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{{#Wiki_filter:.        *
{{#Wiki_filter:*
        -
.
                    4                                      UNITED STATES
g((>Q0800
    g((>Q0800           o
-
                                          NUCLEAR REGULATORY COMMISSION
4
    n .
UNITED STATES
    g                   E-                                   REGION IV
NUCLEAR REGULATORY COMMISSION
    %
n .
      #'+9
o
            *****
g
                      /[                         611 RYAN PLAZA DRIVE, SUITE 400
E-
                                                      AR UNGTON, TEXAS 760114064
REGION IV
                                                          g       g 1998
%
l                                                                                                                       k
#'+9
                                                                                                                        i
/[
              John R. McGaha, Vice President - Operations
611 RYAN PLAZA DRIVE, SUITE 400
              River Bend Station
AR UNGTON, TEXAS 760114064
              Entergy Operations, Inc.
*****
!             P.O. Box 220
g
              St. Francisville, Louisiana 70775
g 1998
!             SUBJECT: NRC INSPECTION REPORT 50-458/98-04
l
              Dear Mr. McGaha:
k
                        Thank you for your letter of April 3,1998, in response to our letter and Notice of Violation
John R. McGaha, Vice President - Operations
              dated March 19,1998. We have reviewed your reply and find it responsive to the concerns
River Bend Station
              raised in our Notice of Violation involving inadequate procedural guidance to maintain control of
Entergy Operations, Inc.
              the position of a maintenance Jacking device on a primary containment purge isolation valve.
!
              We will review the implementation of your corrective actions during a future inspection to
P.O. Box 220
              determine that full compliance has been achieved and will be maintained.
St. Francisville, Louisiana 70775
                                                                Sincerely.
!
                                                                                -     e
SUBJECT: NRC INSPECTION REPORT 50-458/98-04
                                                                              j'       1
Dear Mr. McGaha:
                                                                    N               /
Thank you for your letter of April 3,1998, in response to our letter and Notice of Violation
                                                                Elmo E. Collins, Chief
dated March 19,1998. We have reviewed your reply and find it responsive to the concerns
                                                                Project Branch C
raised in our Notice of Violation involving inadequate procedural guidance to maintain control of
                                                                Division of Reactor Projects                         1-
the position of a maintenance Jacking device on a primary containment purge isolation valve.
              Docket No.: 50-458
We will review the implementation of your corrective actions during a future inspection to
          ' ' License No.: NPF-47                                                                   .
determine that full compliance has been achieved and will be maintained.
              cc:
Sincerely.
              Executive Vice President and
-
                Chief Operating Officer
e
              Entergy Operations, Inc.                                                                     j
j'
h           ' P.O. Box 31995 -
1
                                                                                                              {(
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  .
/
              Jackson, Mississippi 39286-1995
Elmo E. Collins, Chief
            9804130216 900409                     a"
Project Branch C
            PDR       ADOCK 05000458
Division of Reactor Projects
            G                       PDR
1-
                                                                                                                        i
Docket No.: 50-458
                                                                                                                        )
' ' License No.: NPF-47
.
cc:
Executive Vice President and
Chief Operating Officer
Entergy Operations, Inc.
j
{(
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' P.O. Box 31995 -
.
Jackson, Mississippi 39286-1995
9804130216 900409
a"
PDR
ADOCK 05000458
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PDR
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                                                      i
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    1   .
1
                                                    l
.
          ' Entergy Operations, Inc.           -2-
l
            Vice President
' Entergy Operations, Inc.
            Operations Support
-2-
            Entergy Operations, Inc.
Vice President
          ~ P.O. Box 31995
Operations Support
!           Jackson, Mississippi 39286-1995             i
Entergy Operations, Inc.
                                                        1
~ P.O. Box 31995
            General Manager                             I
!
          ' Plant Operations -
Jackson, Mississippi 39286-1995
            River Bend Station
i
            Entergy Operations, Inc.
1
            P.O. Box 220
General Manager
            St. Francisville, Louisiana 70775
' Plant Operations -
            Director- Nuclear Safety
River Bend Station
          . River Bend Station
Entergy Operations, Inc.
            Entergy Operations, Inc.-
P.O. Box 220
            P.O. Box 220                                 i
St. Francisville, Louisiana 70775
            St. Francisville, Louisiana 70775           j
Director- Nuclear Safety
            Wise, Carter, Child & Caraway
. River Bend Station
            P.O. Box 651
Entergy Operations, Inc.-
            Jackson, Mississippi 39205
P.O. Box 220
          - Mark J. Wetterhahn, Esq.-                   1
i
            Winston & Strawn                           !
St. Francisville, Louisiana 70775
            1401 L Street, N.W.                         l
j
            Washington, D.C. 20005-3502 -               1
Wise, Carter, Child & Caraway
                                                        !
P.O. Box 651
          : Manager - Licensing -
Jackson, Mississippi 39205
                                                        l
- Mark J. Wetterhahn, Esq.-
  '
1
          ! River Bend Station -                         !
Winston & Strawn
          - Entergy Operations, Inc.
1401 L Street, N.W.
            P.O. Box 220 :-
Washington, D.C. 20005-3502 -
            St. Francisville Louisiana 70775
1
                -
: Manager - Licensing -
                                                        i
! River Bend Station -
          . The Honorable Richard P. leyoub-
'
            Attorney General .                     -
- Entergy Operations, Inc.
                                                        '
P.O. Box 220 :-
      ,
St. Francisville Louisiana 70775
          . Department of Justice                   .
-
                                                        '
i
          ' State of Louisiana
. The Honorable Richard P. leyoub-
            P.O. Box 94005                               1
Attorney General .
            Baton Rouge, Louisiana .70804-9005           ;
-
            H.~ Anne Plettinger                         i
'
            3456 Villa Rose Drive     ~
. Department of Justice
          .. Baton Rouge, Louisiana 70806               l
.
h                                                       ;
,
' State of Louisiana
'
P.O. Box 94005
1
Baton Rouge, Louisiana .70804-9005
H.~ Anne Plettinger
i
3456 Villa Rose Drive
.. Baton Rouge, Louisiana 70806
~
h
;
p
p
                                                        ,
,


