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=Text=
=Text=
{{#Wiki_filter:-                   -      -.      -    .        ._ --.              .      . - . - .        _ . -
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7 4' f        'a,       JUN-28 '90 Erf 51' ID SONOPCCH.CGTLE                 TEL NO 1-205-877-7995                     , g,77ta Pa2           Lj i
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Georg a Pone Compaar m en~e
' 'a, 7 4' JUN-28 '90 Erf 51' ID SONOPCCH.CGTLE TEL NO 1-205-877-7995
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DOCKETED USHRC um ,                                                                          ExhibitN,page I             of T i
Georg a Pone Compaar i
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                                                                  '95 MAY -3 P5 :02 wonen. as m mi 0FFICE OF e~rRETARY                       the men e*cu s>wn
ExhibitN,page I USHRC of T um,
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Nucer Op roons ELV-01729                     1 0415                           1 Docket No.         50-424 U. $. Nuclear Regulatory Commission                                                                                         f ATTN: Document Control Desk                                                                                                 i Washington, D. C. 20555 Gentlemen:                                                                                                 .
'95 MAY -3 P5 :02 i
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V0GTLE ELECTRIC GENERATING PLANT                                                           l LICENSEE EVENT REPORT                                                                 i LQ11.0F 0FFSITE POWER LEADS TO SITE AREA EMERGENCY                                                   j O             In accordance with 10 CFR 50.73, Georgia Power Company hereby submits the enclosed revised report related to an event which occurred on March 20, 1990.
: w. a. w,. ten, m DOCHEllHG JTilcF sw ve. r,.wi Bfw;a Nucer Op roons
This revision is necessary to correct the information related to the number of successful Diesel Generator starts subsequent to the comprehensive test program
~
  ,                as discussed in the original report and our April 9, 1990 letter (ELV-01516).
ELV-01729 0415 1
1 The previous LER stated that the Diesel Generator had been started at least 18 times without failures or problems. The number of tests was determined by counting Diesel Generator tests regardless of whether or not the test constituted a valid test in accordance with Regulatory Guide 1.108, however, only valid failures were considered in reaching the conclusion that there had been no failures or problems. This revision to the LER reflects the results of                                             :
Docket No.
val.id tests +since the M 206 1990 event 1
50-424 U. $. Nuclear Regulatory Commission f
SfhcereTy,                                                             )
ATTN: Document Control Desk i
l l
Washington, D. C.
l W. G. Hairston, !!!
20555 Gentlemen:
NUCLEAR REGULATORY COMMISSION WGH,111/NJS/ga Ts.H t%-0L A =5 U "" ' "*                                           '
1 V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LQ11.0F 0FFSITE POWER LEADS TO SITE AREA EMERGENCY j
O In accordance with 10 CFR 50.73, Georgia Power Company hereby submits the enclosed revised report related to an event which occurred on March 20, 1990.
This revision is necessary to correct the information related to the number of successful Diesel Generator starts subsequent to the comprehensive test program as discussed in the original report and our {{letter dated|date=April 9, 1990|text=April 9, 1990 letter}} (ELV-01516).
1 The previous LER stated that the Diesel Generator had been started at least 18 times without failures or problems. The number of tests was determined by counting Diesel Generator tests regardless of whether or not the test constituted a valid test in accordance with Regulatory Guide 1.108, however, only valid failures were considered in reaching the conclusion that there had been no failures or problems. This revision to the LER reflects the results of val.id tests +since the M 206 1990 event 1
SfhcereTy, l
W. G. Hairston, !!!
NUCLEAR REGULATORY COMMISSION WGH,111/NJS/ga Ts.H t%-0L A =5
" ' " " 'n 2 U "" ' "*


==Enclosure:==
==Enclosure:==
LER 50-424/1990-006-01                 in tne matters       hw'     " u.m
LER 50-424/1990-006-01 u.m in tne matters hw' O
                                                                                                              ' " " 'n 2 O              xc (>a a xt a i >                                               -                      'll;';'e         ;
xc (>a a xt a i >
intervenor         V         REJECTED 9505230335 950420                                   Conto Ottr PDR       ADOCK 05000424                           Contractor                     DATE     d 4 6 Q                       PDR                         Other                         Wrtness I-la s %
'll;';'
Reporter         T 1;llask?
e intervenor V
REJECTED 9505230335 950420 Conto Ottr PDR ADOCK 05000424 Contractor DATE d 4 6 Q
PDR Other Wrtness I-la s %
Reporter T 1;llask?


