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| | issue date = 08/31/1994 | | | issue date = 08/31/1994 |
| | title = Informs That Util Successfully Completed Repairs of MDAFWP B on 940831.Pump Parameters as Documented in Post Maint Testing of MDAFWP B Provided in Encl.Nrc Approved Enforcement Discretion Not Required or Used | | | title = Informs That Util Successfully Completed Repairs of MDAFWP B on 940831.Pump Parameters as Documented in Post Maint Testing of MDAFWP B Provided in Encl.Nrc Approved Enforcement Discretion Not Required or Used |
| | author name = MECREDY R C | | | author name = Mecredy R |
| | author affiliation = ROCHESTER GAS & ELECTRIC CORP. | | | author affiliation = ROCHESTER GAS & ELECTRIC CORP. |
| | addressee name = MARTIN T T | | | addressee name = Martin T |
| | addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) | | | addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| | docket = 05000244 | | | docket = 05000244 |
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| =Text= | | =Text= |
| {{#Wiki_filter:i//!iirrrrrr/I/Iarrriilifr | | {{#Wiki_filter:i C 1 |
| //////////i | | //!iirrrrrr/I/Iarrriilifr |
| ///lf/Ill/8 ROCHESTER GAS AND EI ECTRIC CORPORATION | | //////////i ///lf/Ill/8 ROCHESTER GAS AND EI ECTRIC CORPORATION ~ 89 EAST AVENU@ |
| ~89 EAST AVENU@C 1 ROBERT C MECREOY Vice Preridenr Cinna Nuclear Pioduclion August 31, 1994 TELEPHONE rriiEACOOEPie 546-2TOO U.S.Nuclear Regulatory Commission Regional Administrator, Region I Mr.Thomas T.Martin 475 Allendale Road King of Prussia, PA 19406 | | ROBERT C MECREOY Vice Preridenr August 31, 1994 TELEPHONE rriiEACOOEPie 546-2TOO Cinna Nuclear Pioduclion U.S. Nuclear Regulatory Commission Regional Administrator, Region I Mr. Thomas T. Martin 475 Allendale Road King of Prussia, PA 19406 |
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| ==Subject:== | | ==Subject:== |
| Request For Enforcement Discretion R.E.Ginna Nuclear Power Plant Docket No.50-244 | | Request For Enforcement Discretion R. E. Ginna Nuclear Power Plant Docket No. 50-244 |
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| ==Reference:== | | ==Reference:== |
| | | : a. Letter from R. C. Mecredy, RG&E, to T.T. Martin, NRC, |
| a.Letter from R.C.Mecredy, RG&E, to T.T.Martin, NRC, | |
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| |
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| ==Subject:== | | ==Subject:== |
| "Request For Enforcement Discretion," dated August 30, 1994. | | "Request For Enforcement Discretion," dated August 30, 1994. |
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| ==Dear Mr.Martin,== | | ==Dear Mr. Martin,== |
| In accordance with 10 CFR Part 2, Appendix C, and using the guidance contained in NRC Inspection Manual Part 9900, RG&E had requested Enforcement Discretion on August 30, 1994 with respect to Ginna Station Technical Specification 3.4.2.1.a (Ref.a).Mls request was a contingency action in the event that necessary repairs and testing of Motor-Driven Auxiliary Feedwater (MDAFW)Pump B could not be completed within the seven day LCO limit which expired on August 31, 1994 at 0530 hours.Me requested Enforcement Discretion was verbally approved by the NRC during a phone conversation between Mr.William Lazarus NRC, Region I, and Robert Mecredy, Vice President, Nuclear Production at approximately 1720 EST on August 30, 1994.RG&E successfully completed repairs of MDAFW Pump B on August 31, 1994 at 0508 hours.The pump parameters as documented in the post maintenance testing of MDAFW Pump B are provided in Attachment A.Therefore, the LCO was exited before the expiration of the seven day LCO limit and the NRC authorized. | | |
| Enforcement Discretion was not required or used.Very ly yours, cC'obert C.Mecred XC: U.S.Nuclear Regulatory Commission Office of Nuclear Reactor Regulation Assistant Director for Region I Reactors Mr.Jose A.Calvo Washington, D.C.20555 Ginna Station Senior Resident Inspector I I 94gi030359 | | In accordance with 10 CFR Part 2, Appendix C, and using the guidance contained in NRC Inspection Manual Part 9900, RG&E had requested Enforcement Discretion on August 30, 1994 with respect to Ginna Station Technical Specification 3.4.2.1.a (Ref. a). Mls request was a contingency action in the event that necessary repairs and testing of Motor-Driven Auxiliary Feedwater (MDAFW) Pump B could not be completed within the seven day LCO limit which expired on August 31, 1994 at 0530 hours. Me requested Enforcement Discretion was verbally approved by the NRC during a phone conversation between Mr. William Lazarus NRC, Region I, and Robert Mecredy, Vice President, Nuclear Production at approximately 1720 EST on August 30, 1994. |
