ENS 51644: Difference between revisions

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| event date = 01/09/2016 02:37 CST
| event date = 01/09/2016 02:37 CST
| last update date = 01/09/2016
| last update date = 01/09/2016
| title = Automatic Reactor Scram On Main Steam Isolation Due To Electrical Fault
| title = Automatic Reactor Scram on Main Steam Isolation Due to Electrical Fault
| event text = On 1/9/16 at 0237 [CST], River Bend Station sustained a reactor scram during a lightning storm.  An electrical transient occurred resulting in a full main steam isolation [MSIV] (Group 6) and a Division II Balance of Plant isolation signal. During the scram, level 8 occurred immediately which tripped the feed pumps. A level 3 signal occurred also during the scram.  Subsequent level 3 was received three times due to isolated vessel level control. The plant was stabilized and all spurious isolation signals reset, then the MSIVs were restored.  The plant is now stable in Mode 3 and plant walkdowns are occurring to assess the transient.
| event text = On 1/9/16 at 0237 [CST], River Bend Station sustained a reactor scram during a lightning storm.  An electrical transient occurred resulting in a full main steam isolation [MSIV] (Group 6) and a Division II Balance of Plant isolation signal. During the scram, level 8 occurred immediately which tripped the feed pumps. A level 3 signal occurred also during the scram.  Subsequent level 3 was received three times due to isolated vessel level control. The plant was stabilized and all spurious isolation signals reset, then the MSIVs were restored.  The plant is now stable in Mode 3 and plant walkdowns are occurring to assess the transient.
During the scram, all rods inserted into the core. The plant was initially cooled down using safety relief valves. Offsite power is available and the plant is in its normal shutdown electrical lineup.
During the scram, all rods inserted into the core. The plant was initially cooled down using safety relief valves. Offsite power is available and the plant is in its normal shutdown electrical lineup.

Latest revision as of 20:46, 1 March 2018

ENS 51644 +/-
Where
River Bend Entergy icon.png
Louisiana (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.55 h-0.0646 days <br />-0.00923 weeks <br />-0.00212 months <br />)
Opened: Daniel Pipkin
07:04 Jan 9, 2016
NRC Officer: Howie Crouch
Last Updated: Jan 9, 2016
51644 - NRC Website
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