                        'm             .'                    Company Mama. Geo<g a 30308 1pophone 404 526 3195 4Te,$b.+..y .                                                           Exhibitb,page 3 of 6 comon.ee so im 4}
'm Company Mama. Geo<g a 30308 1pophone 404 526 3195 4Te,$b.+..y.
Exhibitb,page 3 of 6 comon.ee so im 4}
e;rmingham. Alacema 35201
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e;rmingham. Alacema 35201 Tolophone 205 868 5561 rne soumemewc system
Tolophone 205 868 5561 rne soumemewc system
                                              . w. o. newen, m                                                           ,
. w. o. newen, m Dei EN/a"o$"
i Dei EN/a"o$"                                                                                                     l ELV-01729 0468 Docket No. 50-424 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LOSS OF OFFSITE POWER LEADS TO SITE AREA EMERGENCY                                   ,
ELV-01729 0468 Docket No. 50-424 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C.
In accordance with 10 CFR 50.73, Georgia Power Company (GPC) hereby submits the                                     i enclosed revised report related to an event which occurred on March 20, 1990.                                         !
20555 Gentlemen V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LOSS OF OFFSITE POWER LEADS TO SITE AREA EMERGENCY In accordance with 10 CFR 50.73, Georgia Power Company (GPC) hereby submits the i
O                                       This revision is necessary to clarify the information related to the number of                                       ;
enclosed revised report related to an event which occurred on March 20, 1990.
successful diesel generator starts as discussed in the original LER dated April                                       l 19, 1990 and our earlier letter (ELV-01516) dated April 9,1990 and to update                                         ,
O This revision is necessary to clarify the information related to the number of successful diesel generator starts as discussed in the original LER dated April 19, 1990 and our earlier letter (ELV-01516) dated April 9,1990 and to update the status of corrective actions. The letter of April 9 stated that Diesel Generator IA had been started 18 times and that Diesel Generator 18 had been started 19 times since March 20, 1990. The LER dated April 19 inadvertently stated " subsequent to this test program, DG1A and DG18 have been started at j
the status of corrective actions. The letter of April 9 stated that Diesel Generator IA had been started 18 times and that Diesel Generator 18 had been started 19 times since March 20, 1990. The LER dated April 19 inadvertently stated " subsequent to this test program, DG1A and DG18 have been started at                                         j least 18 times each and no failures or problems have occurred during any of                                           '
least 18 times each and no failures or problems have occurred during any of these starts". The report should have stated " Subsequent to the event
these     starts". The report should have stated " Subsequent to the event
... rather than " Subsequent to this test program..." with this change the.LER is consistent with the letter of April 9 and the presentation made by GPC to the NRC in Atlanta on the same day.
                                            ... rather than " Subsequent to this test program..." with this change the.LER is consistent with the letter of April 9 and the presentation made by GPC to the NRC in Atlanta on the same day.
In. order.to. correct the. LEA.. ant to.pec;.da more. usaful and.
In. order.to. correct the. LEA.. ant to.pec;.da more. usaful and.                   to.. da.ta,                     !
to.. da.ta, informationtheLERhasbeenrevisedtostatethenumberofialiddietel generator tests in accordance with Regulatory Guide 1.108 rather ti.:..: the number of " successful" starts since the event. The number of valid tests was established by reviewing diesel generator testing data from March 20 through June 7, 1990.
informationtheLERhasbeenrevisedtostatethenumberofialiddietel                                                         I generator tests in accordance with Regulatory Guide 1.108 rather ti.:..: the number of " successful" starts since the event. The number of valid tests was established by reviewing diesel generator testing data from March 20 through June 7, 1990.
Sincerely.
Sincerely.
W. G. Hairston, III WCW,III/HWM/gm
W. G. Hairston, III WCW,III/HWM/gm