                                  .
.
      .     .
.
                Entergy. Operations, Inc.               -3-
.
          '
Entergy. Operations, Inc.
    >
-3-
                President of West Feliciana
'
                Police Jury ~                                     8
President of West Feliciana
              - P.O. Box 1921
>
              ' St. Francisville, Louisiana 70775   ,
Police Jury ~
      '                                                       '
8
                William H. Spell, Administrator
- P.O. Box 1921
                Louisiana Radiation Protection Division
' St. Francisville, Louisiana 70775
                P.O. Box 82135
,
                Baton Rouge, Louisiana 70884-2135
'
;/-     ,
'
                                                                    1
William H. Spell, Administrator
                                                                    i
Louisiana Radiation Protection Division
P.O. Box 82135
Baton Rouge, Louisiana 70884-2135
;/-
,
1
i
l
l
l
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          Entergy Operations, Inc.                                   -4"
. ..
                                                                                                            APR - 9 1998
.
l
Entergy Operations, Inc.
-4"
APR - 9 1998
._
._
          bec to DCD (IE01)
bec to DCD (IE01)
l-
l-
L.       bec distrib. by RIV:
L.
          Regional Administrator                       . Senior Resident inspector (Grand Gulf)
bec distrib. by RIV:
          DRP Director                                   DRS-PSB
Regional Administrator
          Branch Chief (DRP/C)                           MIS System
. Senior Resident inspector (Grand Gulf)
l         Project Engineer (DRP/C)                       RIV File
DRP Director
          Branch Chief (DRP/TSS)                         Resident inspector
DRS-PSB
Branch Chief (DRP/C)
MIS System
l
Project Engineer (DRP/C)
RIV File
Branch Chief (DRP/TSS)
Resident inspector
l
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!
!
                                                                                                                            i
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                                                                                                                            !
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!.
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l         DOCUMENT NAME: R:\_RB\RB804AK.GDR
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          To recohe copy of documant, inacate in box: "C" = Copy without enclosures "E" = Copy with enclosures "N" = No copy ,
DOCUMENT NAME: R:\\_RB\\RB804AK.GDR
          RIV:DRP/C                                                                                                         l
To recohe copy of documant, inacate in box: "C" = Copy without enclosures "E" = Copy with enclosures "N" = No copy
                                        C:DI)ff/9 -
,
          PJAlter:df       b         EECMtf(df
RIV:DRP/C
          4/ 7 /98           #         4/G /98
C:DI)ff/9 -
                                                    OFFICIAL RECORD COPY
l
                                                                                                                              !
PJAlter:df
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4/ 7 /98
#
4/G /98
OFFICIAL RECORD COPY


