ML18153C338: Difference between revisions

From kanterella
Jump to navigation Jump to search
Created page by program invented by StriderTol
StriderTol Bot change
 
(3 intermediate revisions by the same user not shown)
Line 2: Line 2:
| number = ML18153C338
| number = ML18153C338
| issue date = 08/22/1990
| issue date = 08/22/1990
| title = Responds to NRC 900723 Ltr Re Violations Noted in Insp Rept 50-280/90-21 & 50-281/90-21.Corrective actions:as-found-as- Left Conditions of Auxiliary Feedwater Evaluated & Found Operable
| title = Responds to NRC Re Violations Noted in Insp Rept 50-280/90-21 & 50-281/90-21.Corrective actions:as-found-as- Left Conditions of Auxiliary Feedwater Evaluated & Found Operable
| author name = Stewart W
| author name = Stewart W
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
Line 11: Line 11:
| contact person =  
| contact person =  
| document report number = 90-467, NUDOCS 9008300155
| document report number = 90-467, NUDOCS 9008300155
| title reference date = 07-23-1990
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| page count = 3
| page count = 3
}}
}}
See also: [[see also::IR 05000280/1990021]]


=Text=
=Text=
{{#Wiki_filter:' i _/ VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 August 22, 1990 United States Nuclear Regulatory  
{{#Wiki_filter:'  
Commission  
~ i
Attention:  
_/
Document Control Desk Washington, D.C. 20555 Gentlemen:  
VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 August 22, 1990 United States Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 REPLY TO A NOTICE OF VIOLATION  
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 REPLY TO A NOTICE OF VIOLATION NRC INSPECTION REPORT NO. 50-280/90-21 Serial No.
NRC INSPECTION  
90-467 SPS/JWH/pmk Docket No.:
REPORT NO. 50-280/90-21  
50-280 License No.:
Serial No. 90-467 SPS/JWH/pmk  
DPR -32 We have reviewed your {{letter dated|date=July 23, 1990|text=letter dated July 23, 1990}}, in reference to the NRC inspection conducted from June 3, 1990 - June 30, 1990, for Surry Power Station. The inspection was reported in Inspection Report Nos. 50-280/90-21 and 50-281 /90-21.
Docket No.: 50-280 License No.: DPR -32 We have reviewed your letter dated July 23, 1990, in reference  
Our response to the violation described in the Notice of Violation is provided in the attachment.
to the NRC inspection  
We have no objection to this response being made a matter of public disclosure.
conducted  
If you have any further questions, please contact us.
from June 3, 1990 -June 30, 1990, for Surry Power Station. The inspection  
W. L. St art Senior Vice President - Nuclear Attachment cc:
was reported in Inspection  
U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N.W.
Report Nos. 50-280/90-21  
Suite 2900 Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station 9006300155 9~~80 PDR ADOCK O PNU Q  
and 50-281 /90-21. Our response to the violation  
 
described  
'"'i
in the Notice of Violation  
_)
is provided in the attachment.  
ATIACHMENT REPLY TO NOTICE OF VIOLATION NRC INSPECTION CONDUCTED JUNE 3, 1990 - JUNE 30, 1990 INSPECTION REPORT NO. 50-280/90-21 NRC COMMENT:  
* * We have no objection  
"Technical Specification 6.4 requires, in part, that procedures for the testing of components and systems involving nuclear safety of the station shall be followed.
to this response being made a matter of public disclosure.  
Contrary to the above, a procedure for testing of components was not followed, in that, on June 2, 1990, during performance of periodic testing,on the Unit 1 turbine driven auxiliary feedwater pump, operators made adjustments to the turbine speed which were not in accordance with procedure, 1-PT-15.1 C, Turbine Driven Auxiliary Feedwater Pump (1-FW-P-2), dated July 25, 1989. This violation is similar to a violation which was cited in a report dated September 28, 1989.
* If you have any further questions, please contact us. W. L. St art Senior Vice President  
This is a Severity Level IV violation (Supplement I) and applies to Unit 1 only."  
-Nuclear Attachment  
 
