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| {{Adams
| | #REDIRECT [[05000219/LER-1981-019-03, /03L-0:on 810328,during Normal Shutdown Sequence, IRM Calibr Was Not Performed as Required by Tech Specs. Caused by Procedural Inadequacy.Procedures Will Be Revised]] |
| | number = ML20003H304
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| | issue date = 04/27/1981
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| | title = LER 81-019/03L-0:on 810328,during Normal Shutdown Sequence, IRM Calibr Was Not Performed as Required by Tech Specs. Caused by Procedural Inadequacy.Procedures Will Be Revised
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| | author name = Sklar J
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| | author affiliation = JERSEY CENTRAL POWER & LIGHT CO.
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| | addressee name =
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| | addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
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| | docket = 05000219
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| | license number =
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| | contact person =
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| | document report number = LER-81-019-03L, LER-81-19-3L, NUDOCS 8105050511
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| | package number = ML20003H301
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| | document type = LICENSEE EVENT REPORT (SEE ALSO AO,RO), TEXT-SAFETY REPORT
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| | page count = 1
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| }}
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| | |
| =Text=
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| {{#Wiki_filter:s .
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| c:Rc poRas as u.s.NuctaAn REcutATay consulsslON 87,7M "
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| LICENSEE EVENT REPORT .
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| Q - CcNTRot sLOCK: l l l l l l
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| @ (PLEAsa palNT cR TYPE ALL REQUIRED INFORMATIOM l l
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| @ lSNl F 9 Jl UCENS44 Ol ClCCCE Pl 1l @IS0 l 0 l-l UCENSE 14 0 l0 NUMeem l0*l0 lo If l0 l0 l@284l1l1l1l1l@l 25 uCENSE TYPt JO S3 CAT $5 @
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| 10121119 l@l CioCRET NUMegR ' W of 312181811 SS EVENT C ATE l@l 01412 74 75 l 7 i s il 80l@
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| REPORT D ATE EvEN r DESCRWTION AND PRQ5AOLE CONSEQUENCES h l'5T5'l i On March 28, the plant was progressina towards cold shutdown to correct an I g l increasing leak rate in the primary containment. During the normal shut- l g o 14, I down sequence, the Im m1ibration was not performed as required by Tech l Io isi i Spec 4.1, Table 4.1.1. 'Ihe event is a Reportable Occurrence as defined by I icIei i Tech Spec 6.9.2.b.3. l Ic i:i i l I
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| 3 13 ft 12 32 18 19 20 SEQUENTIAL OCCURRENCE matemT 4EvtssCN
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| $ VENT YEA R REPCRT NC. CcQE TYPE NO.
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| ; ration procedure and the Plant Cooldown frcm Hot Standby to Cold Shut- l l down will be revised. [
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