  .. .                                                                                                                     ..
..
.
..
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        Entergy Operations, Inc.                                 -4-                                     APR - 9 1998
Entergy Operations, Inc.
                                                                                                                              i
-4-
                                ..                                                                                            8
APR - 9 1998
        bec distrib. by RIV:
        Regional Administrator                        Senior Resident inspector (Grand Gulf)
        DRP Director                                  DRS-PSB
        Branch Chief (DRP/C)                          MIS System                                                            '
      ' Project Engineer (DRP/C)                      RIV File
        Branch Chief (DRP/TSS)                        Resident inspector
                                                                                                                .
i
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..
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bec distrib. by RIV:
Regional Administrator
Senior Resident inspector (Grand Gulf)
DRP Director
DRS-PSB
' Project Engineer (DRP/C)
RIV File
'
Branch Chief (DRP/C)
MIS System
Branch Chief (DRP/TSS)
Resident inspector
.
i
DOCUMENT NAME: R:\\_RB\\RB804AK.GDR
:
:
'
'
        DOCUMENT NAME: R:\_RB\RB804AK.GDR
To receive copy of document, Indicate in box:"C" = Copy w'Aout enclosures "E" = Copy with enclosures "N" s No copy
        To receive copy of document, Indicate in box:"C" = Copy w'Aout enclosures "E" = Copy with enclosures "N" s No copy
'
                                                            '
lRIV:DRP/C
        lRIV:DRP/C                   C:DfW)/9                                                                                 l
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                              '
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        l4/ / /98                     4/9 /98
EEC3 fin (df
                                                    OFFICIAL RECORD COPY
l4/ / /98
                130012
'
                                                                                                                              I
4/9 /98
OFFICIAL RECORD COPY
130012


