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| number = ML18066A892 | | number = ML18066A892 | ||
| issue date = 02/21/1997 | | issue date = 02/21/1997 | ||
| title = Responds to NRC | | title = Responds to NRC Re Violations Noted in Insp Rept 50-255/96-14.Corrective actions:SPS050 Revised to Use Terminology of Operating Procedure SOP 30 | ||
| author name = | | author name = Palmisano T | ||
| author affiliation = CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.), | | author affiliation = CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.), | ||
| addressee name = | | addressee name = | ||
| Line 11: | Line 11: | ||
| contact person = | | contact person = | ||
| document report number = NUDOCS 9703030519 | | document report number = NUDOCS 9703030519 | ||
| title reference date = 01-22-1997 | |||
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE | | document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE | ||
| page count = 13 | | page count = 13 | ||
}} | }} | ||
=Text= | =Text= | ||
{{#Wiki_filter:consumers . Power*.*** . l'OWERIN& | {{#Wiki_filter:consumers | ||
llllClllliAWS | . Power*.*** | ||
l'IUlliRESS | . l'OWERIN& | ||
Palisades | llllClllliAWS l'IUlliRESS Palisades Nuclear Plant: 27780 Blue Star Memorlal Highway, Covert, Ml 49043 February 21, 1997 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 DOCKET 50-255 - LICENSE PPR PALISADES PLANT Thomas J. Palmisano Plant General Manager | ||
Nuclear Plant: 27780 Blue Star Memorlal Highway, Covert, Ml 49043 February 21, 1997 U.S. Nuclear Regulatory | . RESPONSE TO NOTICE OF VIOLATION FOR TWO VIOLATIONS IN NRC. | ||
Commission | INTEGRATED INSPECTION REPORT NO. 50-255/96014(DRP) | ||
Document Control Desk Washington, DC 20555 DOCKET 50-255 -LICENSE PPR | NRC Inspection Report No. 50-255/96014(DRP) dated January 22,_1997, identified two Severity Level IV Violations of NRC requirements. The first violation identified two examples where the plant staff did not adhere to procedures while performing outage related activities. The second violation identified an example where adequate installation instructions were not provided for a temporary modification to the containment polar crane. Ou~ response to these violations is in Attachment 1. | ||
PLANT Thomas J. Palmisano | Consumers Power Company (CPCo) agrees to the violations as stated. | ||
Plant General Manager . RESPONSE TO NOTICE OF VIOLATION | |||
FOR TWO VIOLATIONS | ==SUMMARY== | ||
IN NRC . INTEGRATED | OF COMMITMENTS This letter contains three new commitments and no revisions to existing commitments. | ||
INSPECTION | : 1. | ||
REPORT NO. 50-255/96014(DRP) | Periodic.activity, SPSOSO, will be revised to use the terminology of operating procedure, SOP 30, and to make the steps to align automatic transfer switch, | ||
* YSO, an Operations responsibility with the appropriate sign offs. | |||
Report No. 50-255/96014(DRP) | A review of all installed te~porary modifications will be conducted to verify tha. t J | ||
dated January 22,_1997, identified | . acceptable standards were used for installation. | ||
two Severity Level IV Violations | -r-~ | ||
of NRC requirements. | / | ||
The first violation | 1 | ||
identified | : 2. | ||
two examples where the plant staff did not adhere to procedures | 9703030519 970221 PDR ADOCK 05000255 G | ||
while performing | PDR l~Mljlfil ~~If Ml f HD /ID/ f MIJMI JI~ /ID A CMS ENERGY COMPANY | ||
outage related activities. | |||
The second violation | . 3. | ||
identified | The Temporary Modification process will be reviewed to assure that adequate | ||
an example where adequate installation | . guidance is provided to the design engineer for providing inst~llation. | ||
instructions | . instructions, and for verifying that the temporary modification was installed as intended by the design. | ||
were not provided for a temporary | 7~***; | ||
modification | Thomas J. Palmisano Plant General Manager CC | ||
to the containment | * Administrator, Region Ill, USNRC Project Manager, NRR, USNRC NRC Resident.Inspector - Palisades | ||
polar crane. response to these violations | * Attachment | ||
is in Attachment 1 . | * 2 | ||
Power Company (CPCo) agrees to the violations | |||
as stated. SUMMARY OF COMMITMENTS | . ATTACHMENT 1 CONSUMERS POWER COMPANY | ||
This letter contains three new commitments | . PALISADES PLANT | ||
and no revisions | ** DOCKET 50-255 RESPONSE TO TWO VIOLATIONS FROM NRC INSPECTION | ||
to existing commitments. | - REPO_RT NO~ 50-255/96014 (DRP) D~TED JANUARY 22, 1997 10 Pages | ||
1. Periodic.activity, SPSOSO, will be revised to use the terminology | |||
of operating | *~. | ||
procedure, SOP 30, and to make the steps to align automatic | RESPONSE TO-NOTICE OF VIOLATION FROM NRC INSPECTION REPORT NO. 5'?_,-255/96014(DRP) | ||
transfer switch, * YSO, an Operations | NRG VIOLATION | ||
responsibility | : 1) 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings, 11 requires that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. | ||
with the appropriate | : a. | ||
sign offs. | * Licensee procedure CPAL-RFM-002, Revision 0, Section 9.2.11, "Uncouple CROMs and Raise RackExtensions, 11 required in step C.4 that all CRDMs be mechanically' locked prior to ins*erting a reactor trip | ||
modifications | . into the ~eactor protection system.. | ||
will be conducted | : b. | ||
to verify tha. t J . acceptable | Work Order No. 24610226 and PPAC No. SPS050, "PM Auto Transfer | ||
standards | : Switch, 11 Step 11, required that operations return the isolation handle to. | ||
were used for installation. | normal position prior to performing step.12, which required that operations return the bypass handle to automatic. | ||
970221 PDR ADOCK 05000255 G PDR | Contrary to the above, a.* | ||
Ml f HD /ID/ f MIJMI /ID A CMS ENERGY COMPANY | On November 7, 1996, the operations shift did not ensure that the. | ||
control rod drive mechanisms were mechanically locked prior to inserting a reactor trip signal, resulting in the CROM racks dropping into | |||
Modification | **the reactor vessel upper guide structure.* | ||
process will be reviewed to assure that adequate . guidance is provided to the design engineer for providing . . instructions, and for verifying | : b. | ||
that the temporary | 'On November 17, 1996, the operations shift did not return the isolation handle to the normal position prior to returning the bypass handle to *: | ||
modification | automatic position *. resulting in a loss of power to instrument AC bus Y- | ||
was installed | : 01. | ||
as intended by the design. * | This is a Severity Level IV violation (Supplement /). | ||
Thomas J. Palmisano | 1 | ||
Plant General Manager CC * Administrator, Region Ill, USNRC Project Manager, NRR, USNRC NRC Resident.Inspector | |||
-Palisades | CONSUMERS POWER COMPANY RESPONSE | ||
* Attachment | *Consumers-Power Company (CPCo) agrees with the violation as stated. | ||
* | ,REASON FOR VIOLATION Event 1a. | ||
. ATTACHMENT | Several factors *Contributed to this event. First, the "C" shift Control Room Supervisor and the Control Operator were not fully knowledgeable about the status of the control rod drive mechanisms. Second, the shift turnover between "B" shift and "C" shift was inadequate in that it failed to identify the controlling procedure and it failed to discuss. | ||
1 CONSUMERS | the need to contact Refueling Services after Electrical maintenance was completed with | ||
POWER COMPANY . PALISADES | -CRD #33. Third, the Control Room Supervisor and the Control Operator failed.to question the need for a-procedure and determine which procedure was governing the evolution. | ||
