure negative < - 0.30 inches WC.
The System was returned to normal with two Reactor Building HVAC trains running and the Standby Gas Treatment System shutdown and in standby. Reactor building pressure is stable with differential pressure negative < - 0.30 inches WC.

Latest revision as of 21:01, 1 March 2018

ENS 48689 +/-
Where
Fermi DTE Energy icon.png
Michigan (NRC Region 3)
Reporting
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Time - Person (Reporting Time:+2.42 h0.101 days <br />0.0144 weeks <br />0.00331 months <br />)
Opened: Kelley Blenky
08:38 Jan 22, 2013
NRC Officer: Pete Snyder
Last Updated: Jan 22, 2013
48689 - NRC Website
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