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| number = ML17333B038
| number = ML17333B038
| issue date = 09/15/1997
| issue date = 09/15/1997
| title = Responds to NRC 970815 Ltr Re Violations Noted in Insp Repts 50-315/97-09 & 50-316/97-09 on 970505-23.Corrective Actions: Calculation DC-D-1-SI-F101 Was Revised & Approved on 970602 to Address Cited Discrepancies
| title = Responds to NRC Re Violations Noted in Insp Repts 50-315/97-09 & 50-316/97-09 on 970505-23.Corrective Actions: Calculation DC-D-1-SI-F101 Was Revised & Approved on 970602 to Address Cited Discrepancies
| author name = FITZPATRICK E
| author name = Fitzpatrick E
| author affiliation = INDIANA MICHIGAN POWER CO.
| author affiliation = INDIANA MICHIGAN POWER CO.
| addressee name =  
| addressee name =  
Line 11: Line 11:
| contact person =  
| contact person =  
| document report number = 50-315-97-09, 50-315-97-9, 50-316-97-09, 50-316-97-9, AEP:NRC:1260H, NUDOCS 9709230028
| document report number = 50-315-97-09, 50-315-97-9, 50-316-97-09, 50-316-97-9, AEP:NRC:1260H, NUDOCS 9709230028
| title reference date = 08-15-1997
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE
| page count = 19
| page count = 19
}}
}}
See also: [[followed by::IR 05000315/1997009]]


=Text=
=Text=
{{#Wiki_filter:CATEGORY l REGULATORY
{{#Wiki_filter:CATEGORY l REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
INFORMATION
DOCKET 05000315 05000316 NOTES:
DISTRIBUTION
CCESSION NBR:9709230028 DOC.DATE: 97/09/15 NOTARIZED: YES FACIL:50-315 Donald C.
SYSTEM (RIDS)DOCKET 05000315 05000316 NOTES: CCESSION NBR:9709230028
Cook Nuclear Power Plant, Unit 1, Indiana M
DOC.DATE: 97/09/15 NOTARIZED:
, 50-316 Donald C.
YES FACIL:50-315
Cook Nuclear Power Plant, Unit 2, Indiana M
Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M , 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M AUTH.NAME AUTHOR AFFILIATION
AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.
FITZPATRICK,E.
Indiana Michigan Power Co.
Indiana Michigan Power Co.RECIP.NAME
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
RECIPIENT AFFILIATION
 
Document Control Branch (Document Control Desk)SUBJECT: Responds to NRC 970815 ltr re violations
==SUBJECT:==
noted in insp repts 50-315/97-09
Responds to NRC 970815 ltr re violations noted in insp repts 50-315/97-09 a 50-316/97-09 on 970505-23.Corrective actions:
a 50-316/97-09
calculation DC-D-1-SI-F101 revised a revised safety review incorporating correct MDAFW pump start time approved.
on 970505-23.Corrective
DISTRIBUTION CODE:
actions: calculation
IE01D COPIES RECEIVED:LTR ENCL SIZE-TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response INTERNAL:
DC-D-1-SI-F101
RECIPIENT ID CODE/NAME PD3-3 PD AEOD/SPD/RAB DEDRO NRR/DISP/PIPB NRR/DRPM/PECB NUDOCS-ABSTRACT OGC/HDS2 COPIES RECIPIENT LTTR ENCL ID CODE/NAME 1
revised a revised safety review incorporating
1 HICKMANiJ 1
correct MDAFW pump start time approved.DISTRIBUTION
AEODf&T~
CODE: IE01D COPIES RECEIVED:LTR
1
ENCL SIZE-TITLE: General (50 Dkt)-Insp Rept/Notice
+FILE CEHTE~RQN 1
of Violation Response INTERNAL: RECIPIENT ID CODE/NAME PD3-3 PD AEOD/SPD/RAB
/DRC@HHFB 1
DEDRO NRR/DISP/PIPB
NRR/DRPM/PERB 1
NRR/DRPM/PECB
OE DIR 1
NUDOCS-ABSTRACT
RGN3 FILE 01 COPIES LTTR ENCL 1
OGC/HDS2 COPIES RECIPIENT LTTR ENCL ID CODE/NAME 1 1 HICKMANiJ 1 AEODf&T~1+FILE CEHTE~RQN 1/DRC@HHFB 1 NRR/DRPM/PERB
1 1
1 OE DIR 1 RGN3 FILE 01 COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 0 R EXTERNAL LITCO BRYCE g J H NRC PDR 1 1 NOAC 1 1 NUDOCS FULLTEXT 1 1 1 1 D 0 N 0 NOTE TO ALL"RIDS" RECIPIENTS:
1 1
PLEASE HELP US TO REDUCE WASTE.TO HAVE YOUR NAME OR ORGANIZATION
1 1
REMOVED FROM DISTRIBUTION
1 1
LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD)ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR 18 ENCL 18  
1 1
0  
1 1
indiana Michigan Power Company 500 Circle Orive Buchanan, Mi 491071395 INDIANA ItrIICHIGAN
1 0
PWER September 15, 1997 AEP:NRC:1260H
R EXTERNAL LITCO BRYCE g J H
10'CFR 2.201 Docket Nos.: 50-315 50-316 U.S.Nuclear Regulatory
NRC PDR 1
Commission
1 NOAC 1
ATTN: Document Control Desk Washington, D.C.20555 Gentlemen:
1 NUDOCS FULLTEXT 1
Donald C.Cook Nuclear Plant Units 1 and 2 NRC INSPECTION
1 1
REPORTS NO.50-315/97009 (DRP)AND 50-316/97009 (DRP)REPLY TO NOTICE OF VIOLATION This letter is in response to a letter from G~E.Grant, dated August 15, 1997, that forwarded a notice of two violations
1 D
of NRC requirements
0 N
to Cook Nuclear Plant.The violations
0 NOTE TO ALL "RIDS" RECIPIENTS:
were identified
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD)
during the operational
ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR 18 ENCL 18
safety team inspection (OSTI)conducted by the NRC from May 5, 1997, to May 23, 1997.The attachment
 
