ML20005E173: Difference between revisions

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j c; ...     'SSM M M'On     %.r se Shwngen PA160774004
'SSM M M'On %.r se Shwngen PA160774004
  '3 J N N D SICBER
'3 J N N D SICBER
                      * **"' * '**                                                                          ~
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December 21, 1989 U. S'. Nuclear Regulatory Commission Attn:           Document Control Desk' Washington,-DC- '20555
December 21, 1989 U.
S'.
Nuclear Regulatory Commission Attn:
Document Control Desk' Washington,-DC- '20555


==Reference:==
==Reference:==
Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 NRC Bulletin 88-11 Gentlemen:
Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 NRC Bulletin 88-11 Gentlemen:
In accordance with Item 1.a of Bulletin 88-11, " Pressurizer Surge Line. Thermal-Stratification", we performed a visual inspection (ASME, Section XI, VT-3) of the Beaver Valley Unit 1 (BV-1) pressurizer surge line during the seventh refueling
In accordance with Item 1.a of Bulletin 88-11, " Pressurizer Surge Line. Thermal-Stratification", we performed a visual inspection (ASME, Section XI, VT-3) of the Beaver Valley Unit 1 (BV-1) pressurizer surge line during the seventh refueling
                  . outage.           No discernible distress or damage was identified for the pressurizer surge line piping, supports, pipe whip restraints, and anchor bolts.
. outage.
No discernible distress or damage was identified for the pressurizer surge line piping, supports, pipe whip restraints, and anchor bolts.
However, during the inspection of this line, the rupture restraint gaps were found to be open greater than the original
However, during the inspection of this line, the rupture restraint gaps were found to be open greater than the original
                  -design ~ analysis and-the rupture restraints baseplate to embedments were welded together and the shear bars / lugs were not' installed.
-design ~ analysis and-the rupture restraints baseplate to embedments were welded together and the shear bars / lugs were not' installed.
These deficiencies were reported in Licensee Event Report (LER) 89-011-00.             Both of the deficiencies were corrected during the seventh refueling outage.
These deficiencies were reported in Licensee Event Report (LER) 89-011-00.
Both of the deficiencies were corrected during the seventh refueling outage.
We are continuing our efforts to complete the BV-1 plant
We are continuing our efforts to complete the BV-1 plant
: specific analyses for Item 1.d of the Bulletin by January, 1991.
: specific analyses for Item 1.d of the Bulletin by January, 1991.
If you have any questions concerning this response, please contact my office.
If you have any questions concerning this response, please contact my office.
Very truly yours,
Very truly yours,
                                                                                      -)
-)
                                                                                  . D. Sieber ice President Nuclear Group cc:         Mr. J. Beall, Sr. Resident Inspector Mr. W. T. Russell, NRC Region I Administrator Mr. P. Ta .n , Sr. Project Manager Mr. R. Saunders (VEPCO) 30 9001040020 891221 PDR                                                                   i0 0     ADOCK 05000334 PDC
D.
Sieber ice President Nuclear Group cc:
Mr. J.
Beall, Sr. Resident Inspector Mr. W.
T. Russell, NRC Region I Administrator Mr. P. Ta.n, Sr. Project Manager Mr. R.
Saunders (VEPCO) 30 9001040020 891221 PDR ADOCK 05000334 i0 0
PDC


