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Director, Office of Management and Program Analysis Page 2
Director, Office of Management and Program Analysis
+-
+-                   Page 2 De: ember 8, 1982 ATTACHMEfff I
De: ember 8, 1982 ATTACHMEfff I AIERAGE DAILY UNIT POWER LEVEL
                                              "          ~
~
                        ~
~
AIERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50/395 UNIT v.c.5 mmer I DATE 12-08-82 COMPLETED BY G.J           Tavior
DOCKET NO. 50/395 UNIT v.c.5 mmer I DATE 12-08-82 COMPLETED BY G.J Tavior TELEPHONE (803) 345-5209 MONTH NOVEMBER 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
                              -                                                                        TELEPHONE (803) 345-5209 NOVEMBER 1982 MONTH DAY AVERAGE DAILY POWER LEVEL                                       DAY AVERAGE DAILY POWER LEVEL
!                                              (MWe-Net)                                       _
(MWe-Ne:)
(MWe-Ne:)
1 0                                   17           29 0                                   13 ,           n             -
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115 9
10                             0                                  26           M2 11                             0                                   gy           143 0                                               170 12                                                                 28 13                           0                                   29         -156 0                                   y            0
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gy 143 0
_                3 14_                         5 8301270164 821208 PDR ADOCK 05000395                 PDR R
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Director, Office of Managemer c and Program Aialysis Page 3 December 8, 1982                               ATTACHMENT II OPERATING DATA REPORT DOCKET NO.           50/395 UNIT    V.C. Summer I e
Director, Office of Managemer c and Program Aialysis Page 3 December 8, 1982 ATTACHMENT II OPERATING DATA REPORT DOCKET NO.
DATE 12-08-82
50/395 V.C. Summer I UNIT e
                                                                                                                                            ~
12-08-82 DATE G.J. Taylor ~ ~
G.J. Taylor ~ ~
~
COMPLETED BY TELEPHONE (803) 345-5209 OPERATING STATUS 720 IIOVEMBER 1982             Gross HOURS IN RhPORTING PE81tOO:
COMPLETED BY (803) 345-5209 TELEPHONE OPERATING STATUS 720 IIOVEMBER 1982 Gross HOURS IN RhPORTING PE81tOO:
: 1. REPORTING PERIOD:
: 1. REPORTING PERIOD:
2775           MAX. DEPEND. CAPACITY (MWerNet):
N/A 2775 MAX. DEPEND. CAPACITY (MWerNet):
N/A
: 2. CUM ENTLY AUTHORIZED POWER LEVEL (MWti:
: 2. CUM ENTLY AUTHORIZED POWER LEVEL (MWti:               9 0 0 .,,,,,
DES! JN ELECTRICAL RATING (MWo.Neel:
DES! JN ELECTRICAL RATING (MWo.Neel:
9 0 0.,,,,,
N/A (50% MWt)
N/A (50% MWt)
: 3. POWER LEVC.TO WHICH RESTRICTED (IF ANY) (MhNet):
: 3. POWER LEVC.TO WHICH RESTRICTED (IF ANY) (MhNet):
: 4. REASONS FOR RESTRICTION llF ANYl:
: 4. REASONS FOR RESTRICTION llF ANYl:
The Operating License allows operations to
The Operating License allows operations to mis MONTH YR TO DATE CUMULATIVE
                                                      ~~
~~
mis MONTH YR TO DATE CUMULATIVE 50% MWt fer power operations testing.                                                                   655.7       655.7 484.3
50% MWt fer power operations testing.
: 5. NUMBER OF HOURS REACTOR VEAS CRITICAL 0                 0           0
484.3 655.7 655.7
: 4. REACTOR RESERVE SHUTOOWr4 HOURS . . . . . . . . . . . . . . . . . . .                                                             '
: 5. NUMBER OF HOURS REACTOR VEAS CRITICAL 0
192.3             192.3       192.3
0 0
: 7. HOURS GENER ATOR ON LINE . . . . . . . . . . . . . . . . . . . . . . . . . .
: 4. REACTOR RESERVE SHUTOOWr4 HOURS...................
0                 0           0 S. UNIT RESERVE SHUTDOWN HOURS ......................
192.3 192.3 192.3
143.789          144,802_      144,802
: 7. HOURS GENER ATOR ON LINE..........................
: 9. GROSS THERMAL ENERGY GENERATED (MWH) .............
0 0
30.567             30.567,     30,567
0 S. UNIT RESERVE SHUTDOWN HOURS......................
: 10. GROSS ELECTRICAL ENERGY GENERATED (MWHI . . . . . . . . . . . . .
: 9. GROSS THERMAL ENERGY GENERATED (MWH).............
24.839             24.839       24,839
143.789 144,802_
: 11. NEY ELECTRICAL ENERGY GENERATID (MWH)           ..............
144,802 30.567 30.567, 30,567
N/A               N/A         N/A
: 10. GROSS ELECTRICAL ENERGY GENERATED (MWHI.............
: 12. REACTOR SERVICE F ACTOR . . . . . . . . . . . . . . . . . . . . . . . . . . .
24.839 24.839 24,839
                                                                                                        *N/A.               N/A         N/A
: 11. NEY ELECTRICAL ENERGY GENERATID (MWH)
: 13. REACTOR AVAILABIllTY F ACTOR . . . . . . . . . . . . . . . . . . . . . . .
N/A N/A N/A
N/A               N/A         N/A
: 12. REACTOR SERVICE F ACTOR...........................
: 14. UNIT SERVICE F ACTOR . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .
*N/A.
N/A               N/A         N/A
N/A N/A
: 15. UNIT AVAILABILITY F ACTOR . . . . . . . . . . . . . . . . . . . . . . . . . .
: 13. REACTOR AVAILABIllTY F ACTOR.......................
N/A               N/A         N/A
N/A N/A N/A
: 16. UNIT CAPACITY FACTOR (using MDC) 7. . . . . . . . . . . . . . . . . . . .
: 14. UNIT SERVICE F ACTOR..............................
N/A               N/A         N/A
N/A N/A N/A
: 17. UNIT CAPACITY FACTOR (Using Design MWel . . . . . . . . . . . . . . . . .                       ''
: 15. UNIT AVAILABILITY F ACTOR..........................
N/A N/A N/A
: 16. UNIT CAPACITY FACTOR (using MDC) 7....................
N/A N/A N/A
: 17. UNIT CAPACITY FACTOR (Using Design MWel.................
N/A
N/A
                                                                                                                    ~
~
N/A               N/A
N/A N/A
: 18. UNIT FORCED OUTAGE R ATE . . . . . . . . . . . . . . . . . . . . . . . . . .
: 18. UNIT FORCED OUTAGE R ATE..........................
: 19. SHUTDOWN 4 SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACHl:
: 19. SHUTDOWN 4 SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACHl:
(
(
D-3 Steam Cenerator Modification -- March 1983, through May,1983                           M/A i
i D-3 Steam Cenerator Modification -- March 1983, through May,1983 M/A
: 20. iF SHUT DOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARTUP:
: 20. iF SHUT DOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARTUP:
FORECAST ACHIEVED
: 21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPGRATION):
: 21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPGRATION):
INITIAL CRITICALITY 10-20-82 10-22-82 INITIAL ELECTRICITY l1-l7-82_ 11-16-82 I                                                                                                   __
FORECAST ACHIEVED 10-20-82 10-22-82 INITIAL CRITICALITY l1-l7-82_ 11-16-82 INITIAL ELECTRICITY I
COMMERCIAL OPERATION l
COMMERCIAL OPERATION l


