ML17318A265: Difference between revisions

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{{#Wiki_filter:A9
{{#Wiki_filter:A9
  ~ ~
~
AVERAGE DA(LY U.'(IT PON:"R L:-VH DOCZ=-V    io. 50->>5 DAr=
~
CO~PL:-Tr D BY T=t ~HOWL-   616-465-5901 lee)
AVERAGE DA(LYU.'(ITPON:"R L:-VH DOCZ=-Vio.
AUgUst 1979 pq~
50->>5 DAr=
DAY       AVERAGE DAlLYPOKER L It'EL                                 DAY      AVERAGc. DAlLYPOKER LEVEL (M'Ke-i                                                                     (MWe..'(e! )
CO~PL:-Tr D BY T=t ~HOWL-616-465-5901 pq~
982                                          17                            1,035 1 025                                                                           1,034 1,006                                           19 1,034 995                                                                         .1,032 997                                                                         1 035 1,005                                                                           1,035 1 020 1,018                                                                           1,030 1,021                                                                           1 017 1,                                                                             1 030 014',030 1 030 1,034                                                                           1 031 1,029                                           'l9                           1,031 l3 1, 029                                          30                            1,031 1,036                                                                          1,030 l5                  1 035 lNSTRUCT)ONS O" '"'s:at-at 'v '"
AUgUst 1979 DAY AVERAGE DAlLYPOKER L It'EL (M'Ke-i lee)
I v .-a~     '- 'y "!: ei:<<et ie'e::.-..":t'e   et ter ae.'", -'av t.-. ~
982 17 1,035 DAY AVERAGc. DAlLYPOKER LEVEL (MWe..'(e! )
        '3J 1Ja ~ 5'ielJ ~rracat:.
l3 l5 1 025 1,006 995 997 1,005 1 020 1,018 1,021 1,
c   ~                                                             {~l:7 i )
014',030 1,034 1,029 1, 029 1,036 1 035 19
'l9 30 1,034 1,034
.1,032 1 035 1,035 1,030 1 017 1 030 1 030 1 031 1,031 1,031 1,030 lNSTRUCT)ONS O" '"'s:at-at
'v '"
v.-a~ '- 'y "!: ei:<<et ie'e::.-..":t'e et ter ae.'", -'av t.-.
~ '-
I
'3J 1Ja
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c
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V9999OO&/P
V9999OO&/P