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the 30Whern eductraf SrSlem tiederd Nucie.t Ope,aws ELV-01729 0415 Docket No.           50-424 U. 3. Nuclear Regulatory Commission ATTN: Document control Desk Washington, D. C. 20555 Gentlemen:
ExhibitU'page 3-C 4o n
V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT
e.am,
,                                  LOSS OF 0FFSITE POWER LEADS TO SITE AREA EMERGENCY O     In accordance with 10 CFR 50.73, Georgia Power Company hereby submits the enclosed revised report related to an event which occurred on March 20, 1990.                                           l This revision is necessary to correct the information related to the number of                                         I successful Diesel Generator starts subsequent to the comprehensive test program                                         i as discussed in the original report and our April 9,1990 letter (ELV-01516).                                           l The previous LER stated that the Olesel Generator had been started at least 18                                         !
t;;ch'a*;.*.'"''
times without failures or problems. The number of starts was determined by counting Diesel Generator starts regardless of whether or not the test constituted a valid test in accordance with Repulatory Guide 1.108. This revision to the LER reflects the results of va id tests since the March 20, 1990 event.
the 30Whern eductraf SrSlem tiederd Nucie.t Ope,aws ELV-01729 0415 Docket No.
Sincerely,                                                     l W. G. Hhirston, !!!
50-424 U. 3. Nuclear Regulatory Commission ATTN: Document control Desk Washington, D. C.
20555 Gentlemen:
V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LOSS OF 0FFSITE POWER LEADS TO SITE AREA EMERGENCY O
In accordance with 10 CFR 50.73, Georgia Power Company hereby submits the enclosed revised report related to an event which occurred on March 20, 1990.
This revision is necessary to correct the information related to the number of successful Diesel Generator starts subsequent to the comprehensive test program as discussed in the original report and our {{letter dated|date=April 9, 1990|text=April 9,1990 letter}} (ELV-01516).
The previous LER stated that the Olesel Generator had been started at least 18 times without failures or problems. The number of starts was determined by counting Diesel Generator starts regardless of whether or not the test constituted a valid test in accordance with Repulatory Guide 1.108.
This revision to the LER reflects the results of va id tests since the March 20, 1990 event.
Sincerely, W. G. Hhirston, !!!
WGH,!!!/NJS/gm
WGH,!!!/NJS/gm


==Enclosure:==
==Enclosure:==
LER 50-424/1990-006-01 XC(seentXtpage)
LER 50-424/1990-006-01 XC(seentXtpage)
O                                                                                                                             l
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Q                                                                                                                Int $OutItm titCl!C $r$lem Se rV Pt             rw .                                          .
00'*'gTs["***
w., op.,.m ELV-01729 0468                                           :
Exhibit kdl,pa08b of.$I Q
Docket No. 50-424                                                                                                                                         !
t."21auTia?"
U. S. Nuclear Regulatory Commission                                                                                                                       i ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen:
Int $OutItm titCl!C $r$lem Se rV Pt rw.
V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT                                                                               1 Loss OF 0FFt1TE POWER LEADS To SITE AREA EMERCENcY Inaccordancewith10CFR50.73,GeorgiaPowerCompany(GPC)herebysubmitsthe                                                                                       I enclosed revised report related to an event which occurred on March 20, 1990,                                                                             l This revision is necessary to clarify the information related to the number of successful diesel generator starts as discussed in the original LER dated April 19, 1990 and our earlier letter (ELV-01516) dated April 9,1990 and to update                                                                               j O,         the status of corrective. actions. The letter of April 9 stated.that Diesel Generator 1A had been started 18 times and that Diesel Generator 1B had been                                                                             :
w., op.,.m ELV-01729 0468 Docket No. 50-424 U. S. Nuclear Regulatory Commission i
started 19 times since March 20, 1990. The LER dated A)ril 19 inadvertently                                                                               !
ATTN: Document Control Desk Washington, D. C.
stated " Subsequent to this test program, DG1A and DG1B inve been started at-                                                                             l 1 east 18 times each and no failures or problems have occurred during any of these starts". The statement made in the LER and in the April 9 letter did not consider troubleshooting problems associated with the restarting of Diesel Generator 18, which was out of service for maintenance at the time of the event.
20555 Gentlemen:
The report should have stated " Subsequent to the event ..."rather than
V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT 1
            " Subsequent to this test program..." with this change the LER is consistent with the letter of April 9 and the presentation made by GPC to the NRC in Atlanta on the same day.
Loss OF 0FFt1TE POWER LEADS To SITE AREA EMERCENcY Inaccordancewith10CFR50.73,GeorgiaPowerCompany(GPC)herebysubmitsthe enclosed revised report related to an event which occurred on March 20, 1990, This revision is necessary to clarify the information related to the number of successful diesel generator starts as discussed in the original LER dated April 19, 1990 and our earlier letter (ELV-01516) dated April 9,1990 and to update j
4            in order tu correct' the tER"and'to provide more nefut and'up to dute -
O, the status of corrective. actions.
information the LER has been revised to state the number of valid diesel generator tests in accordance with Regulatory Guide 1.108 rather than the number of successful starts since the event. The number of valid tests was established by reviewing diesel generator testing data from March 21 inrough June 7, 1990.                                                                             !
The letter of April 9 stated.that Diesel Generator 1A had been started 18 times and that Diesel Generator 1B had been started 19 times since March 20, 1990. The LER dated A)ril 19 inadvertently stated " Subsequent to this test program, DG1A and DG1B inve been started at-1 east 18 times each and no failures or problems have occurred during any of these starts". The statement made in the LER and in the April 9 letter did not consider troubleshooting problems associated with the restarting of Diesel Generator 18, which was out of service for maintenance at the time of the event.
Sincerely, W. G. Hairston, III                                                                       i l
The report should have stated " Subsequent to the event..."rather than
O          WGH,111/HWM/gm
" Subsequent to this test program..." with this change the LER is consistent with the letter of April 9 and the presentation made by GPC to the NRC in Atlanta on the same day.
in order tu correct' the tER"and'to provide more nefut and'up to dute -
4 information the LER has been revised to state the number of valid diesel generator tests in accordance with Regulatory Guide 1.108 rather than the number of successful starts since the event. The number of valid tests was established by reviewing diesel generator testing data from March 21 inrough June 7, 1990.
Sincerely, W. G. Hairston, III O
WGH,111/HWM/gm