contains our response to these violations.
0
Commitments
 
were made by Cook Nuclear Plant personnel to the NRC OSTI.The inspectors
indiana Michigan Power Company 500 Circle Orive Buchanan, Mi 491071395 INDIANA ItrIICHIGAN PWER September 15, 1997 AEP:NRC:1260H 10'CFR 2.201 Docket Nos.:
identified
50-315 50-316 U. S. Nuclear Regulatory Commission ATTN:
concerns related to valve descriptions
Document Control Desk Washington, D.
on labels, drawings, and in procedures, and they had concerns related to our program for sealed valves.The characterization
C.
and detail of these commitments
20555 Gentlemen:
in the inspection
Donald C.
report reflects our intent.when the commitments
Cook Nuclear Plant Units 1 and 2
were made.The second violation relates to the issue of design control.While reviewing the OSTI report and preparing this response, Cook Nuclear Plant underwent an NRC architect engineering (AE)team inspection.
NRC INSPECTION REPORTS NO. 50-315/97009 (DRP)
The AE inspection
AND 50-316/97009 (DRP)
identified
REPLY TO NOTICE OF VIOLATION This letter is in response to a letter from G ~
design control issues, some that are similar to those cited in this violation.
E. Grant, dated August 15, 1997, that forwarded a notice of two violations of NRC requirements to Cook Nuclear Plant.
Resolution
The violations were identified during the operational safety team inspection (OSTI) conducted by the NRC from May 5, 1997, to May 23, 1997.
of the overall design control issue will require action beyond that which is committed to here.Those actions will be defined in the course of addressing
The attachment contains our response to these violations.
the AE team inspection
Commitments were made by Cook Nuclear Plant personnel to the NRC OSTI.
issues.The nuclear engineering
The inspectors identified concerns related to valve descriptions on labels,
organization, along with our entire nuclear generation
: drawings, and in procedures, and they had concerns related to our program for sealed valves.
group, understands
The characterization and detail of these commitments in the inspection report reflects our intent. when the commitments were made.
the importance
The second violation relates to the issue of design control.
of error free human performance
While reviewing the OSTI report and preparing this response, Cook Nuclear Plant underwent an NRC architect engineering (AE) team inspection.
and attention to detail, and to having a design basis that is clear, understandable, and retrievable.
The AE inspection identified design control issues, some that are similar to those cited in this violation.
We believe that a first step was taken on September 2, 1997, when standards for technical information
Resolution of the overall design control issue will require action beyond that which is committed to here.
exchange and use in the nuclear engineering
Those actions will be defined in the course of addressing the AE team inspection issues.
9'709'230028
The nuclear engineering organization, along with our entire nuclear generation
9709i5 PDR ADQCK 050003%5 8 PDR r.~~0,<iQ ,,s llllllllilllliIIIJlllllllllllliillilf
: group, understands the importance of error free human performance and attention to detail, and to having a design basis that is clear, understandable, and retrievable.
ill
We believe that a first step was taken on September 2,
U.S.Nuclear Regulatory
: 1997, when standards for technical information exchange and use in the nuclear engineering 9'709'230028 9709i5 PDR ADQCK 050003%5 8
Commission
PDR r.~~0,<iQ
Page 2 AEP: NRC: 1260H organization
,,s llllllllilllliIIIJlllllllllllliillilf ill
were formally established.
 
The objective of the guidance is to provide assurances
U. S. Nuclear Regulatory Commission Page 2
that technical information
AEP: NRC: 1260H organization were formally established.
is accurate, based on sound engineering
The objective of the guidance is to provide assurances that technical information is
principles, properly conveyed, and properly, documented.
: accurate, based on sound engineering principles, properly conveyed, and properly, documented.
Sincerely, E.E.Fitzpatrick
Sincerely, E.
Vice President SWORN TO AND SUBSCRIBED
E. Fitzpatrick Vice President SWORN TO AND SUBSCRIBED BEFORE-ME THIS I'5 DAY OF ~LV', 1997 Notary Public My Commission Expires vlb Attachments JANWA%0N CAARYPQSC,BBNKNcoWn,e MYCOMMSSOMEXPtRES FEL 10, 1999 c:
BEFORE-ME THIS I'5 DAY OF~LV', 1997 Notary Public My Commission
A. A. Blind A. B. Beach MDEQ "
Expires vlb Attachments
DW & RPD NRC Resident Inspector J.
JAN WA%0N CAARYPQSC,BBNKNcoWn, e MYCOMMSSOM
R. Padgett
EXPtRES FEL 10, 1999 c: A.A.Blind A.B.Beach MDEQ" DW&RPD NRC Resident Inspector J.R.Padgett  
 
ATTACHMENT TO AEP:NRC: 1260H REPLY TO NOTICE OF VIOLATION:
ATTACHMENT
NRC INSPECTION REPORT NOS.
TO AEP:NRC: 1260H REPLY TO NOTICE OF VIOLATION:
50-315/97009 (DRP)
NRC INSPECTION
AND 50-316/97009 (DRP)
REPORT NOS.50-315/97009 (DRP)AND 50-316/97009 (DRP)  
 
Attachment
Attachment to AEP:NRC:1260H Page 1
to AEP:NRC:1260H
On May 23,
Page 1 On May 23, 1997, the NRC completed an operational
: 1997, the NRC completed an operational safety team inspection (OSTI) of Cook Nuclear Plant units 1
safety team inspection (OSTI)of Cook Nuclear Plant units 1 and 2 reactor facilities.
and 2 reactor facilities.
Two violations
Two violations of NRC requirements were identified during this inspection.
of NRC requirements
In accordance with the 60 FR
were identified
: 34381,
during this inspection.
'General Statement of Policy and Procedures for NRC Enforcement Actions", dated June 30, 1995, the violations and our responses are provided below.
In accordance
NRC Violation I "10 CFR 50, Appendix B, Criterion V, 'Instructions, Procedures, and Drawings, 'equires, in part, that activities affecting quality be prescribed by procedures of a type appropriate to the circumstances and be accomplished in accordance with these procedures.
with the 60 FR 34381,'General Statement of Policy and Procedures
Contrary to the above, On May 10,
for NRC Enforcement
: 1997, the inspectors identified that safety related Temporary Modification (TM) 1-95-1, which did not require an outage for restoration, had been assigned a
Actions", dated June 30, 1995, the violations
(administrative) date of August 27,
and our responses are provided below.NRC Violation I"10 CFR 50, Appendix B, Criterion V,'Instructions, Procedures, and Drawings,'equires, in part, that activities
: 1996, but had not been made a permanent installation through a design change or been removed as of May 10, 1997 as required by Plant Managers Procedure (PMP) 5040.MOD.OO1,
affecting quality be prescribed
'Temporary Modifications,'evision 7.
by procedures
B.
of a type appropriate
On May 7,
to the circumstances
: 1997, the inspectors identified that an activity affecting quality, the deenergization of the DG2AB inverter, was completed without placing 2-DGAB-INV-CB2 and 2-DGAB-INV-CB1 to off, contrary to steps 2.1.2 and 2.1.3 of procedure 02-OHP 4021.032.008
and be accomplished
'Aligning DG2AB Subsystems For Standby Operation,'evision 4, Attachment 7.
in accordance
This is a Severity Level IV violation (Supplement I)."
with these procedures.
Res onse to NRC Violation I The letter from Mr. Grant, and the notice of viola'on, state that Cook Nuclear Plant's staff provided the NRC with satisfactory information regarding the reasons for the violation, and the corrective actions taken and planned to correct both examples of the violation and prevent recurrence.
Contrary to the above, On May 10, 1997, the inspectors
The letter goes on to say
identified
: that, unless our corrective actions or our position are not accurately reflected in the inspection report, we are not required to further respond to this violation.
that safety related Temporary Modification (TM)1-95-1, which did not require an outage for restoration, had been assigned a (administrative)
We have reviewed inspection report no.
date of August 27, 1996, but had not been made a permanent installation
50-315/316)-97009 and determined that it reflects the circumstances of the examples in the violation as cited, as well as the corrective actions taken for each.
through a design change or been removed as of May 10, 1997 as required by Plant Managers Procedure (PMP)5040.MOD.OO1,'Temporary
Notwithstanding, for consistency in understanding, there is information in the discussion section of the inspection report that we wish to clarify.
Modifications,'evision
Several condition reports (CRs) are listed as having been reviewed in conjunction with'he 2AB EDG voltage regulator work.
7.B.On May 7, 1997, the inspectors
In particular, CR 97-1452 is listed with the title "Partial Clearance Addition Determined As Root Cause for Blown Fuse On 2AB EDG Inverter."
identified
We would like to clarify that the failure to deenergize the EDG inverter using the appropriate procedure is not
that an activity affecting quality, the deenergization
 