OPERATE G DATA REPORT DOCI uT NO.,
OPERATE G DATAREPORT DOCI uT NO.,
D*rZ ~>-<->
D*rZ ~>-<->
COifPLETED SY     ~~i'l3.<<t ypjppvoyp 616-465-5901'PERATING STATUS Notes Donald C. Cook         1
COifPLETED SY ~~i'l3.<<t ypjppvoyp 616-465-5901'PERATING STATUS Donald C. Cook 1
: 3. Licensed Thermal Power (MWt):
: 3. Licensed Thermal Power (MWt):
3250 1089
: 4. Namephte Rating (Gross MWe)!
: 4. Namephte Rating (Gross MWe)!
1054 S. Design EIectrIM R" ting (Net MWe):
S. Design EIectrIM R"ting (Net MWe):
1080
: 6. !!Iaximum Dependable Capacity (Gross MWe)t
: 6. !!Iaximum Dependable Capacity (Gross MWe) t 1044
: 7. Maximum Dependable Capacity (Net ifWe}:
: 7. Maximum Dependable Capacity (Net ifWe}:
S. IfChanges Occur in Capacity Ratings (Items Number       3 Through 7) Since Last Report. Give Reasons:
3250 1089 1054 1080 1044 Notes S. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
: 9. Power Level To Which Restricted,   IfAny (i iet ibfWe):
: 9. Power Level To Which Restricted, IfAny (iiet ibfWe):
: 10. Reasons For Restrictions, If Any:
: 10. Reasons For Restrictions, IfAny:
This Month             Yr:to-Date           Cumuhtive
This Month Yr:to-Date Cumuhtive
: 11. Hours In Reporting Period                                 7 4                  5  831 744                  3  350.1                    30,561.8
: 11. Hours In Reporting Period
: 12. Number Of Hours Reactor Was C;;tiM Re" ctor Reserve Shutdown Houa                               0                        0                                  463 13.
: 12. Number Of Hours Reactor Was C;;tiM
: 14. Hours Gener! tor On. Line 744                  3,279.2*                    29            692.5*
: 13. Re"ctor Reserve Shutdown Houa
0                        0                                  321
: 14. Hours Gener! tor On.Line
: 15. U!us Reserve Shutdown Ho!ns 2,396,428            10 100 787            81,438,578
: 15. U!us Reserve Shutdown Ho!ns
: 16. Gross Thermal Ene~ Cene. ted (MWH) 789,220            3  340 010            26 629s670
: 16. Gross Thermal Ene~ Cene.
: 17. Gross Electric J Energy Generated (M>VH) 7    2            3  219,984            25,557,161
ted (MWH)
: 18. Net c1ectricai Energy Cenerated (MYiH) 100                      56.2                                  74.6
: 17. Gross ElectricJ Energy Generated (M>VH)
: 19. Unit Service Factor 100                      56.2                                  74.6
: 18. Net c1ectricai Energy Cenerated (MYiH)
: 19. Unit Service Factor
: 30. Unit Avaihbility Factor.
: 30. Unit Avaihbility Factor.
: 98. 1                  52.9                                  65. 9 Zl. Un!t Capacity'actor (Using iN!DC Net)
Zl. Un!t Capacity'actor (Using iN!DC Net)
'Z". Unit Caoacity Factor (Using DER Net)                           97.2                  52.4                                  60.6 2.4                                  5.8
'Z". Unit Caoacity Factor (Using DER Net)
    . Unit Forced Outage Rate
. Unit Forced Outage Rate
: 24. Shutdowns Scheduled Over Next 6 bfonths (Type. Date. and Du:ation of Each):
: 24. Shutdowns Scheduled Over Next 6 bfonths 7 4 744 0
"S. If Sh!.t Down At End Of Report P riod. Estimated Date of Startup:   ~
744 0
S. Units In Test Status (Poor to Commercial Opemtion):                           Force" st             Achieved INITIAL CRITICALITY INITIALELECTRICITY CO,'iDIERCIAL OPERATION
2,396,428 789,220 7
2 100 100
: 98. 1 97.2 5 831 3 350.1 0
3,279.2*
0 10 100 787 3 340 010 3 219,984 56.2 56.2 52.9 52.4 2.4 (Type. Date. and Du:ation of Each):
30,561.8 463 29 692.5*
321 81,438,578 26 629s670 25,557,161 74.6 74.6
: 65. 9 60.6 5.8 "S. IfSh!.t Down At End Of Report P riod. Estimated Date of Startup:
~
S. Units In Test Status (Poor to Commercial Opemtion):
Force" st Achieved INITIAL CRITICALITY INITIALELECTRICITY CO,'iDIERCIALOPERATION


UNIT SIIUTI)O)VNS AND POWER REDUCTIONS                     I)OCKET NO.
UNITSIIUTI)O)VNS AND POWER REDUCTIONS I)OCKETNO.
U it.
U it.
                                                                            ~A. i         979 rl          =n C
~A. i 979 Nc).
Llccnscc O D4'                  Cause    & Corrcctivc Nc).           l)atc                         Vl rr                  Ilvci)t                                             Aclhnl to J
l)atc rl VlrrJ
Rcport sr E
=n
O
~ V)
                                                                                            ~                  Prevent Rccurrcncc
Llccnscc Ilvci)t Rcport sr C
                                                    ~ V)
O 4'D E ~
There were no unit*-shutdowns or power reductions.         The unit operated at essentially 100$ reactor power for the erttire month.
O Cause &Corrcctivc Aclhnl to Prevent Rccurrcncc There were no unit*-shutdowns or power reductions.
I': Fof cell        Reason:                                                 Method:                              Exhibit G Instru<<tions
The unit operated at essentially 100$ reactor power for the erttire month.
                                                                                                                                  ~
I': Fofcell S: SchclluIcII (9II7)
S: SchclluIcII      A-E(luipn)cnt Failufc (Explan))                         I -hlanual                          for Preparation ol')ata Il.hlaintcnancc or Tesl                                 2 Manual Scraln.                      I.:ntry Shccts for Li<<cnscc, C-Refueling                                             3-Aulonlatic Scran).                  Event Rcport (I.I!R) File (NUltl:G~
Reason:
D.Regulatory Rcstri<<lion                               -I-Other (Explain)                    Ol 6I )
A-E(luipn)cnt Failufc (Explan))
I: Operator 'I'raining & License I:xanlination F-AIIfninistrative G Oper J th)nlll Ll fof (I:xpiJhl)                                                           'I:xhibit I Saln<<Soul<<<<
Il.hlaintcnancc or Tesl C-Refueling D.Regulatory Rcstri<<lion I: Operator 'I'raining & License I:xanlination F-AIIfninistrative G Oper J th)nlll Llfof (I:xpiJhl)
                                                                                                                                ~
I l Other (Explain)
(9II7)                I l Other (Explain)
Method:
I -hlanual 2 Manual Scraln.
3-Aulonlatic Scran).
-I-Other (Explain)
Exhibit G
~ Instru<<tions for Preparation ol')ata I.:ntry Shccts for Li<<cnscc, Event Rcport (I.I!R)File (NUltl:G~
Ol 6I )
'I:xhibit I
~ Saln<<Soul<<<<