==Enclosure:==
==Enclosure:==
LER 50-424/1990-006-01                                                               PLADmFFS EXWBTT g oo                               l 1
LER 50-424/1990-006-01 PLADmFFS EXWBTT g oo
--.. ~....


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Exhibit M,page 6 of.1.
wer s                 x Exhibit M,page 6 of.1.                         !
l l
ELV-01729 i
ELV-01729 i
0470 l
0470 Docket No.
Docket No.             50-424                                                                                       l i
50-424 i
U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen:
U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C.
l V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LOSS OF 0FFSITE POWER LEADS TO SITE AREA EMERGENCY In accordance with 10 CFR 50.73, Georgia Power Company enclosed revised report related to an event which occurr(GPC)               ed onhereby March submits 20, 1990.the This revision is necessary to clarify the information related to the number of O successful                        diesel generator starts as discussed in the origina 19, 1990 and to update the status of corrective actions.
20555 Gentlemen:
V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LOSS OF 0FFSITE POWER LEADS TO SITE AREA EMERGENCY In accordance with 10 CFR 50.73, Georgia Power Company enclosed revised report related to an event which occurr(GPC) hereby submits the ed on March 20, 1990.
O successful diesel generator starts as discussed in the origina This revision is necessary to clarify the information related to the number of 19, 1990 and to update the status of corrective actions.
If the criteria for the completion of the test program is understood to be the first successful test in accordance with Vogtle Electric Generating Plant
If the criteria for the completion of the test program is understood to be the first successful test in accordance with Vogtle Electric Generating Plant
        " Diesel Generator Operability Test," then there were(VEGP) procedure 14980-1 10 successful starts of Diesel completion               Generator of the test 1A  and and program      12 the successful    starts end of April         of Diesel 19, 1990,   the dateGenerator the LER     1B bet 50-424/1990-06               was submitted to the NRC.
" Diesel Generator Operability Test," then there were(VEGP) procedure 14980-1 10 successful starts of Diesel Generator 1A and 12 successful starts of Diesel Generator 1B bet completion of the test program and the end of April 19, 1990, the date the LER 50-424/1990-06 was submitted to the NRC.
In order to correct the LER and to provide more useful and up to date information the LER has been revised to state the number of valid diesel of successfut* startr sfnce the event. generator tests in accordance with Regulato The number of valid tests was established by reviewing diesel generator testing. data. froa March 2.L thr@ Jewh 1996:
In order to correct the LER and to provide more useful and up to date information the LER has been revised to state the number of valid diesel of successfut* startr sfnce the event. generator tests in accordance with Regulato The number of valid tests was established by reviewing diesel generator testing. data. froa March 2.L thr@ Jewh 1996:
Sincerely, W. G. Hairston, Ill WGH,!!!                                                                                                                   j Enclosur/HWH/gm       e: LER 50-424/1990-006-01                                                                         l
Sincerely, W. G. Hairston, Ill WGH,!!!
                                                                                                                                )
j Enclosur/HWH/gm e:
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LER 50-424/1990-006-01 ya 5 45 M L
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Latest revision as of 06:06, 14 December 2024