* Piscussion On November 7, 1996, preparations were being made to remove thereactor vessel* | |||
FROM NRC INSPECTION | head. These preparations require. | ||
-REPO_RT 50-255/96014 (DRP) | : 1) The uncoupling of the control rods from their drive mechanisms. | ||
JANUARY 22, 1997 10 Pages | : 2) Raising the control rod drive racks | ||
. | : 3) Mechanically locking.the control rod drive racks | ||
OF VIOLATION | : 4) De.-energizing the control rod drive motors, clutches, and brakes by placing the reactor protection system in the "reactor. trip" mode. | ||
FROM NRC INSPECTION | On "A" shift, the Refueling Services personnel began to uncouple the control rod drives. About 1300 on "B" shift, the Refueling Ser-Vices Supervisor called the Control | ||
REPORT NO. 5'?_,-255/96014(DRP) | -Room to let the Control Room know the uncoupling was completed and Operations was requested to raise the control rod drive racks. At this time, Operations discussed the status of the uncoupling with Refueling Services and understood that the Refueling Services procedure was controlling. Operations then withdrew forty-four of the forty-five control rod drive racks, but problems were*encountered with CRD #33 rack. | ||
NRG VIOLATION | Electrical maintenance personnel assistance was requested. While the plant electricians were repairing CRD #33, Operations turnover between "B" and '!C" shifts occurred. During this turnover, general information concerning the control rods was. | ||
1) 10 CFR 50, Appendix B, Criterion | exchanged, but it was not established.that the Refueling Services procedure was controlling. "C"*shift Operations personnel did not understand that the Refueling | ||
V, "Instructions, Procedures, and Drawings, 11 requires that activities | * Services procedure was controlling the evolution and that Refueling Services required notification to lock the control rod drive racks after CRD#33 rack was withdrawn.. | ||
affecting | 2 | ||
quality shall be prescribed | |||
by documented | On "C" shift the electricians finished repairing CRD #33, withdrew the control rod drive rack and mechanically locked itin place. The Shift Supervisor, upon being notified that CRD #33 problem had been resolved and the control rod drive rack was mechanically locked, thought the next sequential step to be performed was to place the reactor protective system in the "reactor trip" mode. The Shift Supervisor did not verify the status of the control rod drive racks nor did he determine which procedure was controlling the evolution and verify that the prerequisites were met. The Shift Supervisor directed Control Room personnel to place the reactor protection system in the "reactor trip" mode. Control Room personnel observed all control rod drive racks, except CRD #33 rack, reinserting into the reactor vessel upon the reactor protection system trip initiation. Subsequently, it was recognized that the control rod racks had not been mechanically locked when control rod #33 rack problem was encountered. | ||
instructions, procedures, or drawings, of a type appropriate | The Refueling Services procedure allowed the control rod drive racks to be l.ocked after all the racks were withdrawn. | ||
to the circumstances | Event 1b. | ||
and shall be accomplished | The reasons for this event included inadequate understanding of the work scope, inadequate communications, inadequate work control documents and improper equipment operation. | ||
in accordance | Discussion | ||
with these instructions, procedures, or drawings. | * On November 17, 1996, the plant was in refueling shutdown conditions with shutdown cooling system in operation. The instrument AC Bus, Y01, was being supplied from Motor Control Center 1. Y01 is critical to the operation of the shutdown cooling system as it affects shutdown cooling heat exchanger bypass and: discharge valves (CV-3006 | ||
. and CV-3025). Earlier in the day these valves were placed on their manual hand jacks to maintain their position as instrument air was isolated and tagged for another maintenance activity. | |||
CPAL-RFM-002, Revision 0, Section 9.2.11, "Uncouple | An electrical preventative maintenance activity (PPAC) was schedul_ed for the Y01 automatic transfer switch, YSO. This required the YSO switch to be removed.from | ||
CROMs and Raise RackExtensions, 11 required in step C.4 that all CRDMs be mechanically' | _ service so electrical maintenance personnel could remove the switch from the cabinet and take it to the electrical shop to perform the preventative maintenance. | ||
locked prior to ins*erting | Control Room personnel reviewed the activity but focused on the impact of this activity on the operation of the shutdown cooling system. They determined that the shutdown cooling heat exchanger bypass and discharge valves would not be affected as they were manually peing operated by the valves' hand jacks. The outage schedule stated that Operations was to "Manually align Y01 to'its normal supply". However, because all | ||
a reactor trip . into the | *the PPAC steps were assigned to Electrical Maintenance for completion, Operations 3 | ||
protection | * did not obtain a copy of the procedure to review, and failed to establish the full electrical maintenance work scope... Subsequently, Operations decided to implement a portion of SOP 30 that configured the YSO switch from automatic to normal, but did not recognize the need to place the isolation handle to "open" (see attached sketch). This configuration fulfilled only one of two alignment steps specified in the PPAC. | ||
system. . b. Work Order No. 24610226 and PPAC No. SPS050, "PM Auto Transfer Switch, 11 Step 11, required that operations | The Control Room Supervisor (CRS) directed an Auxiliary Operator (AO) to configure Y01 onto its normal supply using SOP 30. The AO accompanied by the System Engineering Test Coordinator (SETC) performed the alignment. The SETC explained to the AO that not only would Y01 have to be placed on its normal power supply but, also, YSO must be isolated by moving the isolation handle to the "open" position. At this point the AO should have contacted the.CRS for direction and permission to perform the isolation. However, the AO did the isolation and then communicated the completion of the activity and the additional step taken to the Nuclear Control Operator (NCO). The NCO understood this message to mean that the activity was completed as directed by the CRS. Therefore, the CRS was not informed that YSO was isolated. | ||
return the isolation | After the electrical mainter:iance activity was completed, the Electrician informed the Work Control Center Lead SRO that maintenance was completed and that the Electrician* needed to be present when Operations restored the switch in order to sign. | ||
handle to . normal position prior to performing | the work order steps. Also, the SETC contacted the Work Control Center and *. | ||
step .12, which required that operations | reque$ted that he be notified prior to the restoration activity; however, neither were contacted. If either the Eiectrician or the SETC had been at the work site.during restoration, or if the work activity been written to have Operations sign off for the~. | ||
return the bypass handle to automatic. | . restoration, Operations would have understood the desired position of YSO. | ||
Contrary to the above, a.* On November 7, 1996, the operations | \\ | ||