Director, Office of Management and Program Analysis                                                                                                     ATTACHMENT III                             DOCKET NO. 50/395                   -:
Director, Office of Management and Program Analysis ATTACHMENT III DOCKET NO. 50/395 Page 4 December 8, 1982 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME V. c. S u==ar i I) ATE 19 nn n?
Page 4                                                                                                                                                                                                 .
COMPLETED BY _G J. Tavlor REPORT MONTil NOVEMBER 1982 TELEPHONE (803) m-mo METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR GR NO.
December 8, 1982                                                                                           UNIT SHUTDOWNS AND POWER REDUCTIONS                         UNIT NAME V . c . S u==ar i I) ATE 19 nn n?             .
DATE S: SCHEDULED (HOURS)
COMPLETED BY _G     J. Tavlor REPORT MONTil             NOVEMBER 1982             TELEPHONE (803) m-mo METHOD OF TYPE                                                                   SHUTTING DOWN F: FORCED DURATION                                                         THE REACTOR GR NO.                             DATE                   S: SCHEDULED (HOURS)                                     REASON (1)     REDUCING POWER (2)             CORRECTIVE ACTION 0mENTS
REASON (1)
                                                                                                        ~
REDUCING POWER (2)
N/A                     821116                           S           382.0                                       H                   ,
CORRECTIVE ACTION 0mENTS
4               Initial Plant Start-up Testing I'                     82?l17                           F             54.7                                       G                     3               1) Reactor trip due to low-low level in Steam Generator "B".
~
2                     d21119                           S             14.0                                       H                     2               2) Tripped reactor while performing control room evacuation test.
N/A 821116 S
3           (821120                                     F             19.3                                       G                     3   .            3) Reactor trip due to low-low la"al. it all Steam Generators.          .
382.0 H
4                     821121                           S             12.3                                       H                     4               4) Tripped reactor while performing Station Blackout Test.
4 Initial Plant Start-up Testing I'
18.5 5                      821122                            F                                                        C                     3               5) Reactor trip due to low level in Deaerator tank, caused main feen-water pumps to trip causing turbine to trip, in turn tripping reactor.
82?l17 F
6                     821129                           F             26.9                                       G                     3               6) Reactor trip due to low-low level in g                                                                                                                                                         B Steam Generator while performing i                                                                                                                                                         Steam Generator level test.
54.7 G
3
: 1) Reactor trip due to low-low level in Steam Generator "B".
2 d21119 S
14.0 H
2
: 2) Tripped reactor while performing control room evacuation test.
3 (821120 F
19.3 G
3
: 3) Reactor trip due to low-low la"al. it all Steam Generators.
4 821121 S
12.3 H
4
: 4) Tripped reactor while performing Station Blackout Test.
5 821122 F
18.5 C
3
: 5) Reactor trip due to low level in Deaerator tank, caused main feen-water pumps to trip causing turbine to trip, in turn tripping reactor.
6 821129 F
26.9 G
3
: 6) Reactor trip due to low-low level in g
B Steam Generator while performing i
Steam Generator level test.
t
t


