ENS 40957: Difference between revisions

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| event date = 08/15/2004 04:05 CDT
| event date = 08/15/2004 04:05 CDT
| last update date = 08/15/2004
| last update date = 08/15/2004
| title = Automatic Reactor Scram Following Partial Loss Of Offsite Power
| title = Automatic Reactor Scram Following Partial Loss of Offsite Power
| event text = At 0405 on August 15, 2004, River Bend Station had a loss of 230Kv Line #353 (RSS #2, Port Hudson) feeding the plant's switchyard. This resulted in a generator trip and a reactor scram. Feedwater tripped on a Reactor vessel Level 8 signal. RCIC is operating to control reactor vessel level. SRVs were used to manually control pressure. Mechanical vacuum pump (ARC A) would not start to control condenser vacuum. The MSIVs were manually isolated in anticipation of a Group 6 isolation (low vacuum). There was no ECCS initiation. Power was restored to the mechanical vacuum pump ARC B. Vacuum was restored and main steam lanes are in use for pressure control. We are still investigating the root cause.
| event text = At 0405 on August 15, 2004, River Bend Station had a loss of 230Kv Line #353 (RSS #2, Port Hudson) feeding the plant's switchyard. This resulted in a generator trip and a reactor scram. Feedwater tripped on a Reactor vessel Level 8 signal. RCIC is operating to control reactor vessel level. SRVs were used to manually control pressure. Mechanical vacuum pump (ARC A) would not start to control condenser vacuum. The MSIVs were manually isolated in anticipation of a Group 6 isolation (low vacuum). There was no ECCS initiation. Power was restored to the mechanical vacuum pump ARC B. Vacuum was restored and main steam lanes are in use for pressure control. We are still investigating the root cause.
The following ESF actuations occurred:
The following ESF actuations occurred:

Latest revision as of 21:23, 1 March 2018

ENS 40957 +/-
Where
River Bend Entergy icon.png
Louisiana (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-0.25 h-0.0104 days <br />-0.00149 weeks <br />-3.4245e-4 months <br />)
Opened: James Boyle
08:50 Aug 15, 2004
NRC Officer: Steve Sandin
Last Updated: Aug 15, 2004
40957 - NRC Website
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