of the DG2AB inverter, was completed without placing 2-DGAB-INV-CB2
0
and 2-DGAB-INV-
 
CB1 to off, contrary to steps 2.1.2 and 2.1.3 of procedure 02-OHP 4021.032.008
Attachment to AEP:NRC:1260H Page 2
'Aligning DG2AB Subsystems
considered to be the root cause for the inverter fuse blowing during reenergization.
For Standby Operation,'evision
Subsequent investigation has determined that the failure to follow
4, Attachment
'the deenergization procedure was recognized before actions were taken to reenergize.
7.This is a Severity Level IV violation (Supplement
Prior to using the procedure to reenergize the inverter and place it back in service, the inverter circuit alignment was corrected and the integrity of the fuse was verified.
I)." Res onse to NRC Violation I The letter from Mr.Grant, and the notice of viola'on, state that Cook Nuclear Plant's staff provided the NRC with satisfactory
The fuse did blow coincident with performance of the procedure to reenergize the inverter.
information
NRC Violation ZZ "10 CFR 50, Appendix B, Criterion ZZZ, requires, in part, that mdasures be established to assure that the design basis are correctly translated into specifications, drawings, procedures, and instructions.
regarding the reasons for the violation, and the corrective
Design control measures shall provide for verifying or checking the adequacy of design.
actions taken and planned to correct both examples of the violation and prevent recurrence.
Contrary to the above, design control measures were not adequate to assure that the design basis was correctly translated into design modification documents:
The letter goes on to say that, unless our corrective
b.
actions or our position are not accurately
On May 7,
reflected in the inspection
: 1997, the inspectors identified that calculation DC-D-1-SZ-F101, 'Stress Analysis
report, we are not required to further respond to this violation.
& Load Generation for System 1-SI-F101 Per 12-MM-590,'sed the wrong moment arm and had a missing reaction force and moment.
We have reviewed inspection
On May 13, 1997, the inspectors identified that incorrect and non-conservative design input was used for the motor-driven auxiliary feedwater pump start time in the Safety Review Memorandum for the Setpoint Values for the Time Delay Pickup Relays in the AFW Flow Retention
report no.50-315/316)-97009
: Circuits, dated January 15,
and determined
: 1997, for design change package 12-DCP-0817,
that it reflects the circumstances
'Revise Aux. Feedwater Flow Retention Circuit.',
of the examples in the violation as cited, as well as the corrective
On May 13, 1997, the inspectors identified that a calculation for the seismic design adequacy of minor modification 12-MM-337 was not per formed.
actions taken for each.Notwithstanding, for consistency
The design package for 12-MM-337 indicated this calculation existed as DC-D-12-ES-116.
in understanding, there is information
This is a Severity Level IV violation (Sur,v>lement I)."
in the discussion
Res onse to NRC Violation ZZ 1.
section of the inspection
Admission or Denial of the Violation We admit to violation ZI as cited in the NRC notice of violation.
report that we wish to clarify.Several condition reports (CRs)are listed as having been reviewed in conjunction
Reasons for the Violation
with'he 2AB EDG voltage regulator work.In particular, CR 97-1452 is listed with the title"Partial Clearance Addition Determined
, The examples cited in the violation represent issues in the area of design control.
As Root Cause for Blown Fuse On 2AB EDG Inverter." We would like to clarify that the failure to deenergize
Concurrent with the review of the OSTI report and preparation of this
the EDG inverter using the appropriate
: response, Cook Nuclear Plant underwent an NRC architect engineering (AE) team inspection.
procedure is not  
This inspection identified design control issues, some that are similar to those cited in the violation.
0  
Zt is recognized that the three examples cited in this notice of violation must be
Attachment
 
to AEP:NRC:1260H
0
Page 2 considered
 
to be the root cause for the inverter fuse blowing during reenergization.
Attachment to AEP:NRC: 1260H Page 3
Subsequent
considered along with any new issues identified by the AE team inspection, relative to the overall issue of design control.
investigation
The circumstances of each issue cited in this notice of violation are discussed below.
has determined
Calculation DC-D-1-SI-F101, "Stress Analysis and Load Generation for System 1-SI-F101 per 12-MM-590",
that the failure to follow'the deenergization
was performed in support of adding a permanent vent line to the safety injection system (SIS) piping.
procedure was recognized
The inspector's review of the design change package identified errors made by the authors and overlooked by the calculation reviewers.
before actions were taken to reenergize.
The errors are characterized as insufficient attention to detail on the part of the engineers performing and reviewing the design change package.
Prior to using the procedure to reenergize
When calculating reaction forces, the length value of a piping span, used as a moment arm in the calculation, was transcribed from the input data presentation to the actual algebraic presentation incorrectly, from 37-5/8" to 35-5/8".
the inverter and place it back in service, the inverter circuit alignment was corrected and the integrity of the fuse was verified.The fuse did blow coincident
This discrepancy caused the maximum reaction force result to be incorrect, but in a
with performance
conservative direction.
of the procedure to reenergize
In another section of the package, values for reaction force and moment were omitted from a summary format.
the inverter.NRC Violation ZZ"10 CFR 50, Appendix B, Criterion ZZZ, requires, in part, that mdasures be established
These discrepancies consisted of numbers correctly derived in the body of the calculation on one page, but omitted from the summary on the following page.
to assure that the design basis are correctly translated
This problem was administrative in nature; no incorrect information was presented or used as a result.
into specifications, drawings, procedures, and instructions.
A third discrepancy related to this design change package was noted in the body of the inspection report, but not specified in the notice of violation.
Design control measures shall provide for verifying or checking the adequacy of design.Contrary to the above, design control measures were not adequate to assure that the design basis was correctly translated
The inspector made an observation that incorrect design information was stated in the safety review documentation.
into design modification
Our investigation concluded there was no discrepancy in the safety review input information.
documents:
The values of design temperature and pressure used by the safety reviewer were correct for the specific location where the new vent valve was to be installed.
b.On May 7, 1997, the inspectors
The engineer performing the design calculation conservatively used the highest bounding design temperature and pressure for the SIS as a whole.
identified
This approach is often adopted when the inherent safety margin of a design is such that the more stringent design requirements can be accommodated.
that calculation
The thought process involved in taking this approach was not clearly documented in the calculation package.
DC-D-1-SZ-F101,'Stress Analysis&Load Generation
Design change 12-DCP-0817 was developed to add a time delay relay to the auxiliary feedwater (AFW) flow retention actuation circuit to prevent spurious actuation from momentary outlet pressure
for System 1-SI-F101 Per 12-MM-590,'sed
: spikes, especially those that occur when the AFW pumps
the wrong moment arm and had a missing reaction force and moment.On May 13, 1997, the inspectors
 