Docket No.:   50-315 Unit  Name:  D. C. Cook   Unit 01 Completed By:    R. S. Lease
Docket No.:
                                                  .Telephone:  (616) 465-5901 Date:  September 6, 1979 Page:  1 of2 MONTHLY OPERATING EXPERIENCES   -- AUGUST, 1979 Hi hli hts The Unit entered the reporting operating at 935 power and was increased to 99% August 1, 1979 and operated between 97K and 991 until August 14, 1979. A new core was being conditioned and operated with a narrow Fz margin.       Power was increased to 100K August 14, 1979 and maintained at this point other than where noted in the summary.
Unit Name:
Total electrical generation for the month       was 789,220 Mwh.
Completed By:
Summar 08/01/79 The   West Centrifugal Charging Pump was inoperable for a 2.5 hour period for removal of drain plugs from the inboard seal.
.Telephone:
08/06/79 -- The middle heater drain pump was removed from ser-vice for replacement of a pump seal. The pump was returned to service 8/13/79.
Date:
08/07/79 -- Steam 'Jet Air Ejector Radiation Monitor     R-15 failed.
Page:
50-315 D.
C.
Cook Unit 01 R.
S.
Lease (616) 465-5901 September 6,
1979 1 of2 MONTHLY OPERATING EXPERIENCES -- AUGUST, 1979 Hi hli hts The Unit entered the reporting operating at 935 power and was increased to 99% August 1, 1979 and operated between 97K and 991 until August 14, 1979.
A new core was being conditioned and operated with a narrow Fz margin.
Power was increased to 100K August 14, 1979 and maintained at this point other than where noted in the summary.
Total electrical generation for the month was 789,220 Mwh.
Summar 08/01/79 The West Centrifugal Charging Pump was inoperable for a 2.5 hour period for removal of drain plugs from the inboard seal.
08/06/79 -- The middle heater drain pump was removed from ser-vice for replacement of a pump seal.
The pump was returned to service 8/13/79.
08/07/79 -- Steam 'Jet Air Ejector Radiation Monitor R-15 failed.
Repairs were made and the monitor returned to ser-vice 8/10/79.
Repairs were made and the monitor returned to ser-vice 8/10/79.
08/14/79 -- The "B" train   of heaters for   Boron Injection Tank failed when a   heater went to ground. The "A" train remained =operable and -in. servi.ce. The. grounded-heater was replaced and the "B" train returned to operable 8/17/79.
08/14/79 08/16/79 08/23/79
08/16/79    The Reciprocating Charging Pump was removed from service for repairs to leaking stuffing boxes.
-- The "B" train of heaters for Boron Injection Tank failed when a heater went to ground.
The "A" train remained =operable and -in. servi.ce.
The. grounded-heater was replaced and the "B" train returned to operable 8/17/79.
The Reciprocating Charging Pump was removed from service for repairs to leaking stuffing boxes.
The pump was again operable 8/16/79.
The pump was again operable 8/16/79.
08/23/79    The Turbine Driven Auxiliary Feedwater Pump was inoperable for a 3. 5 hour period to remove the automatic transfer function from the Turbine power supply.
The Turbine Driven Auxiliary Feedwater Pump was inoperable for a 3. 5 hour period to remove the automatic transfer function from the Turbine power supply.