                                                                                        Entergy operations. Inc.
Entergy operations. Inc.
  *  *                                                                                  A '.e' Berc S a: cc
A '.e' Berc S a: cc
                                                                                        EaB5 0 5 e grnar V
*
    .O .                                                                               DO Bce 220
*
EaB5 0 5 e grna V
r
.O .
DO Bce 220
..
..
  '
y
              y                                                                          5: Pace s.me LA 'S??5
5: Pace s.me LA 'S??5
                                                                                        Te. 504 336 6225
'
                                                                                        Ca 504 635 5C68
Te. 504 336 6225
                                                                                        Rick J. King
Ca 504 635 5C68
                                                                                        : *e:'or
Rick J. King
                                                                                        %TeF $4'ety & Negs dX's 4''J 's
: *e:'or
                              .
%TeF $4'ety & Negs dX's 4''J 's
            April 3,1998
.
            U.S. Nuclear Regulatory Commission
April 3,1998
            Document Control Desk, OPI-17                                                                               i
U.S. Nuclear Regulatory Commission
            Washington, DC 20555
Document Control Desk, OPI-17
                                                                                                                        l
i
                                                                                                                          l
Washington, DC 20555
                                                                                                                          '
Subject:
            Subject:     Reply to Notice of Violation in IR 98-004
Reply to Notice of Violation in IR 98-004
                          River Bend Station - Unit I
'
                          License No. NPF-47
River Bend Station - Unit I
                          Docket No. 50-458                                       dfA   ,
License No. NPF-47
            File Nos.:   G9.5,G15.4.1                                 j%                                               I
Docket No. 50-458
                                                                                                  'N
dfA
            RBG-44445                                                                                                 ;
,
            RBF1-98-0072
File Nos.:
            Gentlemen:
G9.5,G15.4.1
            Pursuant to the provisions of 10CFR2.201, Attachment A provides the Entergy
j%
            Operations, Inc. response to the Notice of Violation (NOV) described in NRC Inspection
I
            Report (IR) 50-458/98-004.                 '
'N
            The subject violation,50-458/98004-02, involves inadequate procedural guidance to
RBG-44445
            maintain control of the position of an attached maintenance jacking device on a primary
;
            containment purge valve.
RBF1-98-0072
                                                                                                                          !
Gentlemen:
            Should you have any questions regarding the attached information, please contact Mr.                         j
Pursuant to the provisions of 10CFR2.201, Attachment A provides the Entergy
            David Lorfing of my staff at (504) 381-4157.
Operations, Inc. response to the Notice of Violation (NOV) described in NRC Inspection
                                                                                                                        1
Report (IR) 50-458/98-004.
            Sincerely,
'
            ' hth c         (L n     'N                                                                                 l
The subject violation,50-458/98004-02, involves inadequate procedural guidance to
            bK/MGM                                                                                                       ;
maintain control of the position of an attached maintenance jacking device on a primary
            attachment
containment purge valve.
                                                                                                                          4
Should you have any questions regarding the attached information, please contact Mr.
                                                        ss-us t
j
    &[\500\ \
David Lorfing of my staff at (504) 381-4157.
          .
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                                  ~
Sincerely,
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bK/MGM
attachment
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                                                        1
1
      '
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  . ..   .
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,   g,
. ..
  .
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          Reply to Notice of Violation in 50-458/98-004
,
          April 3,1998
.
          RBG-44445
Reply to Notice of Violation in 50-458/98-004
          RBF1-98-0072
April 3,1998
          Page 2 0f 2
RBG-44445
          cc:     U.S. Nuclear Regulatory Commission
RBF1-98-0072
                    Region IV                           ;
Page 2 0f 2
                    611 Ryan Plaza Drive, Suite 400
cc:
                    Arlington,TX 76011
U.S. Nuclear Regulatory Commission
                  NRC Sr. Resident Inspector
Region IV
                    P.O. Box 1050
;
                    St. Francisville, LA 70775
611 Ryan Plaza Drive, Suite 400
                    David Wigginton
Arlington,TX 76011
                  ' NRR Project Manager
NRC Sr. Resident Inspector
                  U.S. Nuclear Regulatory Commission
P.O. Box 1050
                  M/S OWFN 13-H-3
St. Francisville, LA 70775
                - Washington, DC 20555                   l
David Wigginton
                                                          i
' NRR Project Manager
                                                        I
U.S. Nuclear Regulatory Commission
                                                          :
M/S OWFN 13-H-3