identified
0
that incorrect and non-conservative
 
design input was used for the motor-driven
Attachment to AEP:NRC:1260H Page 4
auxiliary feedwater pump start time in the Safety Review Memorandum
automatically start.
f or the Setpoint Values f or the Time Delay Pickup Relays in the AFW Flow Retention Circuits, dated January 15, 1997, for design change package 12-DCP-0817,'Revise Aux.Feedwater Flow Retention Circuit.', On May 13, 1997, the inspectors
A safety review was performed by the design engineering organization for the addition of the time delay pick-up relay to the AFW system circuits.
identified
The nuclear safety and analysis section was asked to perform an evaluation of the setpoint value for the time delay relay.
that a calculation
The review performed by this group was intended to demonstrate that the magnitude of the time delay in the flow retention circuits would not adversely impact related accident analysis assumptions or safety margins.
for the seismic design adequacy of minor modification
In order to complete this review, the engineer needed to know how quickly the motor driven AFW pumps would start.
12-MM-337 was not per formed.The design package for 12-MM-337 indicated this calculation
An 'incorrect value of thirty seconds was used, based on a telephone conversation with the AFW system engineer at the plant site.
existed as DC-D-12-ES-116.
The system engineer communicated that the turbine driven AFW (TDAFW) pumps start and come up to speed within thirty seconds.
This is a Severity Level IV violation (Sur,v>lement
Surveillance data on the TDAFW pumps was available on the system engineers desk at the time.
I)." Res onse to NRC Violation ZZ 1.Admission or Denial of the Violation We admit to violation ZI as cited in the NRC notice of violation.
What the system engineer intended was that thirty seconds would bound the start time on the motor driven pumps.
Reasons for the Violation , The examples cited in the violation represent issues in the area of design control.Concurrent
Most often, in relation to safety analysis or T/S surveillance, the information of concern is a time which bounds the pump start, time.
with the review of the OSTI report and preparation
However, the safety reviewer understood that the thirty seconds would characterize the start time for the motor driven auxiliary feedwater (MDAFW) pumps.
of this response, Cook Nuclear Plant underwent an NRC architect engineering (AE)team inspection.
Based on surveillance measurements, the correct start time for the motor driven pumps is three seconds.
This inspection
Investigation into the reason for this incorrect input to the safety review concluded that it was poor communications between the involved engineers, and an incomplete understanding on the part of the system engineer as to the intended use of the information.
identified
One engineer believed the bounding start time was needed, while the other was trying to determine the shortest start time for the pumps.
design control issues, some that are similar to those cited in the violation.
Minor modification 12-MM-337 was performed to replace the emergency diesel generator (EDG) starting air system safety valves.
Zt is recognized
The NRC inspector indicated that the calculation for the seismic adequacy of the new valve type was not performed.
that the three examples cited in this notice of violation must be  
The design change package referenced calculation DC-D-12-ES-116.
0  
This referenced calculation was not intended to follow the typical format in what was then the calculation procedure.
Attachment
DC-D-12-ES-116 was a record-keeping and retrieval file for a
to AEP:NRC: 1260H Page 3 considered
number of individual reviews prepared for the replacement of non-identical valves.
along with any new issues identified
The file did contain the final approval letter from the structural design section documenting that the valve change had been reviewed.
by the AE team inspection, relative to the overall issue of design control.The circumstances
: However, we would have expected to find information in this file related to
of each issue cited in this notice of violation are discussed below.Calculation
 
DC-D-1-SI-F101,"Stress Analysis and Load Generation
Attachment to AEP:NRC:1260H Page 5
for System 1-SI-F101 per 12-MM-590", was performed in support of adding a permanent vent line to the safety injection system (SIS)piping.The inspector's
the decision making process, such as isometric data, weight data, and support location information.
review of the design change package identified
For unknown
errors made by the authors and overlooked
: reasons, this file did not contain the information that would have been expected pertaining to the review of the valve replacement of 12-MM-337.
by the calculation
The information could not be found. It was reconstructed and the new review was documented appropriately.
reviewers.
The file now contains the appropriate information and review documentation (performed in May 1997) that confirmed the conclusion of the original design approval letter.
The errors are characterized
Whether the file was
as insufficient
: lost, or the review never documented, this condition is characterized as insufficient attention to detail.
attention to detail on the part of the engineers performing
It resulted in the inability to retrieve design data or design basis related information.
and reviewing the design change package.When calculating
3.
reaction forces, the length value of a piping span, used as a moment arm in the calculation, was transcribed
Corrective Action Taken and Results Achieved b.
from the input data presentation
c Calculation DC-D-1-SI-F101, for the safety injection system stress
to the actual algebraic presentation
: analysis, was revised and approved on June 2,
incorrectly, from 37-5/8" to 35-5/8".This discrepancy
1997, to address the cited discrepancies.
caused the maximum reaction force result to be incorrect, but in a conservative
On May 29, 1997, a revised safety review, incorporating the correct MDAFW pump start time was approved by the plant nuclear safety review committee (PNSRC).
direction.
The conclusions of the original safety review remained unchanged.
In another section of the package, values for reaction force and moment were omitted from a summary format.These discrepancies
A walkdown and review of the valves installed under 12-MM-337, for the EDG starting air system, was performed on May 13,
consisted of numbers correctly derived in the body of the calculation
: 1997, and documented with the related condition report.
on one page, but omitted from the summary on the following page.This problem was administrative
This review confirmed the original conclusions of the seismic qualification review performed in 1992.
in nature;no incorrect information
The review was formally documented on May 15, 1997.
was presented or used as a result.A third discrepancy
Corrective Actions Taken to Avoid Further Violations We understand the importance of "attention to detail", and to having a design basis that is clear, understandable, and retrievable.
related to this design change package was noted in the body of the inspection
Each of the three cited examples in the NRC inspection report refer to a lack of "attention to detail",
report, but not specified in the notice of violation.
or a lack of clear communication of design information.
The inspector made an observation
The three examples of design control problems highlighted in this violation will be considered again as a part of the larger set of issues identified by the NRC AE team inspection of Cook Nuclear Plant.
that incorrect design information
Resolution of the overall design control issue will require action beyond that which is committed 'in this response.
was stated in the safety review documentation.
Those actions will be defined in the course of addressing the AE team inspection issues.
Our investigation
The violation examples a.
concluded there was no discrepancy
and c. have been characterized as insufficient attention to detail.
in the safety review input information.
When the errors were identified by the inspector, discussions were held with the engineers in the design engineering organization who are involved in the development and
The values of design temperature
 