shift did not ensure that the . control rod drive mechanisms | Work Control Center notified the Shift Lead SRO that YSO could be restored. The Shift Lead SRO conferred with the CRS on restoring YSO, and they decided to proceed. The CRS assigned a different AO to restore YSO, informed the AO and Shift Lead SRO of the. steps he had directed the previous AO to perform, and identified the steps of SOP 30 requir~d to restore YSO.. | ||
were mechanically | The Shift Lead SRO and the AO went to perform the alignment of YSO. They observed the isolation handle, the source light indication and the switch's physical position, but they did not recognize their indications were different than expected. The AO placed the YSO bypass handle from normal to automatic. Because the isolation handle had not been restored to the "close" position, YSO failed to transfer and Y01 was de-energized. | ||
locked prior to inserting | l 4 | ||
a reactor trip signal, resulting | |||
in the CROM racks dropping into **the reactor vessel upper guide structure.* | CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED The following actions were taken. _ | ||
b. 'On November 17, 1996, the operations | Event 1a. | ||
shift did not return the isolation | : 1. | ||
handle to the normal position prior to returning | Refueling and Maintenance outage activities were temporarily suspended on November 18, 1996 to review and reinforce nuclear, radiation, and industrial/personnel safety concerns with all work groups on site. This event and several other events from the first two weeks of the outage were reviewed with all crews. A common theme running among the identified issues is the lack of-communications between work groups and alignment among workers. | ||
the bypass handle to *: automatic | : 2. | ||
position *. resulting | Three specific responsibilities were reinforced at the Operations Department stand down meetings. These were: | ||
in a loss of power to instrument | Shift Supervisors, are to identify Operations activities from the outage schedule with an understanding of the relationship between these activiti~s | ||
AC bus Y-01. This is a Severity Level IV violation (Supplement | . and others. It is intended that this understanding will contribute to well-informed decision making ~ithin the Operations organization. | ||
/). 1 | . Work Control Center Senior Reactor Operators are to direct work activities | ||
CONSUMERS | * having Operations involvement to Control Room personnel for authorization. | ||
POWER COMPANY RESPONSE *Consumers-Power | . | ||
Company (CPCo) agrees with the violation | * This is to provide interfacing work documents physically to the individual.s. | ||
as stated. ,REASON FOR VIOLATION | who will be performing the activity, better communications between Operations and other. work discipline* personnel, and improve the information flow to those individuals who will be directing the activity> | ||
Event 1a. Several factors *Contributed | Control. Room personnel are to assure they have a complete understanding | ||
to this event. First, the "C" shift Control Room Supervisor | * of activities requested of them and that proper alignments have been made. | ||
and the Control Operator were not fully knowledgeable | : 3. | ||
about the status of the control rod drive mechanisms. | .. The control rod drive blades and racks were inspected for damage due the trip occurring with a reduced water level. No damage was observed on any of the control rod drive blades or racks. | ||
Second, the shift turnover between "B" shift and "C" shift was inadequate | Event 1b. | ||
in that it failed to identify the controlling | In addition to actions 1 and 2 from above, the following actions were taken. | ||
procedure | : 1. | ||
and it failed to discuss. the need to contact Refueling | Shift Supervisor, CRS, Lead SRO, AO and other Operations personnel involved discussed this event and the barriers that could have prevented it. The 5 | ||
Services after Electrical | |||
maintenance | -~*. | ||
was completed | -discussion included responsibilities for proper communications, pre-job briefings, equipment operation, self checking and other aspects of operator ccmduct. | ||
: 2. | |||
and the Control Operator failed.to | Shift Operations Supervisor has briefed the Shift Supervisors and SROs on the need to identify and conduct pre-job briefings. The expectation to conduct pre- | ||
question the need for a-procedure | .. - -. job briefings whenever coordination between two or more work groups is required has been re-established. | ||
and determine | : 3. | ||
which procedure | * Maintenance and Construction Manager reinforced pre-job briefing expectations with maintenance and construction supervision personnel using this event as an example where a collective pre-job briefing may have prevented the event. | ||
was governing | CORRECTIVE ACTIONS REMAINING TO BE TAKEN TO AVOID FURTHER VIOLATIONS. | ||
the evolution. | Periodic activity, SPS050, will be revised to use the terminology of operating, | ||
* Piscussion | * procedure, SOP 30, and to make the steps to align automatic transfer switch, YSO, an Operations responsibility with the appropriate sign offs. | ||
On November 7, 1996, preparations | DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED | ||
were being made to remove thereactor | * CPCo is now in full compliance. | ||
vessel* head. These preparations | 6 | ||
require. | |||
of the control rods from their drive mechanisms. | Y-50 AUTOMATIC TRANSFER SWITCH I | ||
2) Raising the control rod drive racks 3) Mechanically | I I ! | ||
locking .the control rod drive racks | i i | ||
the control rod drive motors, clutches, and brakes by placing the reactor protection | I I | ||
system in the "reactor. | I I | ||
trip" mode. On "A" shift, the Refueling | I i i I. | ||
Services personnel | EMERGENCY BYPASS HANDLE. CE... | ||
began to uncouple the control rod drives. About 1300 on "B" shift, the Refueling | AUTOMATIC OfEN. | ||
Ser-Vices | *NORMAL T | ||
Supervisor | a.£ROENCY TCJL..IU:XX NORMAL m FAm SWITOf SOURa (KM!Nl'ARY) | ||
called the Control -Room to let the Control Room know the uncoupling | SOURCE | ||
was completed | * AVAJl...&BIE AVAILABIP | ||
and Operations | *.. 0 11tANSFER TE$t' LOAD | ||
was requested | (])NNECJE) | ||
to raise the control rod drive racks. At this time, Operations | TO NORMAL | ||
discussed | * 1t1SI' NORMAL | ||
the status of the uncoupling | (.~) | ||
with Refueling | *1MCC#2! | ||
Services and understood | l | ||
that the Refueling | ~ | ||
Services procedure | RESET ro* | ||
was controlling. | MCC # 1 I* | ||
Operations | I NORMAL 1* *1..-~~~~~~~~~~~~~~~~~~~~......1 7 | ||
then withdrew forty-four | ~ | ||
of the five control rod drive racks, but problems were*encountered | |||
with CRD #33 rack. Electrical | NRC VIOLATION | ||
maintenance | .2.) | ||
personnel | 10 CFR 50, Appendix B, Criterion Ill, Design Control, requires, in part," that | ||
assistance | . design control measures "... shall include provisions to assure that appropriate quality standards are specified and included in design documents...," and that | ||
was requested. | "... design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of.. design reviews. Design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design... " | ||
While the plant electricians | Palisades Administrative Procedure 9.31, "Temporary Modification Control," | ||
were repairing | Revision *12, Paragraph 7.1.8, required that a technical review be conducted to verify that instructions for installation were correct.. | ||
CRD #33, Operations | Contrary to the above~ | ||