                                                                                            ~ 1
~
'I'lb'sllIVEt If~ 3a, II ~
1
                            ~ P L 4 f '2B 4>> s klllk<. 'l < '~, 'J '"'0 < 'fll f k'~ e J 4
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s klllk<.
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Docket No,:   5Q-315 Unit  Name:  D. C. Cook Unit 81 Completed By:    R. S. Lease Telephone:    (616) 465-5901 Date:  September 6, 1979 Page:  2of2 08/25/79 -- Power was reduced to 9QA and again returned to 100/
Docket No,:
between the hours of 0005 and 0713   for testing of Turbine Control Valves.
Unit Name:
Completed By:
Telephone:
Date:
Page:
5Q-315 D.
C.
Cook Unit 81 R.
S.
Lease (616) 465-5901 September 6,
1979 2of2 08/25/79 -- Power was reduced to 9QA and again returned to 100/
between the hours of 0005 and 0713 for testing of Turbine Control Valves.


IH DOCKET NO.      50-315 UNIT  NAME      D. C. Cook  - Unit No. 1 DATE            9-14-79 COMPLETED BY    B. A. Svensson TELEPHONE        616 465-5901 MAJOR SAFETY-RELATED MAINTENANCE AUGUST, 1979 Boron    injection tank train 'B'eater grounded out.        The  heater was  replaced and operability checked satisfactorily.
IH
No. 4 steam    generator stop valve test selector valve MMO-240 would not    move  to position B. Torque switch was found to be malfunctioning. Replaced torque switch and valve operated s ati s factorily.
HARV-302, CVCS    letdown to the  VCT or demineralizers,  limit switch failed. The  failed limit switch prevented    normal valve operation.
The  limit switch    actuation  arm required replacement. The  correct operation of    the valve and  indication lights  were verified.
The  release flow rate meter on the waste disposal system control panel was reading low. RFI-285 release flow rate meter and transmitter were calibrated and operation verified.
J Point    83 of containment air temperature recorder SG-18      was indica-ting full scale. The RTD fo'r upper containment quad 3        was found to  be  open. Replacing the  RTD corrected the problem.
Protection channel I delta T/Taverage would periodically spike upward giving spurious overtemperature and overpower channel trips. The cold-leg RTD was found to be the. problem. The spare cold-leg RTD was placed in service.
Ice condenser temperature recorder points 1 through 6 were indica-ting full scale. The problem was traced to a defective relay card in the instrument room. Replacing the relay card corrected the problem.
The  glycol return valve VCR-21 limit switch was causing a ground on the AB battery.      The switch box was cleaned out and the internals of the limit switch were replaced to correct the ground.
The  nuclear emergency alarm, when tested from Unit.2, did not sound.
A  faulty transform r was replaced, and the system tested satisfactorily.


J \}}
DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE MAJOR SAFETY-RELATED MAINTENANCE 50-315 D.
C.
Cook - Unit No.
1 9-14-79 B. A. Svensson 616 465-5901 AUGUST, 1979 Boron injection tank train 'B'eater grounded out.
The heater was replaced and operability checked satisfactorily.
No.
4 steam generator stop valve test selector valve MMO-240 would not move to position B.
Torque switch was found to be malfunctioning.
Replaced torque switch and valve operated s ati s factorily.
HARV-302, CVCS letdown to the VCT or demineralizers, limit switch failed.
The failed limit switch prevented normal valve operation.
The limit switch actuation arm required replacement.
The correct operation of the valve and indication lights were verified.
The release flow rate meter on the waste disposal system control panel was reading low.
RFI-285 release flow rate meter and transmitter were calibrated and operation verified.
J Point 83 of containment air temperature recorder SG-18 was indica-ting full scale.
The RTD fo'r upper containment quad 3 was found to be open.
Replacing the RTD corrected the problem.
Protection channel I delta T/Taverage would periodically spike upward giving spurious overtemperature and overpower channel trips.
The cold-leg RTD was found to be the. problem.
The spare cold-leg RTD was placed in service.
Ice condenser temperature recorder points 1 through 6 were indica-ting full scale.
The problem was traced to a defective relay card in the instrument room.
Replacing the relay card corrected the problem.
The glycol return valve VCR-21 limit switch was causing a ground on the AB battery.
The switch box was cleaned out and the internals of the limit switch were replaced to correct the ground.
The nuclear emergency
: alarm, when tested from Unit.2, did not sound.
A faulty transform r was replaced, and the system tested satisfactorily.
 