and pressure used by the safety reviewer were correct for the specific location where the new vent valve was to be installed.
0
The engineer performing
 
the design calculation
Attachment tq AEP:NRC:1260H Page 6
conservatively
documentation of the calculations.
used the highest bounding design temperature
They were made aware of the inspection findings and the importance of attention to detail.
and pressure for the SIS as a whole.This approach is often adopted when the inherent safety margin of a design is such that the more stringent design requirements
This was accomplished while the OSTI was still in progress.
can be accommodated.
Training will be provided for personnel in the nuclear engineering organization who perform,
The thought process involved in taking this approach was not clearly documented
: review, and approve engineering and design calculations.
in the calculation
The session will emphasize the importance of "attention to detail" and good calculation control processes.
package.Design change 12-DCP-0817
This training will be completed by December 31, 1997.
was developed to add a time delay relay to the auxiliary feedwater (AFW)flow retention actuation circuit to prevent spurious actuation from momentary outlet pressure spikes, especially
In 1990, as a result of design verification concerns raised during the safety system functional inspection of our essential service water system, quality review teams (QRTs) were established to periodically review design output documentation for technical adequacy and procedural compliance.
those that occur when the AFW pumps  
These teams were disbanded in 1996.
0  
The discrepancies found under the QRT program had no impact on the conclusions of the calculations.
Attachment
Selected calculations performed during the past
to AEP:NRC:1260H
: year, August 1996, to August 1997, will be reviewed.
Page 4 automatically
The review will look for calculation errors, inconsistencies, proper documentation of assumptions, and procedure adherence.
start.A safety review was performed by the design engineering
Any findings will be addressed and documented under the corrective action program.
organization
This assessment willbe completed by December 1,
for the addition of the time delay pick-up relay to the AFW system circuits.The nuclear safety and analysis section was asked to perform an evaluation
1997.
of the setpoint value for the time delay relay.The review performed by this group was intended to demonstrate
The problem cited in example b. of the violation, incorrect data input to a safety review, has been identified to be a
that the magnitude of the time delay in the flow retention circuits would not adversely impact related accident analysis assumptions
communication problem.
or safety margins.In order to complete this review, the engineer needed to know how quickly the motor driven AFW pumps would start.An'incorrect
On August 26,
value of thirty seconds was used, based on a telephone conversation
: 1997, the nuclear safety and analysis section conducted a tabletop session that discussed the need for precision in the use of technical information in safety reviews.
with the AFW system engineer at the plant site.The system engineer communicated
It stressed that the use of written input is the preferred
that the turbine driven AFW (TDAFW)pumps start and come up to speed within thirty seconds.Surveillance
: method, and that if verbal communication is needed, it must be followed up with a
data on the TDAFW pumps was available on the system engineers desk at the time.What the system engineer intended was that thirty seconds would bound the start time on the motor driven pumps.Most often, in relation to safety analysis or T/S surveillance, the information
written document.
of concern is a time which bounds the pump start, time.However, the safety reviewer understood
These standards for information exchange and use were formally established by procedural direction issued on September 2,
that the thirty seconds would characterize
1997.
the start time for the motor driven auxiliary feedwater (MDAFW)pumps.Based on surveillance
This document provides requirements for nuclear engxneering organization personnel when providing technical direction.
measurements, the correct start time for the motor driven pumps is three seconds.Investigation
The objective of the standard is to provide assurances that the information is accurate, based on sound engineering principles, properly conveyed, and properly documented.
into the reason for this incorrect input to the safety review concluded that it was poor communications
5.
between the involved engineers, and an incomplete
Date When Full Com liance Was Achieved Relative to the individual examples cited in the violation, full compliance was achieved:
understanding
On June 2,
on the part of the system engineer as to the intended use of the information.
: 1997, when calculation DC-D-1-SI-F101 was reviewed and approved for the safety injection system stress analysis.
One engineer believed the bounding start time was needed, while the other was trying to determine the shortest start time for the pumps.Minor modification
On May 29, 1997, when the revised safety review for the AFW flow retention time delay relay setpoint was approved by the PNSRC.
12-MM-337 was performed to replace the emergency diesel generator (EDG)starting air system safety valves.The NRC inspector indicated that the calculation
 
for the seismic adequacy of the new valve type was not performed.
I 1
The design change package referenced
 