                                                        -
- Washington, DC 20555
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                                                        ATTACHMENT A
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                                    REPLY TO NOTICE OF VIOLATION 50-458/98004-02
ATTACHMENT A
l                                                           Page1of2
REPLY TO NOTICE OF VIOLATION 50-458/98004-02
!                 Violation:
l
?               . During an NRC inspection conducted on January 11 through February 21,1998, one
Page1of2
                  violation of NRC requirements was identified. In accordance with the " General
!
                  Statement of Policy and Procedure for NRC Enforcement Actions," NUREG-1600, the
Violation:
                                                                                        -
?
                ' violation is listed below:
. During an NRC inspection conducted on January 11 through February 21,1998, one
                            10 CFR Part 50, Appendix B, Criterion V, states, in part, " Activities affectir's
violation of NRC requirements was identified. In accordance with the " General
                            quality shall be prescribed by documented instructions, procedures, or drawings of
Statement of Policy and Procedure for NRC Enforcement Actions," NUREG-1600, the
                            a type appropriate to the circumstances and shall be accomplished in accordance
-
                            with these instructions, procedures, or drawings . . ."
' violation is listed below:
:                           Matryx Company Drawing Number 410318, dated October 10,1980, required               i
10 CFR Part 50, Appendix B, Criterion V, states, in part, " Activities affectir's
                                                                                                                !
quality shall be prescribed by documented instructions, procedures, or drawings of
l                          that the pump release screws (petcock valves) be positioned one tum
a type appropriate to the circumstances and shall be accomplished in accordance
!                           counterclockwise (open) when operating containment ventilation and purge
with these instructions, procedures, or drawings . . ."
l                           Dampers HVR-AOV-128, HVR-AOV-165, and HVR-AOV-166 in the pneumatic
:
Matryx Company Drawing Number 410318, dated October 10,1980, required
i
l
that the pump release screws (petcock valves) be positioned one tum
!
!
counterclockwise (open) when operating containment ventilation and purge
l
Dampers HVR-AOV-128, HVR-AOV-165, and HVR-AOV-166 in the pneumatic
l.
l.
mode (safety-related mode). This drawing was the only document that specified
'
'
                            mode (safety-related mode). This drawing was the only document that specified
' the position of the petcock valves.
                          ' the position of the petcock valves.
l-
l-                         Contrary to the above, on January 8,1998, the petcock valves for Dampers HVR-
Contrary to the above, on January 8,1998, the petcock valves for Dampers HVR-
L                         . AOV-128, HVR-AOV-165, and HVR-AOV-166 were found full closed, but the
L
                            dampers had been operated in the pneumatic mode. Controls to ensure that the         i
. AOV-128, HVR-AOV-165, and HVR-AOV-166 were found full closed, but the
                            valves were correctly positioned were inadequate.
dampers had been operated in the pneumatic mode. Controls to ensure that the
l                          This is a Severity Level IV violation (Supplement 1)(50-458/9804-02).
i
l                Reasons for the Violation:
valves were correctly positioned were inadequate.
                  River Bend Station has four containment purge dampers, functioning as primary
L                containment isolation barriers, which are fitted with attached hydraulic jacking devices.
l
l
                  These devices can be used to open the dampers during maintenance or abnormal
This is a Severity Level IV violation (Supplement 1)(50-458/9804-02).
                operating conditions. The petcock valves, when closed, allow hydraulic pressure to be
l
                - developed for operation of these jacking devices. The petcocks are opened to disable
Reasons for the Violation:
                thesejacks thereby allowing normal pneumatic operation of the dampers.
River Bend Station has four containment purge dampers, functioning as primary
                  A root cause investigaticu was conducted, with two primary causes identified.
L
                The first primary cause was related to the area of configuration conul in that there were
containment isolation barriers, which are fitted with attached hydraulic jacking devices.
                  inadequate administrative controls established to ensure that the attacned hydraulic
l
                jacking assembly would not interfere with pneumatic operation of the damper. The
These devices can be used to open the dampers during maintenance or abnormal
                  correct restoration position of the petcocks (i.e., one turn open) should have been
operating conditions. The petcock valves, when closed, allow hydraulic pressure to be
                  identified and controlled. If the position had been controlled, the petcocks would have
- developed for operation of these jacking devices. The petcocks are opened to disable
                  been restored to the correct position upon completion of maintenance activities.
thesejacks thereby allowing normal pneumatic operation of the dampers.
                                                                                                              ,
A root cause investigaticu was conducted, with two primary causes identified.
The first primary cause was related to the area of configuration conul in that there were
inadequate administrative controls established to ensure that the attacned hydraulic
jacking assembly would not interfere with pneumatic operation of the damper. The
correct restoration position of the petcocks (i.e., one turn open) should have been
identified and controlled. If the position had been controlled, the petcocks would have
been restored to the correct position upon completion of maintenance activities.
,
l
l
.
.