cc: U. S. Nuclear Regulatory  
REPLY TO NOTICE OF VIOLATION INSPECTION REPORT NO. 50-280/90-21 (1)
Commission  
ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:
Region II 101 Marietta Street, N.W. Suite 2900 Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector  
The violation is correct as stated, with the exception that the procedure in use, 1-PT-15.1C, was dated May 10, 1990.
Surry Power Station 9006300155  
(2)
9~~80 PDR ADOCK O PNU Q
REASON FOR THE VIOLATION:
'"'i _) * ATIACHMENT  
The violation was caused by a failure to follow procedures on the part of the Assistant Shift Supervisor in charge of the test. The Assistant Shift Supervisor adjusted the speed of the auxiliary feedwater (AFW) pump turbine from its as-found value of 4145 RPM to 4200 RPM. This is contrary to Procedure 1-PT-15.1 C. The procedure does not require turbine adjustment unless the as-found pump shaft speed exceeds 4250 RPM. Another operator present for the test questioned if this adjustment was consistent with the procedure, but did not object to the action taken by the Assistant Shift Supervisor to adjust the speed.
REPLY TO NOTICE OF VIOLATION  
The Assistant Shift Supervisor resigned from Virginia Power Company on June 4, 1990, and was not available for detailed discussions as to the reason for his actions.
NRC INSPECTION  
(3)
CONDUCTED  
CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:
JUNE 3, 1990 -JUNE 30, 1990 INSPECTION  
The as found and as left conditions of the AFW pump were evaluated by Engineering, and the pump was determined to be operable. This determination was based on previous test results which showed that, when the pump is operated at 4200 RPM, the pump head falls within the acceptable range and the turbine does not trip on overspeed when started.
REPORT NO. 50-280/90-21  
The Station Manager issued a memorandum to station supervision stressing the need for strict adherence to procedures and the need for the proper understanding of the procedural steps prior to implementation.
NRC COMMENT: "Technical  
(4)
Specification  
CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:
6.4 requires, in part, that procedures  
Although similar to a September, 1989 event, this violation is considered to be an isolated event without programmatic implications. Therefore, no additional corrective action beyond those taken for the September, 1989 event are deemed necessary.
for the testing of components  
(5)
and systems involving  
THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:
nuclear safety of the station shall be followed.  
Full compliance was achieved on June 12, 1990 when the turbine-driven AFW pump was confirmed to be operable despite the turbine speed adjustment.}}
Contrary to the above, a procedure  
for testing of components  
was not followed, in that, on June 2, 1990, during performance  
of periodic testing ,on the Unit 1 turbine driven auxiliary  
feedwater  
pump, operators  
made adjustments  
to the turbine speed which were not in accordance  
with procedure, 1-PT-15.1  
C, Turbine Driven Auxiliary  
Feedwater  
Pump (1-FW-P-2), dated July 25, 1989. This violation  
is similar to a violation  
which was cited in a report dated September  
28, 1989. This is a Severity Level IV violation (Supplement  
I) and applies to Unit 1 only."
REPLY TO NOTICE OF VIOLATION  
INSPECTION  
REPORT NO. 50-280/90-21  
(1) ADMISSION  
OR DENIAL OF THE ALLEGED VIOLATION:  
The violation  
is correct as stated, with the exception  
that the procedure  
in use, 1-PT-15.1C, was dated May 10, 1990. (2) REASON FOR THE VIOLATION:  
The violation  
was caused by a failure to follow procedures  
on the part of the Assistant  
Shift Supervisor  
in charge of the test. The Assistant  
Shift Supervisor  
adjusted the speed of the auxiliary  
feedwater (AFW) pump turbine from its found value of 4145 RPM to 4200 RPM. This is contrary to Procedure  
1-PT-15.1 C. The procedure  
does not require turbine adjustment  
unless the as-found pump shaft speed exceeds 4250 RPM. Another operator present for the test questioned  
if this adjustment  
was consistent  
with the procedure, but did not object to the action taken by the Assistant  
Shift Supervisor  
to adjust the speed. The Assistant  
Shift Supervisor  
resigned from Virginia Power Company on June 4, 1990, and was not available  
for detailed discussions  
as to the reason for his actions. (3) CORRECTIVE  
STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:  
The as found and as left conditions  
of the AFW pump were evaluated  
by Engineering, and the pump was determined  
to be operable.  
This determination  
was based on previous test results which showed that, when the pump is operated at 4200 RPM, the pump head falls within the acceptable  
range and the turbine does not trip on overspeed  
when started. The Station Manager issued a memorandum  
to station supervision  
stressing  
the need for strict adherence  
to procedures  
and the need for the proper understanding  
of the procedural  
steps prior to implementation.  
(4) CORRECTIVE  
STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:  
Although similar to a September, 1989 event, this violation  
is considered  
to be an isolated event without programmatic  
implications.  
Therefore, no additional  
corrective  
action beyond those taken for the September, 1989 event are deemed necessary.  
(5) THE DATE WHEN FULL COMPLIANCE  
WILL BE ACHIEVED:  
Full compliance  
was achieved on June 12, 1990 when the turbine-driven  
AFW pump was confirmed  
to be operable despite the turbine speed adjustment.
}}