turnover between "B" and '!C" shifts occurred. | On November 6, 1996, Temporary Modification (TM) 96-050 to the containment polar came did not contain correct installation instructions for replacement of a single solenoid with two solenoids. The original solenoid was*hard mounted and was provided with adequate ventilation to prevent premature failure. As the result of inadequate preparation and review, TM 96-050 did not provide instructions for mounting the second of the two replacement solenoids. The* | ||
During this turnover, general information | second solenoid was installed utilizing duct tape and "tie-wtaps" in a manner which resulted in overheating and failure of the solenoid coil, and a subsequent. | ||
concerning | * electrical fire.. | ||
the control rods was . exchanged, but it was not established.that | This is a Severity Lev~l IV violation (Supplement 1 ). | ||
the Refueling | CONSUMERS POWER COMPANY RESPONSE Consumers Power Company (CPCo) agrees with the violation as stated. | ||
Services procedure | REASON FOR THE VIOLATION | ||
was controlling. "C"*shift | . Based on the inspection data from the failed coils, the most likely cause of the failure on the trolley crane brake coils is the manner which the coils were mounted. This | ||
Operations | *inadequate mounting design was caused by the failure of design personnel to.identify soler:ioid heat dissipation as critical characteristic during the design process. | ||
personnel | 8 | ||
did not understand | . - --- -~---- | ||
that the Refueling | |||
* Services procedure | Discussion | ||
was controlling | . A temporary modification was required to the containment Polar Crane due to a failure of the existing 460VAC solenoid on the trolley brake actuator. No replacement 460VAC solenoid was available. When this solenoid is energized, the actuator releases the braking mechanism on the crane trolley motor. | ||
the evolution | ) | ||
and that Refueling | The modification involved the replacement of the original 460VAC coil with ~o 230VAC coils. One of the 230V coils would be installed in the position of the original coil and the second would be used as a dummy load to provide a voltage drop across it. This would result in a voltage dividing circuit which would divide the 460 volts from the circuit supply in half thus applying 230 volts across each coil. To ensure that the impedance w<ifs matched a spare plunger was inserted into the dummy coil and fixed in the inserted position using duct tape. The dummy coil was then tye-wrapped to a | ||
Services required notification | . support bar and additional tape was wrapped around it. | ||
to lock the control rod drive racks after CRD#33 rack was withdrawn | The temporary modification to substitute the 230VAC coils for the 460VAC was an acceptable design. However, the dummy coil mounting design was focused on making sure the coil did not come loose and fall into the debris free zone inside containment. * | ||
.. 2 | . Potential overheating of the dummy coil was not considered in the design. | ||
The Polar Crane was in service with the temporary modification in place for approximately 60 hours before failure occurred. With high usage of the Polar Crane. | |||
finished repairing | and repeated starts and stops on the trolley crane motor, the additional layers of tape on the dummy coil caused chronic overheating of the dummy coil. The epoxy insulating material became hot enough to melt and the dummy coil wires shorted togetheL This allowed the full 460 volts to be applied across the 230VAC working coil, causing its failure. The smoke and. arcing observed was the result of the dummy coil overheating, causing the duct tape to catch fire and burn. No evidence of arcing to the support structure was found around either coil. | ||
CRD #33, withdrew the control rod drive rack and mechanically | CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED | ||
locked itin place. The Shift Supervisor, upon being notified that CRD #33 problem had been resolved and the control rod drive rack was mechanically | : 1. | ||
locked, thought the next sequential | * The two 230 volt coils were replaced with a new. 460 volt coil. It has been in use | ||
step to be performed | *without incident since it was installed.. | ||
was to place the reactor protective | : 2. | ||
system in the "reactor trip" mode. The Shift Supervisor | This event was reviewed as a lessons learned with all Design Engineering at a department stand down meeting. Discussions covered conditions leading to the event, and the need for Design Engineering to consider all operating characteristics in design. | ||
did not verify the status of the control rod drive racks nor did he determine | 9 | ||
which procedure | |||
was controlling | CORRECTIVE ACTIONS REMAINING TO BE TAKEN TO AVOID FURTHER VIOLATIONS | ||
the evolution | : 1. | ||
and verify that the prerequisites | A review of all installed temporary modifications will be conducted to verify that acceptable standards were used for installation. | ||
were met. The Shift Supervisor | 2.* | ||
directed Control Room personnel | The Temporary Modification process will be reviewed to assure that adequate guidance is provided to the design engineer for providing installation instructions, arid for verifying that the temporary modification was installed as intended by the design. | ||
to place the reactor protection | DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED CPCo is in full compliance.. | ||
system in the "reactor trip" mode. Control Room personnel | * 10}} | ||
observed all control rod drive racks, except CRD #33 rack, reinserting | |||
into the reactor vessel upon the reactor protection | |||
system trip initiation. | |||
Subsequently, it was recognized | |||
that the control rod racks had not been mechanically | |||
locked when control rod #33 rack problem was encountered. | |||
The Refueling | |||
Services procedure | |||
allowed the control rod drive racks to be l.ocked after all the racks were withdrawn. | |||
Event 1b. The reasons for this event included inadequate | |||
understanding | |||
of the work scope, inadequate | |||
communications, inadequate | |||
work control documents | |||
and improper equipment | |||
operation. | |||
* On November 17, 1996, the plant was in refueling | |||
shutdown conditions | |||
with shutdown cooling system in operation. | |||
The instrument | |||
AC Bus, Y01, was being supplied from Motor Control Center 1. Y01 is critical to the operation | |||
of the shutdown cooling system as it affects shutdown cooling heat exchanger | |||
bypass and: discharge | |||
valves (CV-3006 . and CV-3025). | |||
Earlier in the day these valves were placed on their manual hand jacks to maintain their position as instrument | |||
air was isolated and tagged for another maintenance | |||
activity. | |||
An electrical | |||
preventative | |||
maintenance | |||
activity (PPAC) was schedul_ed | |||
for the Y01 automatic | |||
transfer switch, YSO. This required the YSO switch to be removed .from _ service so electrical | |||
maintenance | |||
personnel | |||
could remove the switch from the cabinet and take it to the electrical | |||
shop to perform the preventative | |||
maintenance. | |||
Control Room personnel | |||
reviewed the activity but focused on the impact of this activity on the operation | |||
of the shutdown cooling system. They determined | |||
that the shutdown cooling heat exchanger | |||
bypass and discharge | |||
valves would not be affected as they were manually peing operated by the valves' hand jacks. The outage schedule stated that Operations | |||