J
\\}}

Latest revision as of 16:50, 7 January 2025

Monthly Operating Rept for Aug 1979
ML17318A265
Person / Time
Site: Cook 
Issue date: 09/05/1979
From: Gillett W
INDIANA MICHIGAN POWER CO.
To:
Shared Package
ML17318A264 List:
References
NUDOCS 7909200316
Download: ML17318A265 (9)


Text

A9

~

~

AVERAGE DA(LYU.'(ITPON:"R L:-VH DOCZ=-Vio.

50->>5 DAr=

CO~PL:-Tr D BY T=t ~HOWL-616-465-5901 pq~

AUgUst 1979 DAY AVERAGE DAlLYPOKER L It'EL (M'Ke-i lee)

982 17 1,035 DAY AVERAGc. DAlLYPOKER LEVEL (MWe..'(e! )

l3 l5 1 025 1,006 995 997 1,005 1 020 1,018 1,021 1,

014',030 1,034 1,029 1, 029 1,036 1 035 19

'l9 30 1,034 1,034

.1,032 1 035 1,035 1,030 1 017 1 030 1 030 1 031 1,031 1,031 1,030 lNSTRUCT)ONS O" '"'s:at-at

'v '"

v.-a~ '- 'y "!: ei:<<et ie'e::.-..":t'e et ter ae.'", -'av t.-.

~ '-

I

'3J 1Ja

~5'ielJ ~rracat:.

c

~

{~l:7i )

V9999OO&/P

OPERATE G DATAREPORT DOCI uT NO.,

D*rZ ~>-<->

COifPLETED SY ~~i'l3.<<t ypjppvoyp 616-465-5901'PERATING STATUS Donald C. Cook 1

3. Licensed Thermal Power (MWt):
4. Namephte Rating (Gross MWe)!

S. Design EIectrIM R"ting (Net MWe):

6. !!Iaximum Dependable Capacity (Gross MWe)t
7. Maximum Dependable Capacity (Net ifWe}:

3250 1089 1054 1080 1044 Notes S. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:

9. Power Level To Which Restricted, IfAny (iiet ibfWe):
10. Reasons For Restrictions, IfAny:

This Month Yr:to-Date Cumuhtive

11. Hours In Reporting Period
12. Number Of Hours Reactor Was C;;tiM
13. Re"ctor Reserve Shutdown Houa
14. Hours Gener! tor On.Line
15. U!us Reserve Shutdown Ho!ns
16. Gross Thermal Ene~ Cene.

ted (MWH)

17. Gross ElectricJ Energy Generated (M>VH)
18. Net c1ectricai Energy Cenerated (MYiH)
19. Unit Service Factor
30. Unit Avaihbility Factor.

Zl. Un!t Capacity'actor (Using iN!DC Net)

'Z". Unit Caoacity Factor (Using DER Net)

. Unit Forced Outage Rate

24. Shutdowns Scheduled Over Next 6 bfonths 7 4 744 0

744 0

2,396,428 789,220 7

2 100 100

98. 1 97.2 5 831 3 350.1 0

3,279.2*

0 10 100 787 3 340 010 3 219,984 56.2 56.2 52.9 52.4 2.4 (Type. Date. and Du:ation of Each):

30,561.8 463 29 692.5*

321 81,438,578 26 629s670 25,557,161 74.6 74.6

65. 9 60.6 5.8 "S. IfSh!.t Down At End Of Report P riod. Estimated Date of Startup:

~

S. Units In Test Status (Poor to Commercial Opemtion):

Force" st Achieved INITIAL CRITICALITY INITIALELECTRICITY CO,'iDIERCIALOPERATION

UNITSIIUTI)O)VNS AND POWER REDUCTIONS I)OCKETNO.

U it.

~A. i 979 Nc).

l)atc rl VlrrJ

=n

~ V)

Llccnscc Ilvci)t Rcport sr C

O 4'D E ~

O Cause &Corrcctivc Aclhnl to Prevent Rccurrcncc There were no unit*-shutdowns or power reductions.

The unit operated at essentially 100$ reactor power for the erttire month.