Intervenor Exhibit I-MOSBA-64,consisting of Ltr Forwarding LER Re Loss of Offsite Power Leads to Site Area Emergency
ML20083D041
Person / Time
Site: Vogtle  
Issue date: 04/20/1995
From: Hairston W
GEORGIA POWER CO.
To:
References
OLA-3-I-MOS-064, OLA-3-I-MOS-64, NUDOCS 9505230335
Download: ML20083D041 (5)


Text

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ELV-01729 0415 1

Docket No.

50-424 U. $. Nuclear Regulatory Commission f

ATTN: Document Control Desk i

Washington, D. C.

20555 Gentlemen:

1 V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LQ11.0F 0FFSITE POWER LEADS TO SITE AREA EMERGENCY j

O In accordance with 10 CFR 50.73, Georgia Power Company hereby submits the enclosed revised report related to an event which occurred on March 20, 1990.

This revision is necessary to correct the information related to the number of successful Diesel Generator starts subsequent to the comprehensive test program as discussed in the original report and our April 9, 1990 letter (ELV-01516).

1 The previous LER stated that the Diesel Generator had been started at least 18 times without failures or problems. The number of tests was determined by counting Diesel Generator tests regardless of whether or not the test constituted a valid test in accordance with Regulatory Guide 1.108, however, only valid failures were considered in reaching the conclusion that there had been no failures or problems. This revision to the LER reflects the results of val.id tests +since the M 206 1990 event 1

SfhcereTy, l

W. G. Hairston, !!!

NUCLEAR REGULATORY COMMISSION WGH,111/NJS/ga Ts.H t%-0L A =5

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Enclosure:

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ELV-01729 0468 Docket No. 50-424 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C.

20555 Gentlemen V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LOSS OF OFFSITE POWER LEADS TO SITE AREA EMERGENCY In accordance with 10 CFR 50.73, Georgia Power Company (GPC) hereby submits the i

enclosed revised report related to an event which occurred on March 20, 1990.

O This revision is necessary to clarify the information related to the number of successful diesel generator starts as discussed in the original LER dated April 19, 1990 and our earlier letter (ELV-01516) dated April 9,1990 and to update the status of corrective actions. The letter of April 9 stated that Diesel Generator IA had been started 18 times and that Diesel Generator 18 had been started 19 times since March 20, 1990. The LER dated April 19 inadvertently stated " subsequent to this test program, DG1A and DG18 have been started at j

least 18 times each and no failures or problems have occurred during any of these starts". The report should have stated " Subsequent to the event

... rather than " Subsequent to this test program..." with this change the.LER is consistent with the letter of April 9 and the presentation made by GPC to the NRC in Atlanta on the same day.

In. order.to. correct the. LEA.. ant to.pec;.da more. usaful and.

to.. da.ta, informationtheLERhasbeenrevisedtostatethenumberofialiddietel generator tests in accordance with Regulatory Guide 1.108 rather ti.:..: the number of " successful" starts since the event. The number of valid tests was established by reviewing diesel generator testing data from March 20 through June 7, 1990.

Sincerely.

W. G. Hairston, III WCW,III/HWM/gm

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the 30Whern eductraf SrSlem tiederd Nucie.t Ope,aws ELV-01729 0415 Docket No.