calculation
Attachment to AEP:NRC:1260H Page 7
DC-D-12-ES-116.
On May 15,
This referenced
: 1997, when walkdown and review of the seismic qualification of the EDG starting air system safety valves was documented and verified.}}
calculation
was not intended to follow the typical format in what was then the calculation
procedure.
DC-D-12-ES-116
was a record-keeping
and retrieval file for a number of individual
reviews prepared for the replacement
of non-identical
valves.The file did contain the final approval letter from the structural
design section documenting
that the valve change had been reviewed.However, we would have expected to find information
in this file related to  
Attachment
to AEP:NRC:1260H
Page 5 the decision making process, such as isometric data, weight data, and support location information.
For unknown reasons, this file did not contain the information
that would have been expected pertaining
to the review of the valve replacement
of 12-MM-337.
The information
could not be found.It was reconstructed
and the new review was documented
appropriately.
The file now contains the appropriate
information
and review documentation (performed
in May 1997)that confirmed the conclusion
of the original design approval letter.Whether the file was lost, or the review never documented, this condition is characterized
as insufficient
attention to detail.It resulted in the inability to retrieve design data or design basis related information.
3.Corrective
Action Taken and Results Achieved b.c Calculation
DC-D-1-SI-F101, for the safety injection system stress analysis, was revised and approved on June 2, 1997, to address the cited discrepancies.
On May 29, 1997, a revised safety review, incorporating
the correct MDAFW pump start time was approved by the plant nuclear safety review committee (PNSRC).The conclusions
of the original safety review remained unchanged.
A walkdown and review of the valves installed under 12-MM-337, for the EDG starting air system, was performed on May 13, 1997, and documented
with the related condition report.This review confirmed the original conclusions
of the seismic qualification
review performed in 1992.The review was formally documented
on May 15, 1997.Corrective
Actions Taken to Avoid Further Violations
We understand
the importance
of"attention
to detail", and to having a design basis that is clear, understandable, and retrievable.
Each of the three cited examples in the NRC inspection
report refer to a lack of"attention
to detail", or a lack of clear communication
of design information.
The three examples of design control problems highlighted
in this violation will be considered
again as a part of the larger set of issues identified
by the NRC AE team inspection
of Cook Nuclear Plant.Resolution
of the overall design control issue will require action beyond that which is committed'in this response.Those actions will be defined in the course of addressing
the AE team inspection
issues.The violation examples a.and c.have been characterized
as insufficient
attention to detail.When the errors were identified
by the inspector, discussions
were held with the engineers in the design engineering
organization
who are involved in the development
and
0  
Attachment
tq AEP:NRC:1260H
Page 6 documentation
of the calculations.
They were made aware of the inspection
findings and the importance
of attention to detail.This was accomplished
while the OSTI was still in progress.Training will be provided for personnel in the nuclear engineering
organization
who perform, review, and approve engineering
and design calculations.
The session will emphasize the importance
of"attention
to detail" and good calculation
control processes.
This training will be completed by December 31, 1997.In 1990, as a result of design verification
concerns raised during the safety system functional
inspection
of our essential service water system, quality review teams (QRTs)were established
to periodically
review design output documentation
for technical adequacy and procedural
compliance.
These teams were disbanded in 1996.The discrepancies
found under the QRT program had no impact on the conclusions
of the calculations.
Selected calculations
performed during the past year, August 1996, to August 1997, will be reviewed.The review will look for calculation
errors, inconsistencies, proper documentation
of assumptions, and procedure adherence.
Any findings will be addressed and documented
under the corrective
action program.This assessment
will be completed by December 1, 1997.The problem cited in example b.of the violation, incorrect data input to a safety review, has been identified
to be a communication
problem.On August 26, 1997, the nuclear safety and analysis section conducted a tabletop session that discussed the need for precision in the use of technical information
in safety reviews.It stressed that the use of written input is the preferred method, and that if verbal communication
is needed, it must be followed up with a written document.These standards for information
exchange and use were formally established
by procedural
direction issued on September 2, 1997.This document provides requirements
for nuclear engxneering
organization
personnel when providing technical direction.
The objective of the standard is to provide assurances
that the information
is accurate, based on sound engineering
principles, properly conveyed, and properly documented.
5.Date When Full Com liance Was Achieved Relative to the individual
examples cited in the violation, full compliance
was achieved: On June 2, 1997, when calculation
DC-D-1-SI-F101
was reviewed and approved for the safety injection system stress analysis.On May 29, 1997, when the revised safety review for the AFW flow retention time delay relay setpoint was approved by the PNSRC.  
I 1  
Attachment
to AEP:NRC:1260H
Page 7 On May 15, 1997, when walkdown and review of the seismic qualification
of the EDG starting air system safety valves was documented
and verified.
}}

Latest revision as of 13:51, 7 January 2025

Responds to NRC Re Violations Noted in Insp Repts 50-315/97-09 & 50-316/97-09 on 970505-23.Corrective Actions: Calculation DC-D-1-SI-F101 Was Revised & Approved on 970602 to Address Cited Discrepancies
ML17333B038
Person / Time
Site: Cook  
Issue date: 09/15/1997
From: Fitzpatrick E
INDIANA MICHIGAN POWER CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
50-315-97-09, 50-315-97-9, 50-316-97-09, 50-316-97-9, AEP:NRC:1260H, NUDOCS 9709230028
Download: ML17333B038 (19)


Text

CATEGORY l REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

DOCKET 05000315 05000316 NOTES:

CCESSION NBR:9709230028 DOC.DATE: 97/09/15 NOTARIZED: YES FACIL:50-315 Donald C.

Cook Nuclear Power Plant, Unit 1, Indiana M

, 50-316 Donald C.

Cook Nuclear Power Plant, Unit 2, Indiana M

AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.

Indiana Michigan Power Co.

RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Responds to NRC 970815 ltr re violations noted in insp repts 50-315/97-09 a 50-316/97-09 on 970505-23.Corrective actions:

calculation DC-D-1-SI-F101 revised a revised safety review incorporating correct MDAFW pump start time approved.

DISTRIBUTION CODE:

IE01D COPIES RECEIVED:LTR ENCL SIZE-TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response INTERNAL:

RECIPIENT ID CODE/NAME PD3-3 PD AEOD/SPD/RAB DEDRO NRR/DISP/PIPB NRR/DRPM/PECB NUDOCS-ABSTRACT OGC/HDS2 COPIES RECIPIENT LTTR ENCL ID CODE/NAME 1

1 HICKMANiJ 1

AEODf&T~

1

+FILE CEHTE~RQN 1

/DRC@HHFB 1

NRR/DRPM/PERB 1

OE DIR 1

RGN3 FILE 01 COPIES LTTR ENCL 1

1 1

1 1

1 1

1 1

1 1

1 1

1 0

R EXTERNAL LITCO BRYCE g J H

NRC PDR 1

1 NOAC 1

1 NUDOCS FULLTEXT 1

1 1

1 D

0 N

0 NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD)

ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR 18 ENCL 18

0

indiana Michigan Power Company 500 Circle Orive Buchanan, Mi 491071395 INDIANA ItrIICHIGAN PWER September 15, 1997 AEP:NRC:1260H 10'CFR 2.201 Docket Nos.:

50-315 50-316 U. S. Nuclear Regulatory Commission ATTN:

Document Control Desk Washington, D.

C.

20555 Gentlemen:

Donald C.

Cook Nuclear Plant Units 1 and 2

NRC INSPECTION REPORTS NO. 50-315/97009 (DRP)

AND 50-316/97009 (DRP)

REPLY TO NOTICE OF VIOLATION This letter is in response to a letter from G ~

E. Grant, dated August 15, 1997, that forwarded a notice of two violations of NRC requirements to Cook Nuclear Plant.

The violations were identified during the operational safety team inspection (OSTI) conducted by the NRC from May 5, 1997, to May 23, 1997.

The attachment contains our response to these violations.

Commitments were made by Cook Nuclear Plant personnel to the NRC OSTI.

The inspectors identified concerns related to valve descriptions on labels,

drawings, and in procedures, and they had concerns related to our program for sealed valves.

The characterization and detail of these commitments in the inspection report reflects our intent. when the commitments were made.

The second violation relates to the issue of design control.

While reviewing the OSTI report and preparing this response, Cook Nuclear Plant underwent an NRC architect engineering (AE) team inspection.

The AE inspection identified design control issues, some that are similar to those cited in this violation.

Resolution of the overall design control issue will require action beyond that which is committed to here.

Those actions will be defined in the course of addressing the AE team inspection issues.

The nuclear engineering organization, along with our entire nuclear generation

group, understands the importance of error free human performance and attention to detail, and to having a design basis that is clear, understandable, and retrievable.