| ~4>02 I PDR ADDCK 05000244 P PDR ATTACHMENT A"B" Motor Driven Auxiliary Feedwater Pump Performance Data Pre-Major Maintenance Test: (Degraded Condition) | | RG&E successfully completed repairs of MDAFW Pump B on August 31, 1994 at 0508 hours. The pump parameters as documented in the post maintenance testing of MDAFW Pump B are provided in Attachment A. |
| Test Date DP (PSID)Acceptance Criteria (PSID)Flow (GPM)Vibration (Mils Disp)8/26/94 1123.2 1125.5 Inbd Outbd Vert Vert.08'10.12.14 Inbd Outbd Horiz Horiz Post-Major Maintenance Test: (Repair Completed) | | Therefore, the LCO was exited before the expiration of the seven day LCO limit and the NRC authorized. Enforcement Discretion was not required or used. |
| Test Date DP (PSID)Acceptance Criteria (PSID)Flow (GPM)Vibration (Mils Disp)8/31/94 1224.4 1125.5 200 Inbd Outbd Inbd Vert Vert Horiz.08.08.07 Outbd Horiz.09}} | | Very ly yours, C. Mecred cC'obert XC: U.S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation Assistant Director for Region I Reactors Mr. Jose A. Calvo Washington, D.C. 20555 Ginna Station Senior Resident Inspector I |
| | I 94gi030359 ~4>02 05000244 I PDR ADDCK PDR P |
| | |
| | ATTACHMENTA "B" Motor Driven Auxiliary Feedwater Pump Performance Data Pre-Major Maintenance Test: (Degraded Condition) |
| | Test Date DP (PSID) Acceptance Criteria Flow (GPM) Vibration (Mils Disp) |
| | (PSID) |
| | Inbd Outbd Inbd Outbd Vert Vert Horiz Horiz 8/26/94 1123.2 1125.5 .08 '10 .12 .14 Post-Major Maintenance Test: (Repair Completed) |
| | Test Date DP (PSID) Acceptance Criteria Flow (GPM) Vibration (Mils Disp) |
| | (PSID) |
| | Inbd Outbd Inbd Outbd Vert Vert Horiz Horiz 8/31/94 1224.4 1125.5 200 .08 .08 .07 .09}} |
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[Table view] |
Text
i C 1
//!iirrrrrr/I/Iarrriilifr
//////////i ///lf/Ill/8 ROCHESTER GAS AND EI ECTRIC CORPORATION ~ 89 EAST AVENU@
ROBERT C MECREOY Vice Preridenr August 31, 1994 TELEPHONE rriiEACOOEPie 546-2TOO Cinna Nuclear Pioduclion U.S. Nuclear Regulatory Commission Regional Administrator, Region I Mr. Thomas T. Martin 475 Allendale Road King of Prussia, PA 19406
Subject:
Request For Enforcement Discretion R. E. Ginna Nuclear Power Plant Docket No. 50-244
Reference:
- a. Letter from R. C. Mecredy, RG&E, to T.T. Martin, NRC,
Subject:
"Request For Enforcement Discretion," dated August 30, 1994.
Dear Mr. Martin,
In accordance with 10 CFR Part 2, Appendix C, and using the guidance contained in NRC Inspection Manual Part 9900, RG&E had requested Enforcement Discretion on August 30, 1994 with respect to Ginna Station Technical Specification 3.4.2.1.a (Ref. a). Mls request was a contingency action in the event that necessary repairs and testing of Motor-Driven Auxiliary Feedwater (MDAFW) Pump B could not be completed within the seven day LCO limit which expired on August 31, 1994 at 0530 hours0.00613 days <br />0.147 hours <br />8.763227e-4 weeks <br />2.01665e-4 months <br />. Me requested Enforcement Discretion was verbally approved by the NRC during a phone conversation between Mr. William Lazarus NRC, Region I, and Robert Mecredy, Vice President, Nuclear Production at approximately 1720 EST on August 30, 1994.
RG&E successfully completed repairs of MDAFW Pump B on August 31, 1994 at 0508 hours0.00588 days <br />0.141 hours <br />8.399471e-4 weeks <br />1.93294e-4 months <br />. The pump parameters as documented in the post maintenance testing of MDAFW Pump B are provided in Attachment A.
Therefore, the LCO was exited before the expiration of the seven day LCO limit and the NRC authorized. Enforcement Discretion was not required or used.
Very ly yours, C. Mecred cC'obert XC: U.S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation Assistant Director for Region I Reactors Mr. Jose A. Calvo Washington, D.C. 20555 Ginna Station Senior Resident Inspector I
I 94gi030359 ~4>02 05000244 I PDR ADDCK PDR P
ATTACHMENTA "B" Motor Driven Auxiliary Feedwater Pump Performance Data Pre-Major Maintenance Test: (Degraded Condition)
Test Date DP (PSID) Acceptance Criteria Flow (GPM) Vibration (Mils Disp)
(PSID)
Inbd Outbd Inbd Outbd Vert Vert Horiz Horiz 8/26/94 1123.2 1125.5 .08 '10 .12 .14 Post-Major Maintenance Test: (Repair Completed)
Test Date DP (PSID) Acceptance Criteria Flow (GPM) Vibration (Mils Disp)
(PSID)
Inbd Outbd Inbd Outbd Vert Vert Horiz Horiz 8/31/94 1224.4 1125.5 200 .08 .08 .07 .09