      i,f*,e
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      *
l
l
*
l
ATTACHMENT A
REPLY TO NOTICE OF VIOLATION 50-458/98004-02
o
. Page 2 of 2 '
L
L
The second primary cause was related to the area of work organization and planning in
l
l
                                                      ATTACHMENT A
that work package preparation was inadequate as related to this event. . The last
                                REPLY TO NOTICE OF VIOLATION 50-458/98004-02
documented maintenance involving steps during which personnel may have manipulated
o                                                          . Page 2 of 2 '
'
the petcocks was performed in June of 1994. There was no step in the job plans directing
,
the workers to return the petcocks to the open position upon completion of the work.
{
Corrective Actions That Have Been Taken:
.l
[
To maintain administrative control over the open position, as depicted on Matryx
Company Drawing Number 410318, dated October 10,1980:
.!
the petcocks on'all four purge dampers were lockwired one turn open;
;
e
L
L
L              The second primary cause was related to the area of work organization and planning in
the four lockwired petcocks were fitted with conspicuous labels to direct personnel to
l              that work package preparation was inadequate as related to this event. . The last
e
'
'
                documented maintenance involving steps during which personnel may have manipulated
maintain that position; and1
                the petcocks was performed in June of 1994. There was no step in the job plans directing          ,
l
                the workers to return the petcocks to the open position upon completion of the work.
the applicable Work Management Screens for the purge dampers were updated with a
                                                                                                                {
e
                Corrective Actions That Have Been Taken:                                                        .l
L
[              To maintain administrative control over the open position, as depicted on Matryx                  l
reference note to direct that future job plans contain instructions for the petcocks to be
                Company Drawing Number 410318, dated October 10,1980:                                          .!
;
;              e    the petcocks on'all four purge dampers were lockwired one turn open;
i.
L              e    the four lockwired petcocks were fitted with conspicuous labels to direct personnel to
lockwired one tum open prior to returning the dampers to service.
            '
j
                    maintain that position; and1
I
l               e    the applicable Work Management Screens for the purge dampers were updated with a
.To address the generic implications:
L                   reference note to direct that future job plans contain instructions for the petcocks to be   ;
regarding other pneumatic opetated valves that serve as primary containment isolation
i.                   lockwired one tum open prior to returning the dampers to service.                         j
e
                                                                                                                  I
valves and are included in the Local Leak Rate Testing Program, a review was
              .To address the generic implications:
conducted finding no other valves fitted with similarly uncontrolled subcomponents
                e    regarding other pneumatic opetated valves that serve as primary containment isolation
                    valves and are included in the Local Leak Rate Testing Program, a review was
                    conducted finding no other valves fitted with similarly uncontrolled subcomponents
L
L
that could affect operation;
'
'
                    that could affect operation;
1
                                                                                                                  1
regarding other plant components, maintenance personnel and system engmeers were
                e    regarding other plant components, maintenance personnel and system engmeers were             i
i
                    briefed on this event, stressing the need to identify configurations that could result m     !
e
                    similar events; and                                                                         I
briefed on this event, stressing the need to identify configurations that could result m
                                                    .                                                           i
similar events; and
                e    regarding other plants, the details of this event were distributed through the Institute
.
                    for Nuclear Power Operation (INPO) Nuclear Network for review by other plants,               j
i
l                                                                                                                 I
regarding other plants, the details of this event were distributed through the Institute
                Corrective Actions That Will Be Taken to Avoid Further Violations:
e
for Nuclear Power Operation (INPO) Nuclear Network for review by other plants,
j
l
'
'
                The applicable operating procedure will be revised to invoke procedural control over
Corrective Actions That Will Be Taken to Avoid Further Violations:
              . retuming the locked open petcock valves to their proper condition after operation.
The applicable operating procedure will be revised to invoke procedural control over
                Preventive maintenance tasks and other standardized maintenance job plans will be               i
. retuming the locked open petcock valves to their proper condition after operation.
                revised to include a specific restoration step for the petcocks where applicable.               ]
Preventive maintenance tasks and other standardized maintenance job plans will be
                Date When Full Compliance Will Be Aebieved:                                                     !
i
                Ad, equate control was achieved upon lockwiring the petcocks open and conspicuously             :
revised to include a specific restoration step for the petcocks where applicable.
                labeling their correct position. Full compliance will be achieved by June 30,1998.               i
]
                                                                                                                  i
Date When Full Compliance Will Be Aebieved:
                                                                                                                  !
Ad, equate control was achieved upon lockwiring the petcocks open and conspicuously
labeling their correct position. Full compliance will be achieved by June 30,1998.
i
i
I
I
                                                                              '
'
                  -                                                                                             ,
-
  ..
,
..
}}
}}