50-424 U. 3. Nuclear Regulatory Commission ATTN: Document control Desk Washington, D. C.

20555 Gentlemen:

V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LOSS OF 0FFSITE POWER LEADS TO SITE AREA EMERGENCY O

In accordance with 10 CFR 50.73, Georgia Power Company hereby submits the enclosed revised report related to an event which occurred on March 20, 1990.

This revision is necessary to correct the information related to the number of successful Diesel Generator starts subsequent to the comprehensive test program as discussed in the original report and our April 9,1990 letter (ELV-01516).

The previous LER stated that the Olesel Generator had been started at least 18 times without failures or problems. The number of starts was determined by counting Diesel Generator starts regardless of whether or not the test constituted a valid test in accordance with Repulatory Guide 1.108.

This revision to the LER reflects the results of va id tests since the March 20, 1990 event.

Sincerely, W. G. Hhirston, !!!

WGH,!!!/NJS/gm

Enclosure:

LER 50-424/1990-006-01 XC(seentXtpage)

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w., op.,.m ELV-01729 0468 Docket No. 50-424 U. S. Nuclear Regulatory Commission i

ATTN: Document Control Desk Washington, D. C.

20555 Gentlemen:

V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT 1

Loss OF 0FFt1TE POWER LEADS To SITE AREA EMERCENcY Inaccordancewith10CFR50.73,GeorgiaPowerCompany(GPC)herebysubmitsthe enclosed revised report related to an event which occurred on March 20, 1990, This revision is necessary to clarify the information related to the number of successful diesel generator starts as discussed in the original LER dated April 19, 1990 and our earlier letter (ELV-01516) dated April 9,1990 and to update j

O, the status of corrective. actions.

The letter of April 9 stated.that Diesel Generator 1A had been started 18 times and that Diesel Generator 1B had been started 19 times since March 20, 1990. The LER dated A)ril 19 inadvertently stated " Subsequent to this test program, DG1A and DG1B inve been started at-1 east 18 times each and no failures or problems have occurred during any of these starts". The statement made in the LER and in the April 9 letter did not consider troubleshooting problems associated with the restarting of Diesel Generator 18, which was out of service for maintenance at the time of the event.

The report should have stated " Subsequent to the event..."rather than

" Subsequent to this test program..." with this change the LER is consistent with the letter of April 9 and the presentation made by GPC to the NRC in Atlanta on the same day.

in order tu correct' the tER"and'to provide more nefut and'up to dute -

4 information the LER has been revised to state the number of valid diesel generator tests in accordance with Regulatory Guide 1.108 rather than the number of successful starts since the event. The number of valid tests was established by reviewing diesel generator testing data from March 21 inrough June 7, 1990.

Sincerely, W. G. Hairston, III O

WGH,111/HWM/gm

Enclosure:

LER 50-424/1990-006-01 PLADmFFS EXWBTT g oo

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29 se mes rois m u O

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Exhibit M,page 6 of.1.

ELV-01729 i

0470 Docket No.

50-424 i

U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C.

20555 Gentlemen:

V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORT LOSS OF 0FFSITE POWER LEADS TO SITE AREA EMERGENCY In accordance with 10 CFR 50.73, Georgia Power Company enclosed revised report related to an event which occurr(GPC) hereby submits the ed on March 20, 1990.

O successful diesel generator starts as discussed in the origina This revision is necessary to clarify the information related to the number of 19, 1990 and to update the status of corrective actions.

If the criteria for the completion of the test program is understood to be the first successful test in accordance with Vogtle Electric Generating Plant

" Diesel Generator Operability Test," then there were(VEGP) procedure 14980-1 10 successful starts of Diesel Generator 1A and 12 successful starts of Diesel Generator 1B bet completion of the test program and the end of April 19, 1990, the date the LER 50-424/1990-06 was submitted to the NRC.

In order to correct the LER and to provide more useful and up to date information the LER has been revised to state the number of valid diesel of successfut* startr sfnce the event. generator tests in accordance with Regulato The number of valid tests was established by reviewing diesel generator testing. data. froa March 2.L thr@ Jewh 1996:

Sincerely, W. G. Hairston, Ill WGH,!!!

j Enclosur/HWH/gm e:

LER 50-424/1990-006-01 ya 5 45 M L

v