05000321/LER-1980-023-03, /03L-0:on 800224,during Startup W/Mode Switch in Startup & Hot Standby,Hpci Sys Did Not Become Operational at 133 Psig Per Tech Specs.Caused by Design Deficiency & Instrument Drift.Pressure Switches Recalibr: Difference between revisions

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{{Adams
#REDIRECT [[05000321/LER-1980-023-03, Hpic Did Not Actuate Until Tech Spec Limit Passed.Caused by Instrument Drift. Switches Calibr & Necessary Design Changes Will Be Implemented]]
| number = ML19312D182
| issue date = 03/10/1980
| title = /03L-0:on 800224,during Startup W/Mode Switch in Startup & Hot Standby,Hpci Sys Did Not Become Operational at 133 Psig Per Tech Specs.Caused by Design Deficiency & Instrument Drift.Pressure Switches Recalibr
| author name = Nix R
| author affiliation = GEORGIA POWER CO.
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| docket = 05000321
| license number =
| contact person =
| document report number = LER-80-023-03L-01, LER-80-23-3L-1, NUDOCS 8003210416
| package number = ML19312D181
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 2
}}
{{LER
| Title = /03L-0:on 800224,during Startup W/Mode Switch in Startup & Hot Standby,Hpci Sys Did Not Become Operational at 133 Psig Per Tech Specs.Caused by Design Deficiency & Instrument Drift.Pressure Switches Recalibr
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000321
| LER year = 1980
| LER number = 23
| LER revision = 3
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
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LICENSEE EVENT REPORT g
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60 61 OOCKET NUMBER E.3 trJ EVENT DATE 74 75 HEPOf t T DATE 41 0 EVENT DESCRIPTION AND PRODADLE CONSEQUENCES h o 2 l During Reactor startup with the mode switch in startup_nnd hot standby.
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the llPCI system did not become operational at 113'psig as specified in l
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Technical Specifications 3.5-0.1.
The system was not operational l
.h O s l until 127 psig. There were no ef fects upon public health and safety due l
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l0 lij l Reportable Occurrened Report No. 50-321/1979-106.
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40 el 42 43 44 47 CAUSE DESCniPTION ANDCORRECTIVE ACTIONS h gl This failure is due to a design deficiency and instrument drift. The l
1111 l l Present design does not allow a trip'at 100 psig and reset at 113 paig.
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The pressure switches were recalibrated to specifications. Future cor-l i 3 l
rective action includes a design change to the pressure switchen and the l
;3 l4 g l pursuit of a document change to the present Tech Specs.
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; NARRATIVE REPORT-M w
:Ceorgia Pober. Company;
< Plant. E. " I., llatch ;
Baxley,1 Georgia.31513)
: Reportable -. Occurrence Report No. 321/1980-23.
DuringEreactor startup with' the mode switch in. startup' and hot standby position,
:the IIPCI System did nor -becomo operational: at 113 psig 'as specified in Technical
- (Specifications Section 3.5.D.'1.
There were no effects upon public health and
~
r safety'duetto.this event. This is a repetit!1ve occurrence as last _ reported on Reportabic Oclcurrene,c - Report. No. 321/1979 106. This report addressed i
the problem of IIPCI Lisointing at 116' psig. Tachnical Specification Section 3.5-D.1 requires that 11PCI be operational:if.the reactor pressure is greater thanill3Lpsig. Prior 'to LER.50-321/1979-106, the switches, IE41-N001A-D, setpoint was:125 poig. '-This setpoint complied with Tech Specs requirement Table 3.2.2 which requires the switches to be set equal to or greater than 1000psigi sbut ;does not comply ~ with Tech Specs Section. 3.5-D.1 which required.
_'llPCI tolhe. operational rt 113 psig. The inherent: prob 1cm was first recognized at.'this point. A' design change-was submitted to change the netpoint to a'value 6
greaterithan'100 psig but Icos than 113 psig.
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.On February 24,1980' 11PCI'did not become operational at reactor pressure c qual to 'or; greater. than ' 113 psig. The calibration of the llPCI Steam Line
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c Low Pressure Switches was checked and found as follows:-
N001A. trip 90.7' psi, reset 127.7 psi.
~ N001B trip 98.7 psi,. reset.123.7 pai.
;N001C trip 100.7 psi, reset.13'2.7 psi.
:N001D.LYip 98.7 pai, reset 123.7 psi.
1Three of the-switches A,' B and D were found below the acceptance criteria
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~ of' actuation ~at - greater thmi 100 psig.: The exoccted actuation point is
'The dif ference' between the ' expected actuation and the L'
:- 10. 5 - c5. psi.
6 Jactual trip point is attributed to instrument setpoint drift.
i 1The manufacturer of these switches is Darksdale.. The' specifications of-the
('
switch permit-a react span different'.alc of 11 to 40 psig and.is not adjustabic.
Decause of the wide differential, the switches cannot be adjusted to meet the Spresent Tech Spec requirements.-
;The planned eorrective;" action willIinclude t!io following.: A design: change to T
A','
;the pressure switches to meet the Technical Specification requirements.is being e
g Jinvestigatedh. Unit.II Tdchnical, Specifi' cations (Standard Tech Specs)- require 3
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s ithat -11PCI be' operational at pressures cqual'to or greater than 150 psig.' AJ fe$;
< proposal"to' change Unit [I Tech ' Specs concerning 11PCI:to Standard Tech Specs 'is sq.
*Theing7 investigated. : A follow-up. report will be submitted.z
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Latest revision as of 11:12, 26 May 2025