Latest revision as of 03:27, 23 May 2025

Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-458/98-04 on 980319
ML20217Q883
Person / Time
Site: River Bend Entergy icon.png
Issue date: 04/09/1998
From: Collins E
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To: Mcgaha J
ENTERGY OPERATIONS, INC.
References
50-458-98-04, 50-458-98-4, NUDOCS 9804130216
Download: ML20217Q883 (5)


See also: IR 05000458/1998004

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

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REGION IV

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611 RYAN PLAZA DRIVE, SUITE 400

AR UNGTON, TEXAS 760114064

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John R. McGaha, Vice President - Operations

River Bend Station

Entergy Operations, Inc.

!

P.O. Box 220

St. Francisville, Louisiana 70775

!

SUBJECT: NRC INSPECTION REPORT 50-458/98-04

Dear Mr. McGaha:

Thank you for your letter of April 3,1998, in response to our letter and Notice of Violation

dated March 19,1998. We have reviewed your reply and find it responsive to the concerns

raised in our Notice of Violation involving inadequate procedural guidance to maintain control of

the position of a maintenance Jacking device on a primary containment purge isolation valve.

We will review the implementation of your corrective actions during a future inspection to

determine that full compliance has been achieved and will be maintained.

Sincerely.

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Elmo E. Collins, Chief

Project Branch C

Division of Reactor Projects

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Docket No.: 50-458

' ' License No.: NPF-47

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Executive Vice President and

Chief Operating Officer

Entergy Operations, Inc.

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Jackson, Mississippi 39286-1995

9804130216 900409

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Vice President

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Entergy Operations, Inc.

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Jackson, Mississippi 39286-1995

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General Manager

' Plant Operations -

River Bend Station

Entergy Operations, Inc.

P.O. Box 220

St. Francisville, Louisiana 70775

Director- Nuclear Safety

. River Bend Station

Entergy Operations, Inc.-

P.O. Box 220

i

St. Francisville, Louisiana 70775

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Wise, Carter, Child & Caraway

P.O. Box 651

Jackson, Mississippi 39205

- Mark J. Wetterhahn, Esq.-

1

Winston & Strawn

1401 L Street, N.W.

Washington, D.C. 20005-3502 -

1

Manager - Licensing -

! River Bend Station -

'

- Entergy Operations, Inc.

P.O. Box 220 :-

St. Francisville Louisiana 70775

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. The Honorable Richard P. leyoub-

Attorney General .

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. Department of Justice

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' State of Louisiana

'

P.O. Box 94005

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Baton Rouge, Louisiana .70804-9005

H.~ Anne Plettinger

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3456 Villa Rose Drive

.. Baton Rouge, Louisiana 70806

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Entergy. Operations, Inc.

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President of West Feliciana

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' St. Francisville, Louisiana 70775

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William H. Spell, Administrator

Louisiana Radiation Protection Division

P.O. Box 82135

Baton Rouge, Louisiana 70884-2135

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DOCUMENT NAME: R:\\_RB\\RB804AK.GDR

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DOCUMENT NAME: R:\\_RB\\RB804AK.GDR

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OFFICIAL RECORD COPY

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Entergy operations. Inc.

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April 3,1998

U.S. Nuclear Regulatory Commission

Document Control Desk, OPI-17

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Washington, DC 20555

Subject:

Reply to Notice of Violation in IR 98-004

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River Bend Station - Unit I

License No. NPF-47

Docket No. 50-458

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File Nos.:

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RBG-44445

RBF1-98-0072

Gentlemen:

Pursuant to the provisions of 10CFR2.201, Attachment A provides the Entergy

Operations, Inc. response to the Notice of Violation (NOV) described in NRC Inspection

Report (IR) 50-458/98-004.

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The subject violation,50-458/98004-02, involves inadequate procedural guidance to

maintain control of the position of an attached maintenance jacking device on a primary

containment purge valve.

Should you have any questions regarding the attached information, please contact Mr.

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David Lorfing of my staff at (504) 381-4157.