j   .1             ,-
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COMMONWEALTH OF PENNSYLVANIA)
.1 COMMONWEALTH OF PENNSYLVANIA)
                                                  )   SS:
)
COUNTY OF-BEAVER                 )
SS:
on   this             o           day of / d// O               D         , 1989, before   me,   M/d     . /d/W
COUNTY OF-BEAVER
                                                ~
)
                                                            ,  a Notary Public in and           for said l             ./
on this o
Commonwealth     and County, personally appeared J. D. Sieber, who being duly   sworn,   deposed, and     said   that (1)   he   is Vice President of Duquesne   Light,   (2) he   is   duly authorized to execute and file the foregoing- Submittal on behalf of said Company, and (3) the statements set   forth   in the   Submittal are true and correct to the best of his
day of / d// O D
                  . knowledge, information and belief.
: 1989, before me, M/d
J   a               a f 0     NotarWSeal Tracey A.Bxzek.Nowy %
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My bonExdre           .kO3 Mstn,Pennsylv:na h d %%}}
Notary Public in and for said l
~
./
Commonwealth and County, personally appeared J. D. Sieber, who being duly
: sworn, deposed, and said that (1) he is Vice President of Duquesne
: Light, (2) he is duly authorized to execute and file the foregoing-Submittal on behalf of said Company, and (3) the statements set forth in the Submittal are true and correct to the best of his
. knowledge, information and belief.
J a
a f
0 NotarWSeal Tracey A.Bxzek.Nowy %
My bonExdre
.kO3 Mstn,Pennsylv:na h d %%}}

Latest revision as of 08:45, 23 December 2024

Responds to NRC Bulletin 88-011, Pressurizer Surge Line Thermal Stratification. No Discernible Distress or Damage Identified for Pressurizer Surge Line Piping,Supports or Pipe Whip Restraints During Visual Insp of Facility
ML20005E173
Person / Time
Site: Beaver Valley
Issue date: 12/21/1989
From: Sieber J
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
IEB-88-011, IEB-88-11, NUDOCS 9001040020
Download: ML20005E173 (2)


Text

.

1 9 -;

i fg '

i t j c;...

'SSM M M'On %.r se Shwngen PA160774004

'3 J N N D SICBER

~

December 21, 1989 U.

S'.

Nuclear Regulatory Commission Attn:

Document Control Desk' Washington,-DC- '20555

Reference:

Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 NRC Bulletin 88-11 Gentlemen:

In accordance with Item 1.a of Bulletin 88-11, " Pressurizer Surge Line. Thermal-Stratification", we performed a visual inspection (ASME,Section XI, VT-3) of the Beaver Valley Unit 1 (BV-1) pressurizer surge line during the seventh refueling

. outage.

No discernible distress or damage was identified for the pressurizer surge line piping, supports, pipe whip restraints, and anchor bolts.

However, during the inspection of this line, the rupture restraint gaps were found to be open greater than the original

-design ~ analysis and-the rupture restraints baseplate to embedments were welded together and the shear bars / lugs were not' installed.

These deficiencies were reported in Licensee Event Report (LER) 89-011-00.

Both of the deficiencies were corrected during the seventh refueling outage.

We are continuing our efforts to complete the BV-1 plant

specific analyses for Item 1.d of the Bulletin by January, 1991.

If you have any questions concerning this response, please contact my office.

Very truly yours,

-)

D.

Sieber ice President Nuclear Group cc:

Mr. J.

Beall, Sr. Resident Inspector Mr. W.

T. Russell, NRC Region I Administrator Mr. P. Ta.n, Sr. Project Manager Mr. R.

Saunders (VEPCO) 30 9001040020 891221 PDR ADOCK 05000334 i0 0

PDC

j

.1 COMMONWEALTH OF PENNSYLVANIA)

)

SS:

COUNTY OF-BEAVER

)

on this o

day of / d// O D

1989, before me, M/d

. /d/W a

Notary Public in and for said l

~

./

Commonwealth and County, personally appeared J. D. Sieber, who being duly

sworn, deposed, and said that (1) he is Vice President of Duquesne
Light, (2) he is duly authorized to execute and file the foregoing-Submittal on behalf of said Company, and (3) the statements set forth in the Submittal are true and correct to the best of his

. knowledge, information and belief.

J a

a f

0 NotarWSeal Tracey A.Bxzek.Nowy %

My bonExdre

.kO3 Mstn,Pennsylv:na h d %%