Latest revision as of 18:56, 5 January 2025

Responds to NRC Re Violations Noted in Insp Rept 50-280/90-21 & 50-281/90-21.Corrective actions:as-found-as- Left Conditions of Auxiliary Feedwater Evaluated & Found Operable
ML18153C338
Person / Time
Site: Surry  
Issue date: 08/22/1990
From: Stewart W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
90-467, NUDOCS 9008300155
Download: ML18153C338 (3)


Text

'

~ i

_/

VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 August 22, 1990 United States Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 Gentlemen:

VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 REPLY TO A NOTICE OF VIOLATION NRC INSPECTION REPORT NO. 50-280/90-21 Serial No.90-467 SPS/JWH/pmk Docket No.:

50-280 License No.:

DPR -32 We have reviewed your letter dated July 23, 1990, in reference to the NRC inspection conducted from June 3, 1990 - June 30, 1990, for Surry Power Station. The inspection was reported in Inspection Report Nos. 50-280/90-21 and 50-281 /90-21.

Our response to the violation described in the Notice of Violation is provided in the attachment.

We have no objection to this response being made a matter of public disclosure.

If you have any further questions, please contact us.

W. L. St art Senior Vice President - Nuclear Attachment cc:

U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N.W.

Suite 2900 Atlanta, Georgia 30323 Mr. W. E. Holland NRC Senior Resident Inspector Surry Power Station 9006300155 9~~80 PDR ADOCK O PNU Q

'"'i

_)

ATIACHMENT REPLY TO NOTICE OF VIOLATION NRC INSPECTION CONDUCTED JUNE 3, 1990 - JUNE 30, 1990 INSPECTION REPORT NO. 50-280/90-21 NRC COMMENT:

"Technical Specification 6.4 requires, in part, that procedures for the testing of components and systems involving nuclear safety of the station shall be followed.

Contrary to the above, a procedure for testing of components was not followed, in that, on June 2, 1990, during performance of periodic testing,on the Unit 1 turbine driven auxiliary feedwater pump, operators made adjustments to the turbine speed which were not in accordance with procedure, 1-PT-15.1 C, Turbine Driven Auxiliary Feedwater Pump (1-FW-P-2), dated July 25, 1989. This violation is similar to a violation which was cited in a report dated September 28, 1989.

This is a Severity Level IV violation (Supplement I) and applies to Unit 1 only."

REPLY TO NOTICE OF VIOLATION INSPECTION REPORT NO. 50-280/90-21 (1)

ADMISSION OR DENIAL OF THE ALLEGED VIOLATION:

The violation is correct as stated, with the exception that the procedure in use, 1-PT-15.1C, was dated May 10, 1990.

(2)

REASON FOR THE VIOLATION:

The violation was caused by a failure to follow procedures on the part of the Assistant Shift Supervisor in charge of the test. The Assistant Shift Supervisor adjusted the speed of the auxiliary feedwater (AFW) pump turbine from its as-found value of 4145 RPM to 4200 RPM. This is contrary to Procedure 1-PT-15.1 C. The procedure does not require turbine adjustment unless the as-found pump shaft speed exceeds 4250 RPM. Another operator present for the test questioned if this adjustment was consistent with the procedure, but did not object to the action taken by the Assistant Shift Supervisor to adjust the speed.

The Assistant Shift Supervisor resigned from Virginia Power Company on June 4, 1990, and was not available for detailed discussions as to the reason for his actions.

(3)

CORRECTIVE STEPS WHICH HAVE BEEN TAKEN AND THE RESULTS ACHIEVED:

The as found and as left conditions of the AFW pump were evaluated by Engineering, and the pump was determined to be operable. This determination was based on previous test results which showed that, when the pump is operated at 4200 RPM, the pump head falls within the acceptable range and the turbine does not trip on overspeed when started.

The Station Manager issued a memorandum to station supervision stressing the need for strict adherence to procedures and the need for the proper understanding of the procedural steps prior to implementation.

(4)

CORRECTIVE STEPS WHICH WILL BE TAKEN TO AVOID FURTHER VIOLATIONS:

Although similar to a September, 1989 event, this violation is considered to be an isolated event without programmatic implications. Therefore, no additional corrective action beyond those taken for the September, 1989 event are deemed necessary.

(5)

THE DATE WHEN FULL COMPLIANCE WILL BE ACHIEVED:

Full compliance was achieved on June 12, 1990 when the turbine-driven AFW pump was confirmed to be operable despite the turbine speed adjustment.