was to "Manually | |||
align Y01 to'its normal supply". However, because all *the PPAC steps were assigned to Electrical | |||
Maintenance | |||
for completion, Operations | |||
3 | |||
to review, and failed to establish | |||
the full electrical | |||
maintenance | |||
work scope ... Subsequently, Operations | |||
decided to implement | |||
a portion of SOP 30 that configured | |||
the YSO switch from automatic | |||
to normal, but did not recognize | |||
the need to place the isolation | |||
handle to "open" (see attached sketch). This configuration | |||
fulfilled | |||
only one of two alignment | |||
steps specified | |||
in the PPAC. The Control Room Supervisor (CRS) directed an Auxiliary | |||
Operator (AO) to configure | |||
Y01 onto its normal supply using SOP 30. The AO accompanied | |||
by the System Engineering | |||
Test Coordinator (SETC) performed | |||
the alignment. | |||
The SETC explained | |||
to the AO that not only would Y01 have to be placed on its normal power supply but, also, YSO must be isolated by moving the isolation | |||
handle to the "open" position. | |||
At this point the AO should have contacted | |||
the.CRS for direction | |||
and permission | |||
to perform the isolation. | |||
However, the AO did the isolation | |||
and then communicated | |||
the completion | |||
of the activity and the additional | |||
step taken to the Nuclear Control Operator (NCO). The NCO understood | |||
this message to mean that the activity was completed | |||
as directed by the CRS. Therefore, the CRS was not informed that YSO was isolated. | |||
After the electrical | |||
mainter:iance | |||
activity was completed, the Electrician | |||
informed the Work Control Center Lead SRO that maintenance | |||
was completed | |||
and that the Electrician* | |||
needed to be present when Operations | |||
restored the switch in order to sign. the work order steps. Also, the SETC contacted | |||
the Work Control Center and * . reque$ted | |||
that he be notified prior to the restoration | |||
activity; | |||
however, neither were contacted. | |||
If either the Eiectrician | |||
or the SETC had been at the work site.during | |||
restoration, or if the work activity been written to have Operations | |||
sign off for . . restoration, Operations | |||
would have understood | |||
the desired position of YSO. \ | |||
The Shift Lead SRO conferred | |||
with the CRS on restoring | |||
YSO, and they decided to proceed. The CRS assigned a different | |||
AO to restore YSO, informed the AO and Shift Lead SRO of the. steps he had directed the previous AO to perform, and identified | |||
the steps of SOP 30 | |||
to restore YSO.. | |||
of YSO. They observed the isolation | |||
handle, the source light indication | |||
and the switch's physical position, but they did not recognize | |||
their indications | |||
were different | |||
than expected. | |||
The AO placed the YSO bypass handle from normal to automatic. | |||
Because the isolation | |||
handle had not been restored to the "close" position, YSO failed to transfer and Y01 was de-energized. | |||
ACTIONS TAKEN AND RESULTS ACHIEVED The following | |||
actions were taken. _ Event 1a. 1. Refueling | |||
and Maintenance | |||
outage activities | |||
were temporarily | |||
suspended | |||
on November 18, 1996 to review and reinforce | |||
nuclear, radiation, and industrial/personnel | |||
safety concerns with all work groups on site. This event and several other events from the first two weeks of the outage were reviewed with all crews. A common theme running among the identified | |||
issues is the lack communications | |||
between work groups and alignment | |||
among workers. | |||
were reinforced | |||
at the Operations | |||
Department | |||
stand down meetings. | |||
These were: | |||
activities | |||
from the outage schedule with an understanding | |||
of the relationship | |||
between these . and others. It is intended that this understanding | |||
will contribute | |||
to well-informed decision making | |||
the Operations | |||
organization. | |||
are to direct work activities | |||
* having Operations | |||
involvement | |||
to Control Room personnel | |||
for authorization . . * This is to provide interfacing | |||
work documents | |||
physically | |||
to the individual.s . who will be performing | |||
the activity, better communications | |||
between Operations | |||
and other. work discipline* | |||
personnel, and improve the information | |||
flow to those individuals | |||
who will be directing | |||
the activity> | |||
are to assure they have a complete understanding | |||
* of activities | |||
requested | |||
of them and that proper alignments | |||
have been made. | |||
for damage due the trip occurring | |||
with a reduced water level. No damage was observed on any of the control rod drive blades or racks. | |||
actions were taken. 1. Shift Supervisor, CRS, Lead SRO, AO and other Operations | |||
personnel | |||
involved discussed | |||
this event and the barriers that could have prevented | |||
it. The 5 | |||
. | |||
included responsibilities | |||
for proper communications, pre-job briefings, equipment | |||
operation, self checking and other aspects of operator ccmduct. 2. Shift Operations | |||
Supervisor | |||
has briefed the Shift Supervisors | |||
and SROs on the need to identify and conduct pre-job briefings. | |||
The expectation | |||
to conduct . . --. job briefings | |||
whenever coordination | |||
between two or more work groups is required has been re-established. | |||
and Construction | |||
Manager reinforced | |||
pre-job briefing expectations | |||
with maintenance | |||
and construction | |||
supervision | |||
personnel | |||
using this event as an example where a collective | |||
pre-job briefing may have prevented | |||
the event. CORRECTIVE | |||
ACTIONS REMAINING | |||
TO BE TAKEN TO AVOID FURTHER VIOLATIONS . Periodic activity, SPS050, will be revised to use the terminology | |||
of operating , * procedure, SOP 30, and to make the steps to align automatic | |||
transfer switch, YSO, an Operations | |||
responsibility | |||
with the appropriate | |||
sign offs. DATE WHEN FULL COMPLIANCE | |||
WILL BE ACHIEVED * CPCo is now in full compliance. | |||
6 | |||
Y-50 AUTOMATIC | |||
TRANSFER SWITCH I I I ! i | |||
BYPASS HANDLE. CE ... AUTOMATIC | |||
TCJL..IU:XX | |||
NORMAL m FAm SWITOf SOURa (KM!Nl'ARY) | |||
SOURCE * AVAJl...&BIE | |||
* .. 0 11tANSFER | |||
TO NORMAL * | |||
. | |||
.2.) 10 CFR 50, Appendix B, Criterion | |||
Ill, Design Control, requires, in part," that . design control measures " ... shall include provisions | |||
to assure that appropriate | |||
quality standards | |||
are specified | |||
and included in design documents | |||
... ," and that " ... design control measures shall provide for verifying | |||
or checking the adequacy of design, such as by the performance | |||
of .. design reviews. Design changes, including | |||
field changes, shall be subject to design control measures commensurate | |||
with those applied to the original design ... " Palisades | |||
Administrative | |||
Procedure | |||
9.31, "Temporary | |||
Modification | |||
Control," Revision *12, Paragraph | |||
7.1.8, required that a technical | |||
review be conducted | |||
to verify that instructions | |||
for installation | |||
were correct .. Contrary to the | |||
On November 6, 1996, Temporary | |||
Modification (TM) 96-050 to the containment | |||
polar came did not contain correct installation | |||
instructions | |||