I': Fofcell S: SchclluIcII (9II7)

Reason:

A-E(luipn)cnt Failufc (Explan))

Il.hlaintcnancc or Tesl C-Refueling D.Regulatory Rcstri<<lion I: Operator 'I'raining & License I:xanlination F-AIIfninistrative G Oper J th)nlll Llfof (I:xpiJhl)

I l Other (Explain)

Method:

I -hlanual 2 Manual Scraln.

3-Aulonlatic Scran).

-I-Other (Explain)

Exhibit G

~ Instru<<tions for Preparation ol')ata I.:ntry Shccts for Li<<cnscc, Event Rcport (I.I!R)File (NUltl:G~

Ol 6I )

'I:xhibit I

~ Saln<<Soul<<<<

Docket No.:

Unit Name:

Completed By:

.Telephone:

Date:

Page:

50-315 D.

C.

Cook Unit 01 R.

S.

Lease (616) 465-5901 September 6,

1979 1 of2 MONTHLY OPERATING EXPERIENCES -- AUGUST, 1979 Hi hli hts The Unit entered the reporting operating at 935 power and was increased to 99% August 1, 1979 and operated between 97K and 991 until August 14, 1979.

A new core was being conditioned and operated with a narrow Fz margin.

Power was increased to 100K August 14, 1979 and maintained at this point other than where noted in the summary.

Total electrical generation for the month was 789,220 Mwh.

Summar 08/01/79 The West Centrifugal Charging Pump was inoperable for a 2.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period for removal of drain plugs from the inboard seal.

08/06/79 -- The middle heater drain pump was removed from ser-vice for replacement of a pump seal.

The pump was returned to service 8/13/79.

08/07/79 -- Steam 'Jet Air Ejector Radiation Monitor R-15 failed.

Repairs were made and the monitor returned to ser-vice 8/10/79.

08/14/79 08/16/79 08/23/79

-- The "B" train of heaters for Boron Injection Tank failed when a heater went to ground.

The "A" train remained =operable and -in. servi.ce.

The. grounded-heater was replaced and the "B" train returned to operable 8/17/79.

The Reciprocating Charging Pump was removed from service for repairs to leaking stuffing boxes.

The pump was again operable 8/16/79.

The Turbine Driven Auxiliary Feedwater Pump was inoperable for a 3. 5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> period to remove the automatic transfer function from the Turbine power supply.

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Docket No,:

Unit Name:

Completed By:

Telephone:

Date:

Page:

5Q-315 D.

C.

Cook Unit 81 R.

S.

Lease (616) 465-5901 September 6,

1979 2of2 08/25/79 -- Power was reduced to 9QA and again returned to 100/

between the hours of 0005 and 0713 for testing of Turbine Control Valves.

IH

DOCKET NO.

UNIT NAME DATE COMPLETED BY TELEPHONE MAJOR SAFETY-RELATED MAINTENANCE 50-315 D.

C.

Cook - Unit No.

1 9-14-79 B. A. Svensson 616 465-5901 AUGUST, 1979 Boron injection tank train 'B'eater grounded out.

The heater was replaced and operability checked satisfactorily.

No.

4 steam generator stop valve test selector valve MMO-240 would not move to position B.

Torque switch was found to be malfunctioning.

Replaced torque switch and valve operated s ati s factorily.

HARV-302, CVCS letdown to the VCT or demineralizers, limit switch failed.

The failed limit switch prevented normal valve operation.

The limit switch actuation arm required replacement.

The correct operation of the valve and indication lights were verified.

The release flow rate meter on the waste disposal system control panel was reading low.

RFI-285 release flow rate meter and transmitter were calibrated and operation verified.

J Point 83 of containment air temperature recorder SG-18 was indica-ting full scale.

The RTD fo'r upper containment quad 3 was found to be open.

Replacing the RTD corrected the problem.

Protection channel I delta T/Taverage would periodically spike upward giving spurious overtemperature and overpower channel trips.

The cold-leg RTD was found to be the. problem.

The spare cold-leg RTD was placed in service.

Ice condenser temperature recorder points 1 through 6 were indica-ting full scale.

The problem was traced to a defective relay card in the instrument room.

Replacing the relay card corrected the problem.

The glycol return valve VCR-21 limit switch was causing a ground on the AB battery.

The switch box was cleaned out and the internals of the limit switch were replaced to correct the ground.

The nuclear emergency

alarm, when tested from Unit.2, did not sound.

A faulty transform r was replaced, and the system tested satisfactorily.

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