ML20207R405: Difference between revisions

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#REDIRECT [[RBG-25462, Responds to NRC Re Violations Noted in Insp Rept 50-458/86-39 on 861208-12 & 870112-16.Corrective Actions: Temporary Change Notice Issued for Rev 6 to Surveillance Test Procedure STP-051-4234]]
| number = ML20207R405
| issue date = 03/11/1987
| title = Responds to NRC 870211 Ltr Re Violations Noted in Insp Rept 50-458/86-39 on 861208-12 & 870112-16.Corrective Actions: Temporary Change Notice Issued for Rev 6 to Surveillance Test Procedure STP-051-4234
| author name = Cahill W
| author affiliation = GULF STATES UTILITIES CO.
| addressee name =
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
| docket = 05000458
| license number =
| contact person =
| document report number = RBG-25462, NUDOCS 8703170198
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| page count = 6
}}
 
=Text=
{{#Wiki_filter:,          -                                                                                      _    __  _ _ _ _ _ _ _ _ _ - _ _ .
GULF STATES                        UTILITIES COMPANY Rive R BENO STAf)ON    POST OFFICE 80x 220    St FRANCisnLt. Louisiana 70776 An,A CODE 604    635 6094    344 e661 March 11, 1987 RBG- 25462 File Nos. G9.5, G15.4.1 Nuclear Regulatory Commission Document Control Desk Washington, D.C.            20555 Gentlement River Bond Station - Unit 1 Refor to:              Region IV Docket No. 50-458/ Report 86-39 This letter responds to the Notico of Violation contained in NRC Inspection Report No. 50-458/86-39. The inspection was performed by Mossro. W. R. Bonnott, M. E. Skow and R. D. Vickory during the period December 8-12, 1986, and January 12-16, 1987 of activition authorized by NRC Operating License NPF-47 for River Bond Station.
Gulf Staton Utilition Company'n                              (GSU)        responuo to Notice of Violation      8639-01,              " Failure              to        Follow Surveillance Tost Proceduron", and 8639-02, " Failure to Utilizo Proper Revision of Survoillanco        Tout Proceduro", in provided in the onclosed attachment purnuant to 10CFR2.201 and 10CFR50.4. This completon GSU's responno to the Notico of Violation.
Sincoroly, Af          '/ /
                                                                          . J. Cahill, Jr.
Senior Vice President Gulf Staton Utilition Company WJC/    /1 J f        /jo Attachmont cci  Mr. Robert D. Martin, Regionni Administrator U.S. Nucionr Rogulatory Comminnion Rogion IV 611 Ryan Plaza Drivo, Suito 1000 Arlington, TX 76011 River Bond Runident Inspector                                                                                            Ol !
P.O. Box 1051 St. Francinvillo, lA                    70775 jl6    '
0703170190 070311                                                                                                                      Ilt EDH  ADUCK 03000450
 
UNITED STATES OF AMEICA NUCLEAR RECULATORT C(ESEISSION STATE OF IABISIAEA                                              5 PARISE OF WEST FELICIANA                                        5 In the Matter of                                                I                                  Docket Noe. 50-458 GULF STATES UTILITIES CONFANT                                    I (River Bend Station, Unit 1)                                                                                                                                                            .
AFFIDAVIT W. J.              Cahill,          Jr.,  being duly sworn, states that he is a Senior Vice President of Gulf States Utilities Company                                                                              that he is authorised                ,
on the part of said Company to sign and file with the Nuclear Rggulatory Coissission the documents attached hereto                                                      and that all such documents l                  are true and correct to the best of his knowledge, information and belief.
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Subscribed and sworn to before me, a Notary Public in and for the State and Parish above named, this // d                              ayd              of Mb e d[ ,19 ('/.
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l o r, Joan W. Middlebrooks
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Notary Public in and for West Feliciana Parish, toutstana My Commsteston is for IAfa.
 