for replacement | |||
of a single solenoid with two solenoids. | |||
The original solenoid was*hard mounted and was provided with adequate ventilation | |||
to prevent premature | |||
failure. As the result of inadequate | |||
preparation | |||
and review, TM 96-050 did not provide instructions | |||
for mounting the second of the two replacement | |||
solenoids. | |||
The* second solenoid was installed | |||
utilizing | |||
duct tape and "tie-wtaps" in a manner which resulted in overheating | |||
and failure of the solenoid coil, and a subsequent . * electrical | |||
fire .. This is a Severity | |||
IV violation (Supplement | |||
1 ). CONSUMERS | |||
POWER COMPANY RESPONSE Consumers | |||
Power Company (CPCo) agrees with the violation | |||
as stated. REASON FOR THE VIOLATION . Based on the inspection | |||
data from the failed coils, the most likely cause of the failure on the trolley crane brake coils is the manner which the coils were mounted. This *inadequate | |||
mounting design was caused by the failure of design personnel | |||
to.identify | |||
soler:ioid | |||
heat dissipation | |||
as critical characteristic | |||
during the design process . 8 . - | |||
modification | |||
was required to the containment | |||
Polar Crane due to a failure of the existing 460VAC solenoid on the trolley brake actuator. | |||
No replacement | |||
460VAC solenoid was available. | |||
When this solenoid is energized, the actuator releases the braking mechanism | |||
on the crane trolley motor. ) The modification | |||
involved the replacement | |||
of the original 460VAC coil with 230VAC coils. One of the 230V coils would be installed | |||
in the position of the original coil and the second would be used as a dummy load to provide a voltage drop across it. This would result in a voltage dividing circuit which would divide the 460 volts from the circuit supply in half thus applying 230 volts across each coil. To ensure that the impedance | |||
w<ifs matched a spare plunger was inserted into the dummy coil and fixed in the inserted position using duct tape. The dummy coil was then tye-wrapped | |||
to a . support bar and additional | |||
tape was wrapped around it. The temporary | |||
modification | |||
to substitute | |||
the 230VAC coils for the 460VAC was an acceptable | |||
design. However, the dummy coil mounting design was focused on making sure the coil did not come loose and fall into the debris free zone inside containment. | |||
overheating | |||
of the dummy coil was not considered | |||
in the design. The Polar Crane was in service with the temporary | |||
modification | |||
in place for approximately | |||
60 hours before failure occurred. | |||
With high usage of the Polar Crane. and repeated starts and stops on the trolley crane motor, the additional | |||
layers of tape on the dummy coil caused chronic overheating | |||
of the dummy coil. The epoxy insulating | |||
material became hot enough to melt and the dummy coil wires shorted togetheL This allowed the full 460 volts to be applied across the 230VAC working coil, causing its failure. The smoke and. arcing observed was the result of the dummy coil overheating, causing the duct tape to catch fire and burn. No evidence of arcing to the support structure | |||
was found around either coil. CORRECTIVE | |||
ACTIONS TAKEN AND RESULTS ACHIEVED 1. * The two 230 volt coils were replaced with a new. 460 volt coil. It has been in use *without incident since it was installed | |||
.. 2. This event was reviewed as a lessons learned with all Design Engineering | |||
at a department | |||
stand down meeting. Discussions | |||
covered conditions | |||
leading to the event, and the need for Design Engineering | |||
to consider all operating | |||
characteristics | |||
in design . 9 | |||
CORRECTIVE | |||
ACTIONS REMAINING | |||
TO BE TAKEN TO AVOID FURTHER VIOLATIONS | |||
1. A review of all installed | |||
temporary | |||
modifications | |||
will be conducted | |||
to verify that acceptable | |||
standards | |||
were used for installation. | |||
2.* The Temporary | |||
Modification | |||
process will be reviewed to assure that adequate guidance is provided to the design engineer | |||
for providing | |||
installation | |||
instructions, arid for verifying | |||
that the temporary | |||
modification | |||
was installed | |||
as intended by the design. DATE WHEN FULL COMPLIANCE | |||
WILL BE ACHIEVED CPCo is in full compliance. . * 10 | |||
}} | |||
Latest revision as of 06:46, 6 January 2025
| ML18066A892 | |
| Person / Time | |
|---|---|
| Site: | Palisades |
| Issue date: | 02/21/1997 |
| From: | Thomas J. Palmisano CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| NUDOCS 9703030519 | |
| Download: ML18066A892 (13) | |
Text
consumers
. Power*.***
. l'OWERIN&
llllClllliAWS l'IUlliRESS Palisades Nuclear Plant: 27780 Blue Star Memorlal Highway, Covert, Ml 49043 February 21, 1997 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 DOCKET 50-255 - LICENSE PPR PALISADES PLANT Thomas J. Palmisano Plant General Manager
. RESPONSE TO NOTICE OF VIOLATION FOR TWO VIOLATIONS IN NRC.
INTEGRATED INSPECTION REPORT NO. 50-255/96014(DRP)
NRC Inspection Report No. 50-255/96014(DRP) dated January 22,_1997, identified two Severity Level IV Violations of NRC requirements. The first violation identified two examples where the plant staff did not adhere to procedures while performing outage related activities. The second violation identified an example where adequate installation instructions were not provided for a temporary modification to the containment polar crane. Ou~ response to these violations is in Attachment 1.
Consumers Power Company (CPCo) agrees to the violations as stated.
SUMMARY
OF COMMITMENTS This letter contains three new commitments and no revisions to existing commitments.
- 1.
Periodic.activity, SPSOSO, will be revised to use the terminology of operating procedure, SOP 30, and to make the steps to align automatic transfer switch,
- YSO, an Operations responsibility with the appropriate sign offs.
A review of all installed te~porary modifications will be conducted to verify tha. t J
. acceptable standards were used for installation.
-r-~
/
1
- 2.
9703030519 970221 PDR ADOCK 05000255 G
PDR l~Mljlfil ~~If Ml f HD /ID/ f MIJMI JI~ /ID A CMS ENERGY COMPANY
. 3.
The Temporary Modification process will be reviewed to assure that adequate
. guidance is provided to the design engineer for providing inst~llation.
. instructions, and for verifying that the temporary modification was installed as intended by the design.
7~***;
Thomas J. Palmisano Plant General Manager CC
- Attachment
- 2
. ATTACHMENT 1 CONSUMERS POWER COMPANY
. PALISADES PLANT
- DOCKET 50-255 RESPONSE TO TWO VIOLATIONS FROM NRC INSPECTION
- REPO_RT NO~ 50-255/96014 (DRP) D~TED JANUARY 22, 1997 10 Pages
- ~.
RESPONSE TO-NOTICE OF VIOLATION FROM NRC INSPECTION REPORT NO. 5'?_,-255/96014(DRP)
NRG VIOLATION
- 1) 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings, 11 requires that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.
- a.
- Licensee procedure CPAL-RFM-002, Revision 0, Section 9.2.11, "Uncouple CROMs and Raise RackExtensions, 11 required in step C.4 that all CRDMs be mechanically' locked prior to ins*erting a reactor trip
. into the ~eactor protection system..
- b.
Work Order No. 24610226 and PPAC No. SPS050, "PM Auto Transfer
- Switch, 11 Step 11, required that operations return the isolation handle to.
normal position prior to performing step.12, which required that operations return the bypass handle to automatic.