n l'       .
n l'
Director, Office ~ofcManagement and-Program Analysiv Page15                                                                   .
Director, Office ~ofcManagement and-Program Analysiv Page15 December 8, 1982 ATTACHMENT IV NARRATIVE  
December 8, 1982 ATTACHMENT IV NARRATIVE  


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE 4
OF OPERATING EXPERIENCE 4
1The Nuclear Regulatory Commission granted Virgil C. Summer Nuclear Station Unit No. 1 permission to allow teating and operations to a 50% MWth power level at 1821 hours November 12, 1982. Immediately thereaf ter, commencement of the power ascension. testing program took ' place. At 2200 hours November 16, 1982, Virgil ~C. Summer Nuclear Station was syncronized to the grid at a 10%. power level and produced its first electricity.
1The Nuclear Regulatory Commission granted Virgil C.
Summer Nuclear Station Unit No. 1 permission to allow teating and operations to a 50% MWth power level at 1821 hours November 12, 1982.
Immediately thereaf ter, commencement of the power ascension. testing program took ' place.
At 2200 hours November 16, 1982, Virgil ~C.
Summer Nuclear Station was syncronized to the grid at a 10%. power level and produced its first electricity.
A reactor trip occurred ' at 0420 hours' November 4,1982, from 0%
A reactor trip occurred ' at 0420 hours' November 4,1982, from 0%
power. The trip was due to a low-low- level in Steam Generator "B" while-in manual control.
power.
The trip was due to a low-low-level in Steam Generator "B" while-in manual control.
On. November 11, 1982-at 1100 hours, problems were encountered in
On. November 11, 1982-at 1100 hours, problems were encountered in
                  'the. operation-of Main Feedwater Isolation Valve "A". Then the
'the. operation-of Main Feedwater Isolation Valve "A".
                                      ~
Then the Plant was-subsequently shut down for corrective action.. It was
Plant was-subsequently shut down for corrective action. . It was determined later that a redundant solenoid was faulty. -It was replaced, and th'e valve was put back into service.       The valve was considered to have been Technical Specification operable during the duration of -this condition.
~
determined later that a redundant solenoid was faulty. -It was replaced, and th'e valve was put back into service.
The valve was considered to have been Technical Specification operable during the duration of -this condition.
c A reactor - trip occurred Iat 0315 hours November 13,1982, Efran 2%
c A reactor - trip occurred Iat 0315 hours November 13,1982, Efran 2%
power. The trip was due to low feedwater flow to "C" Steam Generator. This occurred due to a. steam flow noise spike on Steam Generator "C" steam flow instrumentation, while testing N-41 Nuclear Instrumentation.
power.
The trip was due to low feedwater flow to "C" Steam Generator.
This occurred due to a. steam flow noise spike on Steam Generator "C" steam flow instrumentation, while testing N-41 Nuclear Instrumentation.
A reactor trip occurred at 2011 hours November 13,1982, from 2%
A reactor trip occurred at 2011 hours November 13,1982, from 2%
power. This trip was due to low-low level in Steam Generator "C". Feedwater was in manual control, and feedwater was isolated due to-high flow through the feedwater bypass valve. Steam Generator level decreased before operator could recover.
power.
i                 A reactor trip occurred at 1444 hours November 17, 1982, from 2%
This trip was due to low-low level in Steam Generator "C".
                  . power. The trip was due ,to low-low level in Steam Generator "B"
Feedwater was in manual control, and feedwater was isolated due to-high flow through the feedwater bypass valve.
                  .w hile transferring emergency feedwater flow to main feedwater flow.
Steam Generator level decreased before operator could recover.
A reactor trip occurred at 2138 hours November 17,1982, from 35 power. The trip was due to low-low level in Steam Generator "A".
i A reactor trip occurred at 1444 hours November 17, 1982, from 2%
. power.
The trip was due,to low-low level in Steam Generator "B"
. hile transferring emergency feedwater flow to main feedwater w
flow.
A reactor trip occurred at 2138 hours November 17,1982, from 35 power.
The trip was due to low-low level in Steam Generator "A".
A reac. tor trip' occurred at 0030 hours November 19,1982, from 6%
A reac. tor trip' occurred at 0030 hours November 19,1982, from 6%
                  . power. The trip was due to low-low level in Steam Generator
. power.
,                  "C".