We believe that a first step was taken on September 2,

1997, when standards for technical information exchange and use in the nuclear engineering 9'709'230028 9709i5 PDR ADQCK 050003%5 8

PDR r.~~0,<iQ

,,s llllllllilllliIIIJlllllllllllliillilf ill

U. S. Nuclear Regulatory Commission Page 2

AEP: NRC: 1260H organization were formally established.

The objective of the guidance is to provide assurances that technical information is

accurate, based on sound engineering principles, properly conveyed, and properly, documented.

Sincerely, E.

E. Fitzpatrick Vice President SWORN TO AND SUBSCRIBED BEFORE-ME THIS I'5 DAY OF ~LV', 1997 Notary Public My Commission Expires vlb Attachments JANWA%0N CAARYPQSC,BBNKNcoWn,e MYCOMMSSOMEXPtRES FEL 10, 1999 c:

A. A. Blind A. B. Beach MDEQ "

DW & RPD NRC Resident Inspector J.

R. Padgett

ATTACHMENT TO AEP:NRC: 1260H REPLY TO NOTICE OF VIOLATION:

NRC INSPECTION REPORT NOS.

50-315/97009 (DRP)

AND 50-316/97009 (DRP)

Attachment to AEP:NRC:1260H Page 1

On May 23,

1997, the NRC completed an operational safety team inspection (OSTI) of Cook Nuclear Plant units 1

and 2 reactor facilities.

Two violations of NRC requirements were identified during this inspection.

In accordance with the 60 FR

34381,

'General Statement of Policy and Procedures for NRC Enforcement Actions", dated June 30, 1995, the violations and our responses are provided below.

NRC Violation I "10 CFR 50, Appendix B, Criterion V, 'Instructions, Procedures, and Drawings, 'equires, in part, that activities affecting quality be prescribed by procedures of a type appropriate to the circumstances and be accomplished in accordance with these procedures.

Contrary to the above, On May 10,

1997, the inspectors identified that safety related Temporary Modification (TM) 1-95-1, which did not require an outage for restoration, had been assigned a

(administrative) date of August 27,

1996, but had not been made a permanent installation through a design change or been removed as of May 10, 1997 as required by Plant Managers Procedure (PMP) 5040.MOD.OO1,

'Temporary Modifications,'evision 7.

B.

On May 7,

1997, the inspectors identified that an activity affecting quality, the deenergization of the DG2AB inverter, was completed without placing 2-DGAB-INV-CB2 and 2-DGAB-INV-CB1 to off, contrary to steps 2.1.2 and 2.1.3 of procedure 02-OHP 4021.032.008

'Aligning DG2AB Subsystems For Standby Operation,'evision 4, Attachment 7.

This is a Severity Level IV violation (Supplement I)."

Res onse to NRC Violation I The letter from Mr. Grant, and the notice of viola'on, state that Cook Nuclear Plant's staff provided the NRC with satisfactory information regarding the reasons for the violation, and the corrective actions taken and planned to correct both examples of the violation and prevent recurrence.

The letter goes on to say

that, unless our corrective actions or our position are not accurately reflected in the inspection report, we are not required to further respond to this violation.

We have reviewed inspection report no.

50-315/316)-97009 and determined that it reflects the circumstances of the examples in the violation as cited, as well as the corrective actions taken for each.

Notwithstanding, for consistency in understanding, there is information in the discussion section of the inspection report that we wish to clarify.

Several condition reports (CRs) are listed as having been reviewed in conjunction with'he 2AB EDG voltage regulator work.

In particular, CR 97-1452 is listed with the title "Partial Clearance Addition Determined As Root Cause for Blown Fuse On 2AB EDG Inverter."

We would like to clarify that the failure to deenergize the EDG inverter using the appropriate procedure is not

0

Attachment to AEP:NRC:1260H Page 2

considered to be the root cause for the inverter fuse blowing during reenergization.

Subsequent investigation has determined that the failure to follow

'the deenergization procedure was recognized before actions were taken to reenergize.

Prior to using the procedure to reenergize the inverter and place it back in service, the inverter circuit alignment was corrected and the integrity of the fuse was verified.

The fuse did blow coincident with performance of the procedure to reenergize the inverter.

NRC Violation ZZ "10 CFR 50, Appendix B, Criterion ZZZ, requires, in part, that mdasures be established to assure that the design basis are correctly translated into specifications, drawings, procedures, and instructions.

Design control measures shall provide for verifying or checking the adequacy of design.

Contrary to the above, design control measures were not adequate to assure that the design basis was correctly translated into design modification documents:

b.

On May 7,

1997, the inspectors identified that calculation DC-D-1-SZ-F101, 'Stress Analysis

& Load Generation for System 1-SI-F101 Per 12-MM-590,'sed the wrong moment arm and had a missing reaction force and moment.

On May 13, 1997, the inspectors identified that incorrect and non-conservative design input was used for the motor-driven auxiliary feedwater pump start time in the Safety Review Memorandum for the Setpoint Values for the Time Delay Pickup Relays in the AFW Flow Retention

Circuits, dated January 15,
1997, for design change package 12-DCP-0817,

'Revise Aux. Feedwater Flow Retention Circuit.',

On May 13, 1997, the inspectors identified that a calculation for the seismic design adequacy of minor modification 12-MM-337 was not per formed.

The design package for 12-MM-337 indicated this calculation existed as DC-D-12-ES-116.

This is a Severity Level IV violation (Sur,v>lement I)."

Res onse to NRC Violation ZZ 1.

Admission or Denial of the Violation We admit to violation ZI as cited in the NRC notice of violation.

Reasons for the Violation

, The examples cited in the violation represent issues in the area of design control.

Concurrent with the review of the OSTI report and preparation of this

response, Cook Nuclear Plant underwent an NRC architect engineering (AE) team inspection.

This inspection identified design control issues, some that are similar to those cited in the violation.

Zt is recognized that the three examples cited in this notice of violation must be

0

Attachment to AEP:NRC: 1260H Page 3

considered along with any new issues identified by the AE team inspection, relative to the overall issue of design control.

The circumstances of each issue cited in this notice of violation are discussed below.

Calculation DC-D-1-SI-F101, "Stress Analysis and Load Generation for System 1-SI-F101 per 12-MM-590",

was performed in support of adding a permanent vent line to the safety injection system (SIS) piping.

The inspector's review of the design change package identified errors made by the authors and overlooked by the calculation reviewers.

The errors are characterized as insufficient attention to detail on the part of the engineers performing and reviewing the design change package.

When calculating reaction forces, the length value of a piping span, used as a moment arm in the calculation, was transcribed from the input data presentation to the actual algebraic presentation incorrectly, from 37-5/8" to 35-5/8".

This discrepancy caused the maximum reaction force result to be incorrect, but in a

conservative direction.

In another section of the package, values for reaction force and moment were omitted from a summary format.

These discrepancies consisted of numbers correctly derived in the body of the calculation on one page, but omitted from the summary on the following page.

This problem was administrative in nature; no incorrect information was presented or used as a result.