Contrary to the above, a.*
On November 7, 1996, the operations shift did not ensure that the.
control rod drive mechanisms were mechanically locked prior to inserting a reactor trip signal, resulting in the CROM racks dropping into
- the reactor vessel upper guide structure.*
- b.
'On November 17, 1996, the operations shift did not return the isolation handle to the normal position prior to returning the bypass handle to *:
automatic position *. resulting in a loss of power to instrument AC bus Y-
- 01.
This is a Severity Level IV violation (Supplement /).
1
CONSUMERS POWER COMPANY RESPONSE
- Consumers-Power Company (CPCo) agrees with the violation as stated.
,REASON FOR VIOLATION Event 1a.
Several factors *Contributed to this event. First, the "C" shift Control Room Supervisor and the Control Operator were not fully knowledgeable about the status of the control rod drive mechanisms. Second, the shift turnover between "B" shift and "C" shift was inadequate in that it failed to identify the controlling procedure and it failed to discuss.
the need to contact Refueling Services after Electrical maintenance was completed with
-CRD #33. Third, the Control Room Supervisor and the Control Operator failed.to question the need for a-procedure and determine which procedure was governing the evolution.
- Piscussion On November 7, 1996, preparations were being made to remove thereactor vessel*
head. These preparations require.
- 1) The uncoupling of the control rods from their drive mechanisms.
- 2) Raising the control rod drive racks
- 3) Mechanically locking.the control rod drive racks
- 4) De.-energizing the control rod drive motors, clutches, and brakes by placing the reactor protection system in the "reactor. trip" mode.
On "A" shift, the Refueling Services personnel began to uncouple the control rod drives. About 1300 on "B" shift, the Refueling Ser-Vices Supervisor called the Control
-Room to let the Control Room know the uncoupling was completed and Operations was requested to raise the control rod drive racks. At this time, Operations discussed the status of the uncoupling with Refueling Services and understood that the Refueling Services procedure was controlling. Operations then withdrew forty-four of the forty-five control rod drive racks, but problems were*encountered with CRD #33 rack.
Electrical maintenance personnel assistance was requested. While the plant electricians were repairing CRD #33, Operations turnover between "B" and '!C" shifts occurred. During this turnover, general information concerning the control rods was.
exchanged, but it was not established.that the Refueling Services procedure was controlling. "C"*shift Operations personnel did not understand that the Refueling
- Services procedure was controlling the evolution and that Refueling Services required notification to lock the control rod drive racks after CRD#33 rack was withdrawn..
2
On "C" shift the electricians finished repairing CRD #33, withdrew the control rod drive rack and mechanically locked itin place. The Shift Supervisor, upon being notified that CRD #33 problem had been resolved and the control rod drive rack was mechanically locked, thought the next sequential step to be performed was to place the reactor protective system in the "reactor trip" mode. The Shift Supervisor did not verify the status of the control rod drive racks nor did he determine which procedure was controlling the evolution and verify that the prerequisites were met. The Shift Supervisor directed Control Room personnel to place the reactor protection system in the "reactor trip" mode. Control Room personnel observed all control rod drive racks, except CRD #33 rack, reinserting into the reactor vessel upon the reactor protection system trip initiation. Subsequently, it was recognized that the control rod racks had not been mechanically locked when control rod #33 rack problem was encountered.
The Refueling Services procedure allowed the control rod drive racks to be l.ocked after all the racks were withdrawn.
Event 1b.
The reasons for this event included inadequate understanding of the work scope, inadequate communications, inadequate work control documents and improper equipment operation.
Discussion
- On November 17, 1996, the plant was in refueling shutdown conditions with shutdown cooling system in operation. The instrument AC Bus, Y01, was being supplied from Motor Control Center 1. Y01 is critical to the operation of the shutdown cooling system as it affects shutdown cooling heat exchanger bypass and: discharge valves (CV-3006
. and CV-3025). Earlier in the day these valves were placed on their manual hand jacks to maintain their position as instrument air was isolated and tagged for another maintenance activity.
An electrical preventative maintenance activity (PPAC) was schedul_ed for the Y01 automatic transfer switch, YSO. This required the YSO switch to be removed.from
_ service so electrical maintenance personnel could remove the switch from the cabinet and take it to the electrical shop to perform the preventative maintenance.
Control Room personnel reviewed the activity but focused on the impact of this activity on the operation of the shutdown cooling system. They determined that the shutdown cooling heat exchanger bypass and discharge valves would not be affected as they were manually peing operated by the valves' hand jacks. The outage schedule stated that Operations was to "Manually align Y01 to'its normal supply". However, because all
- the PPAC steps were assigned to Electrical Maintenance for completion, Operations 3
- did not obtain a copy of the procedure to review, and failed to establish the full electrical maintenance work scope... Subsequently, Operations decided to implement a portion of SOP 30 that configured the YSO switch from automatic to normal, but did not recognize the need to place the isolation handle to "open" (see attached sketch). This configuration fulfilled only one of two alignment steps specified in the PPAC.
The Control Room Supervisor (CRS) directed an Auxiliary Operator (AO) to configure Y01 onto its normal supply using SOP 30. The AO accompanied by the System Engineering Test Coordinator (SETC) performed the alignment. The SETC explained to the AO that not only would Y01 have to be placed on its normal power supply but, also, YSO must be isolated by moving the isolation handle to the "open" position. At this point the AO should have contacted the.CRS for direction and permission to perform the isolation. However, the AO did the isolation and then communicated the completion of the activity and the additional step taken to the Nuclear Control Operator (NCO). The NCO understood this message to mean that the activity was completed as directed by the CRS. Therefore, the CRS was not informed that YSO was isolated.
After the electrical mainter:iance activity was completed, the Electrician informed the Work Control Center Lead SRO that maintenance was completed and that the Electrician* needed to be present when Operations restored the switch in order to sign.
the work order steps. Also, the SETC contacted the Work Control Center and *.
reque$ted that he be notified prior to the restoration activity; however, neither were contacted. If either the Eiectrician or the SETC had been at the work site.during restoration, or if the work activity been written to have Operations sign off for the~.
. restoration, Operations would have understood the desired position of YSO.
\\
Work Control Center notified the Shift Lead SRO that YSO could be restored. The Shift Lead SRO conferred with the CRS on restoring YSO, and they decided to proceed. The CRS assigned a different AO to restore YSO, informed the AO and Shift Lead SRO of the. steps he had directed the previous AO to perform, and identified the steps of SOP 30 requir~d to restore YSO..
The Shift Lead SRO and the AO went to perform the alignment of YSO. They observed the isolation handle, the source light indication and the switch's physical position, but they did not recognize their indications were different than expected. The AO placed the YSO bypass handle from normal to automatic. Because the isolation handle had not been restored to the "close" position, YSO failed to transfer and Y01 was de-energized.
l 4
CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED The following actions were taken. _
Event 1a.
- 1.