The trip was due to low-low level in Steam Generator "C".
l
l


          ; ,v; < -
;,v; <,-.
                      - Director, Office - of . Management and Program Anal'ysis-Page 6 December'8, 1982/
- Director, Office - of. Management and Program Anal'ysis-Page 6 December'8, 1982/
ATTACHMENT IV Continued At.2315 hours November 19, 1982, a control room evacuation test.
ATTACHMENT IV Continued At.2315 hours November 19, 1982, a control room evacuation test.
was conducted which resulted in a manual trip of . the plant.-
was conducted which resulted in a manual trip of. the plant.-
                      ' Control .of- the - plant was satisfactorily maintained while away
' Control.of-the - plant was satisfactorily maintained while away
                                      ~
~
from the Control Room.
from the Control Room.
A reactor trip occurred at 0450 hours November 20,1982, 'from 2%
A reactor trip occurred at 0450 hours November 20,1982, 'from 2%
power. The trip, which was due to Steam Generator Low-Low Level,
power.
                      . occurred .while ettempting to transfer feedwater flow from emergency to main feedwater flow.
The trip, which was due to Steam Generator Low-Low Level,
  ?
. occurred.while ettempting to transfer feedwater flow from emergency to main feedwater flow.
?
A ' reactor trip occurredLat 1626 hours November 20,1982, from 12%
A ' reactor trip occurredLat 1626 hours November 20,1982, from 12%
                                    ~
~
power. The trip was_due to low-low level in all steam generators. Feedwater Isolation Valves A, B, and C tripped when feedwater temperature dropped belor: 225 F.       The feedwater temperature decrease was due to a flow transient in the deaerator tank which caused a cooldown in feedwater.
power.
The trip was_due to low-low level in all steam generators.
Feedwater Isolation Valves A, B, and C tripped when feedwater temperature dropped belor: 225 F.
The feedwater temperature decrease was due to a flow transient in the deaerator tank which caused a cooldown in feedwater.
A reactor trip occurred at 0457 hours November 21,1982, from 1%
A reactor trip occurred at 0457 hours November 21,1982, from 1%
power. The trip, .which was due to Steam Generator Low-Low Level,
power.
                      . occurred while warming up main feedwater lines and transferring feedwater flow ' f rom emergency to main feedwater flow.
The trip,.which was due to Steam Generator Low-Low Level,
At 1419 hours November 21, 1982, a Station Blackout Test was conducted which resulted in a plant trip.     The plant performed as expected, and the test was satisfactorily completed.
. occurred while warming up main feedwater lines and transferring feedwater flow ' f rom emergency to main feedwater flow.
At 1419 hours November 21, 1982, a Station Blackout Test was conducted which resulted in a plant trip.
The plant performed as expected, and the test was satisfactorily completed.
F A reactor trip occurred at 1059 hours November 22, 1982, from 21%
F A reactor trip occurred at 1059 hours November 22, 1982, from 21%
power. .The trip was a result of a feedwater pump trip due to low-low deaerator tank level, while attempting to transfer to main feedwater valves. The feedwater booster pump and feedwater i
power..The trip was a result of a feedwater pump trip due to low-low deaerator tank level, while attempting to transfer to main feedwater valves.
pumps tripped from low level in the deaerator storage tank. This caused the main turbine to trip, subsequently causing the reactor to trip' when power level is greater than 10%.
The feedwater booster pump and feedwater pumps tripped from low level in the deaerator storage tank.
This i
caused the main turbine to trip, subsequently causing the reactor to trip' when power level is greater than 10%.
A reactor trip occurred at 2008 hours November 29,1982, from 30%
A reactor trip occurred at 2008 hours November 29,1982, from 30%
                      ' power. The trip was due tp low-low level in Steam Generator "b" .
' power.
The trip was due tp low-low level in Steam Generator "b".
The trip occurred while pefforming a Steam Generator level test due to a sticking feedwater regulator valve.
The trip occurred while pefforming a Steam Generator level test due to a sticking feedwater regulator valve.
Virgil C. Summer Nuclear Station is presently continuing power ascension testing to a 50% MWth powcr level.
Virgil C.
Summer Nuclear Station is presently continuing power ascension testing to a 50% MWth powcr level.
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__,}}