ATTACHMENT 1 RESPONSE TO NOTICE OF VIOLATION 50-458/8639-01 4                                          LEVEL IV REFERENCE Notice of Violation - J.E.              Gagliardo letter to J.C. Doddens, dated February 11 , 1987, i
FAILURE TO FOLLOW SURVEILLANCE TEST PROCEDURES
:      Technical Specification, paragraph 6.8.1.d requires that written procedures shall be established, implemented, and maintained for survoillance and test activities of safety-related equipment.
Surveillance          Test  Procedure  STP-505-4506,                                                      "RPS/ Control  Rod Block-APRM Wookly Cl!FUNCT, Wookly C il C A L , and 18-Month                                                              LSFT (CSI*K605F) , " Revision 6, stop 7.1.47, requires                                                                  that    the operator"... install a jumpor from pin 2 to pin 50."
Surveillance          Test Proceduro STP-051-4234, "ECCS/HPCS-Roactor Vossol Water Level-Low Low-Levol 2 and High Lovel 8 Monthly CilFUNCT,      18 Month Cl! CAL,    18 Month LSFT (321-N073L; B21-N673L; B21-N674L) ," Revision 5, stop 7.1.33.3, and Revision 6,                                                                  stop 7.1.28.3,        requires that the operator " verify 'llPCS liigh Water
-        Lovel 8 Resot' (Ill 3-P 601-16 B-C- 2 2A-5 6 ) status light is on."
1      Contrary to the above, in stop 7.1.47 of STP-505-4506, performed on November 16, 1986, the operator installed a jumper at a different location than that specified in the proceduro; in stop i      7.1.33.3 of STP 051-4234, Revision 5 performed on May 6 and June 4, 1986, the operator designated thoso stops as not applicable i        when in fact, the procedure required thoso stops to be performed; i        and in stop 7.1.28.3 of STP-051-4234, Revision                                                              6, performed on September          5,    1986, the operator signed off the stop as
+
satinfactory ovon though plant conditions precluded satisfactory performance of this stop.
i This        in    a    Soverity  Lovel    IV                                            violation.              (Supplomont I .D. ) (4 5 8/ 86 3 9-01) i      REASON FOR VIOLATION The      causo    for thin violation      in                    procedural inadequacy and personnel          error. The    Inntrumontation and Controla (I&C) technician failed to identify the alternato location of jumpor pincoment        via a tout exception or Temporary Chango Notico (TCN).
  .      Accessibility of the location specified by the proceduro wan very rontricted.          The technician had rocontly completed installation of terminal blocks por approved modification request.                                                                    Thono terminal blocks wuro installed to provido an altornato location j      to facilitato tonting. Boing awaro of the rovinion which wan l
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ATTACHMENT (cont'd) being processed and being knowledgeable with the system, the technician decided to use the alternate location.
In Surveillance Test Procedure (STP)-051-4234      Revision 5, step 7.1.33.3 and Revision 6, step 7.1.28.3 required the verification of a lighted status light, which under conditions other than having an actual indication of high reactor water level would not be lighted. The procedure was misleading by requiring something which can not normally be done. The technician erred when he did not stop and change the STP when step 7.1.33.3 could not be performed. A TCN    is  required under these circumstances by Administrative Procedure, ADM-0003, " Development, Control and Use of Procedures" and ADM-0015, " Station Surveillance Test Program".
CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND Tile RESULTS ACHIEVED A  TCN has been issued        to STP-051-4234 Revision 6, wording it similarly to other sister procedures. Either initialing or N/A being placed in the block is acceptable.
CORRECTIVE STEPS TAKEN TO AVOID FURTilER VIOLATIONS Memorandum PIC-M-87-007 dated January 8, 1987 and PIC-M-87-033 dated March 10,      1987 have been issued to        reiterate  the requirements      of      administrative    procedures:    ADM-0003,
        " Development, Control and Use of Procedures" and ADM-0015,
        " Station    Surveillance    Test  Program". I&C personnel were
;      instructed via memorandum (PIC-M-87-007) on the use of Comment Control Forms as a means of procedure improvement.
As a result of this violation, the I&C section is conducting a review and revising STP's as needed. Sister procedures are being reviewed for uniformity and are being revised as applicable.
DATE TilAT FULL COMPLIANCE WILL BE ACllIEVED:
River Bond Station is currently in full compliance.
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ATTACHMENT 2 RESPONSE TO NOTICE OF VIOLATION 50-458/8639-02 LEVEL IV REFERENCE Notice of Violation          -
J.E. Gagliardo letter to J.C. Doddens, dated February 11 , 1987.
FAILURE TO UTILIZE PROPER REVISION OF SURVEILLANCE TEST PROCEDURE Technical Specification, paragraph 6.8.1.d requires that written procedures shall be established, implemented, and maintained for surveillance and test activities of safety-related equipment.
Administrative procedure ADM-0005, " Station Document Control,"
Revision 5, dated February 17, 1986, states, in paragraph 3.3, that the user of procedures is"... responsible to assure that they      have    the most current        revision prior to performing safety-related activities."
Contrary to the above, STP-051-4234,            "ECCS/flPCS-Reactor Vessel Water Level-Low Low-Level 2 and liigh Level 8 Monthly CilFUNCT, 18-Month Ci! CAL, 18-Month LSFT (D21-N073L; B21-N673L; B21-N674L),"
Revision 5, was performed on August                6, 1986.      Revision 6 to STP-051-4234 was issued and in effect on August 4, 1986.
This      is    a    Severity    Level      IV  violation.        (Supplement I .D. ) (4 58/ 8639-02)
REASON FOR Tile VIOLATION Personnel error caused an incorrect revision of STP-051-4234, "ECCS/11PCS Reactor Vessel Water Level-Low Low-Level 2 and liigh Level      8    Monthly    CliFUNCT ,    18-Month C llc A L , 18-Month LSFT (B21-N673L; B21-N674L)", to be used.              On July      27,  1986,  the technician withdrew Revision 5 of SrP-051-4234 from Station Document Control. Eight days later, Revision 6 of STP-051-4234 was issued. August 6, 1986, ten days after receiving Revision 5 and two days after Revision 6 became effective,                  the  STP was performed.        The technician      did  not check to  see  if the  STP had been revised.
CORI<ECTIVE STEPS TAKEN AND RESULTS ACilIEVED A  review of Revisions 5 and 6 indicated that Revision 6 incorporated        the TCN's    previously attached to Revision 5.
Because Revision 6 contains no significant technical differences from Revision 5 and the attached TCN's, there was no adverse impact on plant process systems or equipment.
 
ATTACHMENT 2 (cont'd)
CORRECTIVE STEPS TAKEN TO AVOID FURTHER VIOLATION Administrative Procedure, ADM-0015, " Station Surveillance Test Program",  requires the user to verify that the procedure that is to be used in the plant is the latest revision. This requirement has been clarified to assure a check of revision status. prior to use (TCN 87-0124).
Instructions concerning the importance of and methods used to ensure that the correct procedure revision is used in the plant will be provided.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED TCN-87-0124  has  been  issued to ADM-0015 to re-enforce the necessity  for  ensuring  that the procedure used in the plant is current.
Training of Maintenance personnel will be complete by    March  16, 1987, t}}

Latest revision as of 15:52, 5 December 2021