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Sincerely,

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Reply to Notice of Violation in 50-458/98-004

April 3,1998

RBG-44445

RBF1-98-0072

Page 2 0f 2

cc:

U.S. Nuclear Regulatory Commission

Region IV

611 Ryan Plaza Drive, Suite 400

Arlington,TX 76011

NRC Sr. Resident Inspector

P.O. Box 1050

St. Francisville, LA 70775

David Wigginton

' NRR Project Manager

U.S. Nuclear Regulatory Commission

M/S OWFN 13-H-3

- Washington, DC 20555

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ATTACHMENT A

REPLY TO NOTICE OF VIOLATION 50-458/98004-02

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Page1of2

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Violation:

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. During an NRC inspection conducted on January 11 through February 21,1998, one

violation of NRC requirements was identified. In accordance with the " General

Statement of Policy and Procedure for NRC Enforcement Actions," NUREG-1600, the

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' violation is listed below:

10 CFR Part 50, Appendix B, Criterion V, states, in part, " Activities affectir's

quality shall be prescribed by documented instructions, procedures, or drawings of

a type appropriate to the circumstances and shall be accomplished in accordance

with these instructions, procedures, or drawings . . ."

Matryx Company Drawing Number 410318, dated October 10,1980, required

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that the pump release screws (petcock valves) be positioned one tum

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counterclockwise (open) when operating containment ventilation and purge

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Dampers HVR-AOV-128, HVR-AOV-165, and HVR-AOV-166 in the pneumatic

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mode (safety-related mode). This drawing was the only document that specified

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' the position of the petcock valves.

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Contrary to the above, on January 8,1998, the petcock valves for Dampers HVR-

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. AOV-128, HVR-AOV-165, and HVR-AOV-166 were found full closed, but the

dampers had been operated in the pneumatic mode. Controls to ensure that the

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valves were correctly positioned were inadequate.

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This is a Severity Level IV violation (Supplement 1)(50-458/9804-02).

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Reasons for the Violation:

River Bend Station has four containment purge dampers, functioning as primary

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containment isolation barriers, which are fitted with attached hydraulic jacking devices.

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These devices can be used to open the dampers during maintenance or abnormal

operating conditions. The petcock valves, when closed, allow hydraulic pressure to be

- developed for operation of these jacking devices. The petcocks are opened to disable

thesejacks thereby allowing normal pneumatic operation of the dampers.

A root cause investigaticu was conducted, with two primary causes identified.

The first primary cause was related to the area of configuration conul in that there were

inadequate administrative controls established to ensure that the attacned hydraulic

jacking assembly would not interfere with pneumatic operation of the damper. The

correct restoration position of the petcocks (i.e., one turn open) should have been

identified and controlled. If the position had been controlled, the petcocks would have

been restored to the correct position upon completion of maintenance activities.

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ATTACHMENT A

REPLY TO NOTICE OF VIOLATION 50-458/98004-02

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The second primary cause was related to the area of work organization and planning in

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that work package preparation was inadequate as related to this event. . The last

documented maintenance involving steps during which personnel may have manipulated

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the petcocks was performed in June of 1994. There was no step in the job plans directing

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the workers to return the petcocks to the open position upon completion of the work.

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Corrective Actions That Have Been Taken:

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To maintain administrative control over the open position, as depicted on Matryx

Company Drawing Number 410318, dated October 10,1980:

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the petcocks on'all four purge dampers were lockwired one turn open;

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the four lockwired petcocks were fitted with conspicuous labels to direct personnel to

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maintain that position; and1

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the applicable Work Management Screens for the purge dampers were updated with a

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reference note to direct that future job plans contain instructions for the petcocks to be

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lockwired one tum open prior to returning the dampers to service.

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.To address the generic implications:

regarding other pneumatic opetated valves that serve as primary containment isolation

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valves and are included in the Local Leak Rate Testing Program, a review was

conducted finding no other valves fitted with similarly uncontrolled subcomponents

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that could affect operation;

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regarding other plant components, maintenance personnel and system engmeers were

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briefed on this event, stressing the need to identify configurations that could result m

similar events; and

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regarding other plants, the details of this event were distributed through the Institute

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for Nuclear Power Operation (INPO) Nuclear Network for review by other plants,

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Corrective Actions That Will Be Taken to Avoid Further Violations:

The applicable operating procedure will be revised to invoke procedural control over

. retuming the locked open petcock valves to their proper condition after operation.

Preventive maintenance tasks and other standardized maintenance job plans will be

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revised to include a specific restoration step for the petcocks where applicable.

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Date When Full Compliance Will Be Aebieved:

Ad, equate control was achieved upon lockwiring the petcocks open and conspicuously

labeling their correct position. Full compliance will be achieved by June 30,1998.

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