Latest revision as of 09:14, 16 December 2024

Monthly Operating Rept for Nov 1982
ML20070Q770
Person / Time
Site: Summer 
Issue date: 12/08/1982
From: Gabe Taylor
SOUTH CAROLINA ELECTRIC & GAS CO.
To:
Shared Package
ML20070Q749 List:
References
NUDOCS 8301270164
Download: ML20070Q770 (5)


Text

-. _.

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Director, Office of Management and Program Analysis Page 2

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De: ember 8, 1982 ATTACHMEfff I AIERAGE DAILY UNIT POWER LEVEL

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DOCKET NO. 50/395 UNIT v.c.5 mmer I DATE 12-08-82 COMPLETED BY G.J Tavior TELEPHONE (803) 345-5209 MONTH NOVEMBER 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Ne:)

1 0

17 29 2

0 13,

n l

l 3

n jg iA l

0 3

5 4

0 2

l 5

M

(

0 30 6

22 0

91 l

7 g

O 123 8

, 24 0

115 9

2?

0 M2 10 26 11 0

gy 143 0

170 12 28 13 0

29

-156 0

0

- 14 y

0

.N/A gg 3

14_

5 8301270164 821208 PDR ADOCK 05000395 R

PDR g

y,

-r, - - - - -

p 4

s

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Director, Office of Managemer c and Program Aialysis Page 3 December 8, 1982 ATTACHMENT II OPERATING DATA REPORT DOCKET NO.

50/395 V.C. Summer I UNIT e

12-08-82 DATE G.J. Taylor ~ ~

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COMPLETED BY (803) 345-5209 TELEPHONE OPERATING STATUS 720 IIOVEMBER 1982 Gross HOURS IN RhPORTING PE81tOO:

1. REPORTING PERIOD:

N/A 2775 MAX. DEPEND. CAPACITY (MWerNet):

2. CUM ENTLY AUTHORIZED POWER LEVEL (MWti:

DES! JN ELECTRICAL RATING (MWo.Neel:

9 0 0.,,,,,

N/A (50% MWt)

3. POWER LEVC.TO WHICH RESTRICTED (IF ANY) (MhNet):
4. REASONS FOR RESTRICTION llF ANYl:

The Operating License allows operations to mis MONTH YR TO DATE CUMULATIVE

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50% MWt fer power operations testing.