Refueling and Maintenance outage activities were temporarily suspended on November 18, 1996 to review and reinforce nuclear, radiation, and industrial/personnel safety concerns with all work groups on site. This event and several other events from the first two weeks of the outage were reviewed with all crews. A common theme running among the identified issues is the lack of-communications between work groups and alignment among workers.
- 2.
Three specific responsibilities were reinforced at the Operations Department stand down meetings. These were:
Shift Supervisors, are to identify Operations activities from the outage schedule with an understanding of the relationship between these activiti~s
. and others. It is intended that this understanding will contribute to well-informed decision making ~ithin the Operations organization.
. Work Control Center Senior Reactor Operators are to direct work activities
- having Operations involvement to Control Room personnel for authorization.
.
- This is to provide interfacing work documents physically to the individual.s.
who will be performing the activity, better communications between Operations and other. work discipline* personnel, and improve the information flow to those individuals who will be directing the activity>
Control. Room personnel are to assure they have a complete understanding
- of activities requested of them and that proper alignments have been made.
- 3.
.. The control rod drive blades and racks were inspected for damage due the trip occurring with a reduced water level. No damage was observed on any of the control rod drive blades or racks.
Event 1b.
In addition to actions 1 and 2 from above, the following actions were taken.
- 1.
Shift Supervisor, CRS, Lead SRO, AO and other Operations personnel involved discussed this event and the barriers that could have prevented it. The 5
-~*.
-discussion included responsibilities for proper communications, pre-job briefings, equipment operation, self checking and other aspects of operator ccmduct.
- 2.
Shift Operations Supervisor has briefed the Shift Supervisors and SROs on the need to identify and conduct pre-job briefings. The expectation to conduct pre-
.. - -. job briefings whenever coordination between two or more work groups is required has been re-established.
- 3.
- Maintenance and Construction Manager reinforced pre-job briefing expectations with maintenance and construction supervision personnel using this event as an example where a collective pre-job briefing may have prevented the event.
CORRECTIVE ACTIONS REMAINING TO BE TAKEN TO AVOID FURTHER VIOLATIONS.
Periodic activity, SPS050, will be revised to use the terminology of operating,
- procedure, SOP 30, and to make the steps to align automatic transfer switch, YSO, an Operations responsibility with the appropriate sign offs.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED
- CPCo is now in full compliance.
6
Y-50 AUTOMATIC TRANSFER SWITCH I
I I !
i i
I I
I I
I i i I.
EMERGENCY BYPASS HANDLE. CE...
AUTOMATIC OfEN.
- NORMAL T
a.£ROENCY TCJL..IU:XX NORMAL m FAm SWITOf SOURa (KM!Nl'ARY)
SOURCE
- AVAJl...&BIE AVAILABIP
- .. 0 11tANSFER TE$t' LOAD
(])NNECJE)
TO NORMAL
- 1t1SI' NORMAL
(.~)
- 1MCC#2!
l
~
RESET ro*
MCC # 1 I*
I NORMAL 1* *1..-~~~~~~~~~~~~~~~~~~~~......1 7
~
NRC VIOLATION
.2.)
10 CFR 50, Appendix B, Criterion Ill, Design Control, requires, in part," that
. design control measures "... shall include provisions to assure that appropriate quality standards are specified and included in design documents...," and that
"... design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of.. design reviews. Design changes, including field changes, shall be subject to design control measures commensurate with those applied to the original design... "
Palisades Administrative Procedure 9.31, "Temporary Modification Control,"
Revision *12, Paragraph 7.1.8, required that a technical review be conducted to verify that instructions for installation were correct..
Contrary to the above~
On November 6, 1996, Temporary Modification (TM)96-050 to the containment polar came did not contain correct installation instructions for replacement of a single solenoid with two solenoids. The original solenoid was*hard mounted and was provided with adequate ventilation to prevent premature failure. As the result of inadequate preparation and review, TM 96-050 did not provide instructions for mounting the second of the two replacement solenoids. The*
second solenoid was installed utilizing duct tape and "tie-wtaps" in a manner which resulted in overheating and failure of the solenoid coil, and a subsequent.
- electrical fire..
This is a Severity Lev~l IV violation (Supplement 1 ).
CONSUMERS POWER COMPANY RESPONSE Consumers Power Company (CPCo) agrees with the violation as stated.
REASON FOR THE VIOLATION
. Based on the inspection data from the failed coils, the most likely cause of the failure on the trolley crane brake coils is the manner which the coils were mounted. This
- inadequate mounting design was caused by the failure of design personnel to.identify soler:ioid heat dissipation as critical characteristic during the design process.
8
. - --- -~----
Discussion
. A temporary modification was required to the containment Polar Crane due to a failure of the existing 460VAC solenoid on the trolley brake actuator. No replacement 460VAC solenoid was available. When this solenoid is energized, the actuator releases the braking mechanism on the crane trolley motor.
)
The modification involved the replacement of the original 460VAC coil with ~o 230VAC coils. One of the 230V coils would be installed in the position of the original coil and the second would be used as a dummy load to provide a voltage drop across it. This would result in a voltage dividing circuit which would divide the 460 volts from the circuit supply in half thus applying 230 volts across each coil. To ensure that the impedance w<ifs matched a spare plunger was inserted into the dummy coil and fixed in the inserted position using duct tape. The dummy coil was then tye-wrapped to a
. support bar and additional tape was wrapped around it.
The temporary modification to substitute the 230VAC coils for the 460VAC was an acceptable design. However, the dummy coil mounting design was focused on making sure the coil did not come loose and fall into the debris free zone inside containment. *
. Potential overheating of the dummy coil was not considered in the design.
The Polar Crane was in service with the temporary modification in place for approximately 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> before failure occurred. With high usage of the Polar Crane.
and repeated starts and stops on the trolley crane motor, the additional layers of tape on the dummy coil caused chronic overheating of the dummy coil. The epoxy insulating material became hot enough to melt and the dummy coil wires shorted togetheL This allowed the full 460 volts to be applied across the 230VAC working coil, causing its failure. The smoke and. arcing observed was the result of the dummy coil overheating, causing the duct tape to catch fire and burn. No evidence of arcing to the support structure was found around either coil.
CORRECTIVE ACTIONS TAKEN AND RESULTS ACHIEVED
- 1.
- The two 230 volt coils were replaced with a new. 460 volt coil. It has been in use
- without incident since it was installed..
- 2.
This event was reviewed as a lessons learned with all Design Engineering at a department stand down meeting. Discussions covered conditions leading to the event, and the need for Design Engineering to consider all operating characteristics in design.
9
CORRECTIVE ACTIONS REMAINING TO BE TAKEN TO AVOID FURTHER VIOLATIONS
- 1.
A review of all installed temporary modifications will be conducted to verify that acceptable standards were used for installation.
2.*
The Temporary Modification process will be reviewed to assure that adequate guidance is provided to the design engineer for providing installation instructions, arid for verifying that the temporary modification was installed as intended by the design.
DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED CPCo is in full compliance..
- 10