A third discrepancy related to this design change package was noted in the body of the inspection report, but not specified in the notice of violation.

The inspector made an observation that incorrect design information was stated in the safety review documentation.

Our investigation concluded there was no discrepancy in the safety review input information.

The values of design temperature and pressure used by the safety reviewer were correct for the specific location where the new vent valve was to be installed.

The engineer performing the design calculation conservatively used the highest bounding design temperature and pressure for the SIS as a whole.

This approach is often adopted when the inherent safety margin of a design is such that the more stringent design requirements can be accommodated.

The thought process involved in taking this approach was not clearly documented in the calculation package.

Design change 12-DCP-0817 was developed to add a time delay relay to the auxiliary feedwater (AFW) flow retention actuation circuit to prevent spurious actuation from momentary outlet pressure

spikes, especially those that occur when the AFW pumps

0

Attachment to AEP:NRC:1260H Page 4

automatically start.

A safety review was performed by the design engineering organization for the addition of the time delay pick-up relay to the AFW system circuits.

The nuclear safety and analysis section was asked to perform an evaluation of the setpoint value for the time delay relay.

The review performed by this group was intended to demonstrate that the magnitude of the time delay in the flow retention circuits would not adversely impact related accident analysis assumptions or safety margins.

In order to complete this review, the engineer needed to know how quickly the motor driven AFW pumps would start.

An 'incorrect value of thirty seconds was used, based on a telephone conversation with the AFW system engineer at the plant site.

The system engineer communicated that the turbine driven AFW (TDAFW) pumps start and come up to speed within thirty seconds.

Surveillance data on the TDAFW pumps was available on the system engineers desk at the time.

What the system engineer intended was that thirty seconds would bound the start time on the motor driven pumps.

Most often, in relation to safety analysis or T/S surveillance, the information of concern is a time which bounds the pump start, time.

However, the safety reviewer understood that the thirty seconds would characterize the start time for the motor driven auxiliary feedwater (MDAFW) pumps.

Based on surveillance measurements, the correct start time for the motor driven pumps is three seconds.

Investigation into the reason for this incorrect input to the safety review concluded that it was poor communications between the involved engineers, and an incomplete understanding on the part of the system engineer as to the intended use of the information.

One engineer believed the bounding start time was needed, while the other was trying to determine the shortest start time for the pumps.

Minor modification 12-MM-337 was performed to replace the emergency diesel generator (EDG) starting air system safety valves.

The NRC inspector indicated that the calculation for the seismic adequacy of the new valve type was not performed.

The design change package referenced calculation DC-D-12-ES-116.

This referenced calculation was not intended to follow the typical format in what was then the calculation procedure.

DC-D-12-ES-116 was a record-keeping and retrieval file for a

number of individual reviews prepared for the replacement of non-identical valves.

The file did contain the final approval letter from the structural design section documenting that the valve change had been reviewed.

However, we would have expected to find information in this file related to

Attachment to AEP:NRC:1260H Page 5

the decision making process, such as isometric data, weight data, and support location information.

For unknown

reasons, this file did not contain the information that would have been expected pertaining to the review of the valve replacement of 12-MM-337.

The information could not be found. It was reconstructed and the new review was documented appropriately.

The file now contains the appropriate information and review documentation (performed in May 1997) that confirmed the conclusion of the original design approval letter.

Whether the file was

lost, or the review never documented, this condition is characterized as insufficient attention to detail.

It resulted in the inability to retrieve design data or design basis related information.

3.

Corrective Action Taken and Results Achieved b.

c Calculation DC-D-1-SI-F101, for the safety injection system stress

analysis, was revised and approved on June 2,

1997, to address the cited discrepancies.

On May 29, 1997, a revised safety review, incorporating the correct MDAFW pump start time was approved by the plant nuclear safety review committee (PNSRC).

The conclusions of the original safety review remained unchanged.

A walkdown and review of the valves installed under 12-MM-337, for the EDG starting air system, was performed on May 13,

1997, and documented with the related condition report.

This review confirmed the original conclusions of the seismic qualification review performed in 1992.

The review was formally documented on May 15, 1997.

Corrective Actions Taken to Avoid Further Violations We understand the importance of "attention to detail", and to having a design basis that is clear, understandable, and retrievable.

Each of the three cited examples in the NRC inspection report refer to a lack of "attention to detail",

or a lack of clear communication of design information.

The three examples of design control problems highlighted in this violation will be considered again as a part of the larger set of issues identified by the NRC AE team inspection of Cook Nuclear Plant.

Resolution of the overall design control issue will require action beyond that which is committed 'in this response.

Those actions will be defined in the course of addressing the AE team inspection issues.

The violation examples a.

and c. have been characterized as insufficient attention to detail.

When the errors were identified by the inspector, discussions were held with the engineers in the design engineering organization who are involved in the development and

0

Attachment tq AEP:NRC:1260H Page 6

documentation of the calculations.

They were made aware of the inspection findings and the importance of attention to detail.

This was accomplished while the OSTI was still in progress.

Training will be provided for personnel in the nuclear engineering organization who perform,

review, and approve engineering and design calculations.

The session will emphasize the importance of "attention to detail" and good calculation control processes.

This training will be completed by December 31, 1997.

In 1990, as a result of design verification concerns raised during the safety system functional inspection of our essential service water system, quality review teams (QRTs) were established to periodically review design output documentation for technical adequacy and procedural compliance.

These teams were disbanded in 1996.

The discrepancies found under the QRT program had no impact on the conclusions of the calculations.

Selected calculations performed during the past

year, August 1996, to August 1997, will be reviewed.

The review will look for calculation errors, inconsistencies, proper documentation of assumptions, and procedure adherence.

Any findings will be addressed and documented under the corrective action program.

This assessment willbe completed by December 1,

1997.

The problem cited in example b. of the violation, incorrect data input to a safety review, has been identified to be a

communication problem.

On August 26,

1997, the nuclear safety and analysis section conducted a tabletop session that discussed the need for precision in the use of technical information in safety reviews.

It stressed that the use of written input is the preferred

method, and that if verbal communication is needed, it must be followed up with a

written document.

These standards for information exchange and use were formally established by procedural direction issued on September 2,

1997.

This document provides requirements for nuclear engxneering organization personnel when providing technical direction.

The objective of the standard is to provide assurances that the information is accurate, based on sound engineering principles, properly conveyed, and properly documented.

5.

Date When Full Com liance Was Achieved Relative to the individual examples cited in the violation, full compliance was achieved:

On June 2,

1997, when calculation DC-D-1-SI-F101 was reviewed and approved for the safety injection system stress analysis.

On May 29, 1997, when the revised safety review for the AFW flow retention time delay relay setpoint was approved by the PNSRC.

I 1

Attachment to AEP:NRC:1260H Page 7

On May 15,

1997, when walkdown and review of the seismic qualification of the EDG starting air system safety valves was documented and verified.