484.3 655.7 655.7

5. NUMBER OF HOURS REACTOR VEAS CRITICAL 0

0 0

4. REACTOR RESERVE SHUTOOWr4 HOURS...................

192.3 192.3 192.3

7. HOURS GENER ATOR ON LINE..........................

0 0

0 S. UNIT RESERVE SHUTDOWN HOURS......................

9. GROSS THERMAL ENERGY GENERATED (MWH).............

143.789 144,802_

144,802 30.567 30.567, 30,567

10. GROSS ELECTRICAL ENERGY GENERATED (MWHI.............

24.839 24.839 24,839

11. NEY ELECTRICAL ENERGY GENERATID (MWH)

N/A N/A N/A

12. REACTOR SERVICE F ACTOR...........................
  • N/A.

N/A N/A

13. REACTOR AVAILABIllTY F ACTOR.......................

N/A N/A N/A

14. UNIT SERVICE F ACTOR..............................

N/A N/A N/A

15. UNIT AVAILABILITY F ACTOR..........................

N/A N/A N/A

16. UNIT CAPACITY FACTOR (using MDC) 7....................

N/A N/A N/A

17. UNIT CAPACITY FACTOR (Using Design MWel.................

N/A

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N/A N/A

18. UNIT FORCED OUTAGE R ATE..........................
19. SHUTDOWN 4 SCHEDULED OVER NEXT 6 MONTHS (TYPE. DATE. AND DURATION OF EACHl:

(

i D-3 Steam Cenerator Modification -- March 1983, through May,1983 M/A

20. iF SHUT DOWN AT END OF REPORT PERIOD. ESTIMATED DATE OF STARTUP:
21. UNITS IN TEST STATUS (PRIOR TO COMMERCIAL OPGRATION):

FORECAST ACHIEVED 10-20-82 10-22-82 INITIAL CRITICALITY l1-l7-82_ 11-16-82 INITIAL ELECTRICITY I

COMMERCIAL OPERATION l

Director, Office of Management and Program Analysis ATTACHMENT III DOCKET NO. 50/395 Page 4 December 8, 1982 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME V. c. S u==ar i I) ATE 19 nn n?

COMPLETED BY _G J. Tavlor REPORT MONTil NOVEMBER 1982 TELEPHONE (803) m-mo METHOD OF TYPE SHUTTING DOWN F: FORCED DURATION THE REACTOR GR NO.

DATE S: SCHEDULED (HOURS)

REASON (1)

REDUCING POWER (2)

CORRECTIVE ACTION 0mENTS

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N/A 821116 S

382.0 H

4 Initial Plant Start-up Testing I'

82?l17 F

54.7 G

3

1) Reactor trip due to low-low level in Steam Generator "B".

2 d21119 S

14.0 H

2

2) Tripped reactor while performing control room evacuation test.

3 (821120 F

19.3 G

3

3) Reactor trip due to low-low la"al. it all Steam Generators.

4 821121 S

12.3 H

4

4) Tripped reactor while performing Station Blackout Test.

5 821122 F

18.5 C

3

5) Reactor trip due to low level in Deaerator tank, caused main feen-water pumps to trip causing turbine to trip, in turn tripping reactor.

6 821129 F

26.9 G

3

6) Reactor trip due to low-low level in g

B Steam Generator while performing i

Steam Generator level test.

t

n l'

Director, Office ~ofcManagement and-Program Analysiv Page15 December 8, 1982 ATTACHMENT IV NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE 4

1The Nuclear Regulatory Commission granted Virgil C.

Summer Nuclear Station Unit No. 1 permission to allow teating and operations to a 50% MWth power level at 1821 hours0.0211 days <br />0.506 hours <br />0.00301 weeks <br />6.928905e-4 months <br /> November 12, 1982.

Immediately thereaf ter, commencement of the power ascension. testing program took ' place.

At 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> November 16, 1982, Virgil ~C.

Summer Nuclear Station was syncronized to the grid at a 10%. power level and produced its first electricity.

A reactor trip occurred ' at 0420 hours0.00486 days <br />0.117 hours <br />6.944444e-4 weeks <br />1.5981e-4 months <br />' November 4,1982, from 0%

power.

The trip was due to a low-low-level in Steam Generator "B" while-in manual control.

On. November 11, 1982-at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />, problems were encountered in

'the. operation-of Main Feedwater Isolation Valve "A".

Then the Plant was-subsequently shut down for corrective action.. It was

~

determined later that a redundant solenoid was faulty. -It was replaced, and th'e valve was put back into service.

