ML20070W099: Difference between revisions

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k ,,g4[_M MIL' f                                                                                     CINCINNATl, OHIO 452o1 THE CINCINNATI GAS & ELECTRIC WM. H. ZIMMER NUCLEAR POWER STATION, UNIT 1 COMPANYFebruary 8, 1983 45153                             QA-2252 P.O. BOX 201, MOSCOW, OH E A.BoRGM ANN
MIL' f
    *1ENIOR VICC PRC5f DENT U.S. Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Mr. J. G. Keppler Attention: Regional Administrator RE:    WM.                     H. Z1hMER NUCLEAR POWER STATION UNIT 1 10CFR50.55(e) ITEM M-72, LACK OF QA PROGRAM FOR FP SYSTEM INSTALLATION - DOCKET No. 50-358, CONSTRUCTION PERMIT NO. CPPR-88, W.O. 57300, FILE NO. NRC-8 Gentlemen:                                                                  h     ubject condition, This letter constitutes an interim report concerning t e stable deficiency under initially reported to the Commission as a potentially repor 10CFR50.55(e).                                                                 i i lly anticipated, A document and commitment review, more extensive than or g nad commitments is in progress to identify the requirements and related the manner in which these were nical Position (BTP) APCSB 9.5-1, Appendix A, anIt is not possible to draw any definite conc implemented and documented.
THE CINCINNATI GAS & ELECTRIC COMPANY CINCINNATl, OHIO 452o1 February 8, 1983 WM. H. ZIMMER NUCLEAR POWER STATION, UNIT 1 45153 QA-2252 P.O. BOX 201, MOSCOW, OH E A.BoRGM ANN
from the review performed to date.                                                 that the design and i A, We anticipate that the results of this review will indicate thei requirements of BTP APCSB 9.5-1, Appen procurement controls implemented metand that documentation required fo lation and testing can be assembled.at which time a report will be submitted.
*1ENIOR VICC PRC5f DENT U.S. Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Mr. J. G. Keppler Attention:
April 30, 1983                                                                i      port under 10CFR50.55(e).
Regional Administrator WM. H. Z1hMER NUCLEAR POWER STATION UNIT 1 10CFR50.55(e) ITEM M-72, LACK OF QA PROGRAM RE:
We trust the above will be found acceptable as an inter m re Very truly yours, THE CINCINNATI GAS & ELECTRIC COMPANY By
FOR FP SYSTEM INSTALLATION - DOCKET No. 50-358, CONSTRUCTION PERMIT NO. CPPR-88, W.O. 57300, FILE NO. NRC-8 h
                                                                          ~
ubject condition, Gentlemen:
This letter constitutes an interim report concerning t e stable deficiency under initially reported to the Commission as a potentially repor 10CFR50.55(e).
i i lly anticipated, A document and commitment review, more extensive than or g nad commitments is in progress to identify the requirements and related the manner in which these were nical Position (BTP) APCSB 9.5-1, Appendix A, anIt is not possible to draw any definite conc implemented and documented.
from the review performed to date.
that the design and We anticipate that the results of this review will indicate i
A, the requirements of BTP APCSB 9.5-1, Appe procurement controls implemented metand that documentation required fo i
lation and testing can be assembled.at which time a report will be submitted.
port under 10CFR50.55(e).
April 30, 1983 i
We trust the above will be found acceptable as an inter m re Very truly yours, THE CINCINNATI GAS & ELECTRIC COMPANY
~
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E. A. BORGMANN 9302180270 830208                                                      SENIOR VICE PRESIDENT PDR ADOCK 05000359                      PDR S
By 9302180270 830208 E. A. BORGMANN PDR ADOCK 05000359 SENIOR VICE PRESIDENT PDR S
FJS:jas cc:    NRC Office of Inspection and Enforcement Washington, D.C. 20555 NRC Senior Resident Inspector                                                               )Cg07 Attn: W. F. Christianson Zimmer Project Inspector                                                                 FEB 16 1983 Region III
FJS:jas NRC Office of Inspection and Enforcement cc:
                            - - _ - - _ - _ _ __}}
Washington, D.C. 20555 g07 NRC Senior Resident Inspector
)C W. F. Christianson Attn:
Zimmer Project Inspector FEB 16 1983 Region III
- - _ - - _ - _ _ __}}

Latest revision as of 08:55, 16 December 2024

Interim Deficiency Rept Re Lack of QA Program for Fire Protection Sys Installation.Document & Commitment Review Underway.Results Should Indicate That Branch Technical Position Apcsb 9.5-1,App A,Met.Next Rept Due by 830430
ML20070W099
Person / Time
Site: Zimmer
Issue date: 02/08/1983
From: Borgmann E
CINCINNATI GAS & ELECTRIC CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
10CFR-050.55E, 10CFR-50.55E, QA-2252, NUDOCS 8302180270
Download: ML20070W099 (1)


Text

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MIL' f

THE CINCINNATI GAS & ELECTRIC COMPANY CINCINNATl, OHIO 452o1 February 8, 1983 WM. H. ZIMMER NUCLEAR POWER STATION, UNIT 1 45153 QA-2252 P.O. BOX 201, MOSCOW, OH E A.BoRGM ANN

  • 1ENIOR VICC PRC5f DENT U.S. Nuclear Regulatory Commission Region III 799 Roosevelt Road Glen Ellyn, IL 60137 Mr. J. G. Keppler Attention:

Regional Administrator WM. H. Z1hMER NUCLEAR POWER STATION UNIT 1 10CFR50.55(e) ITEM M-72, LACK OF QA PROGRAM RE:

FOR FP SYSTEM INSTALLATION - DOCKET No. 50-358, CONSTRUCTION PERMIT NO. CPPR-88, W.O. 57300, FILE NO. NRC-8 h

ubject condition, Gentlemen:

This letter constitutes an interim report concerning t e stable deficiency under initially reported to the Commission as a potentially repor 10CFR50.55(e).

i i lly anticipated, A document and commitment review, more extensive than or g nad commitments is in progress to identify the requirements and related the manner in which these were nical Position (BTP) APCSB 9.5-1, Appendix A, anIt is not possible to draw any definite conc implemented and documented.

from the review performed to date.

that the design and We anticipate that the results of this review will indicate i

A, the requirements of BTP APCSB 9.5-1, Appe procurement controls implemented metand that documentation required fo i

lation and testing can be assembled.at which time a report will be submitted.

port under 10CFR50.55(e).

April 30, 1983 i

We trust the above will be found acceptable as an inter m re Very truly yours, THE CINCINNATI GAS & ELECTRIC COMPANY

~

[

By 9302180270 830208 E. A. BORGMANN PDR ADOCK 05000359 SENIOR VICE PRESIDENT PDR S

FJS:jas NRC Office of Inspection and Enforcement cc:

Washington, D.C. 20555 g07 NRC Senior Resident Inspector

)C W. F. Christianson Attn:

Zimmer Project Inspector FEB 16 1983 Region III

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