The valve was considered to have been Technical Specification operable during the duration of -this condition.

c A reactor - trip occurred Iat 0315 hours0.00365 days <br />0.0875 hours <br />5.208333e-4 weeks <br />1.198575e-4 months <br /> November 13,1982, Efran 2%

power.

The trip was due to low feedwater flow to "C" Steam Generator.

This occurred due to a. steam flow noise spike on Steam Generator "C" steam flow instrumentation, while testing N-41 Nuclear Instrumentation.

A reactor trip occurred at 2011 hours0.0233 days <br />0.559 hours <br />0.00333 weeks <br />7.651855e-4 months <br /> November 13,1982, from 2%

power.

This trip was due to low-low level in Steam Generator "C".

Feedwater was in manual control, and feedwater was isolated due to-high flow through the feedwater bypass valve.

Steam Generator level decreased before operator could recover.

i A reactor trip occurred at 1444 hours0.0167 days <br />0.401 hours <br />0.00239 weeks <br />5.49442e-4 months <br /> November 17, 1982, from 2%

. power.

The trip was due,to low-low level in Steam Generator "B"

. hile transferring emergency feedwater flow to main feedwater w

flow.

A reactor trip occurred at 2138 hours0.0247 days <br />0.594 hours <br />0.00354 weeks <br />8.13509e-4 months <br /> November 17,1982, from 35 power.

The trip was due to low-low level in Steam Generator "A".

A reac. tor trip' occurred at 0030 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> November 19,1982, from 6%

. power.

The trip was due to low-low level in Steam Generator "C".

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- Director, Office - of. Management and Program Anal'ysis-Page 6 December'8, 1982/

ATTACHMENT IV Continued At.2315 hours0.0268 days <br />0.643 hours <br />0.00383 weeks <br />8.808575e-4 months <br /> November 19, 1982, a control room evacuation test.

was conducted which resulted in a manual trip of. the plant.-

' Control.of-the - plant was satisfactorily maintained while away

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from the Control Room.

A reactor trip occurred at 0450 hours0.00521 days <br />0.125 hours <br />7.440476e-4 weeks <br />1.71225e-4 months <br /> November 20,1982, 'from 2%

power.

The trip, which was due to Steam Generator Low-Low Level,

. occurred.while ettempting to transfer feedwater flow from emergency to main feedwater flow.

?

A ' reactor trip occurredLat 1626 hours0.0188 days <br />0.452 hours <br />0.00269 weeks <br />6.18693e-4 months <br /> November 20,1982, from 12%

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power.

The trip was_due to low-low level in all steam generators.

Feedwater Isolation Valves A, B, and C tripped when feedwater temperature dropped belor: 225 F.

The feedwater temperature decrease was due to a flow transient in the deaerator tank which caused a cooldown in feedwater.

A reactor trip occurred at 0457 hours0.00529 days <br />0.127 hours <br />7.556217e-4 weeks <br />1.738885e-4 months <br /> November 21,1982, from 1%

power.

The trip,.which was due to Steam Generator Low-Low Level,

. occurred while warming up main feedwater lines and transferring feedwater flow ' f rom emergency to main feedwater flow.

At 1419 hours0.0164 days <br />0.394 hours <br />0.00235 weeks <br />5.399295e-4 months <br /> November 21, 1982, a Station Blackout Test was conducted which resulted in a plant trip.

The plant performed as expected, and the test was satisfactorily completed.

F A reactor trip occurred at 1059 hours0.0123 days <br />0.294 hours <br />0.00175 weeks <br />4.029495e-4 months <br /> November 22, 1982, from 21%

power..The trip was a result of a feedwater pump trip due to low-low deaerator tank level, while attempting to transfer to main feedwater valves.

The feedwater booster pump and feedwater pumps tripped from low level in the deaerator storage tank.

This i

caused the main turbine to trip, subsequently causing the reactor to trip' when power level is greater than 10%.

A reactor trip occurred at 2008 hours0.0232 days <br />0.558 hours <br />0.00332 weeks <br />7.64044e-4 months <br /> November 29,1982, from 30%

' power.

The trip was due tp low-low level in Steam Generator "b".

The trip occurred while pefforming a Steam Generator level test due to a sticking feedwater regulator valve.

Virgil C.

Summer Nuclear Station is presently continuing power ascension testing to a 50% MWth powcr level.

__,