ENS 41402: Difference between revisions

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| event date = 02/10/2005 23:00 EST
| event date = 02/10/2005 23:00 EST
| last update date = 02/11/2005
| last update date = 02/11/2005
| title = Technical Specification Required Shutdown Due To Loss Of Electrical Power Sources
| title = Technical Specification Required Shutdown Due to Loss of Electrical Power Sources
| event text = Event:  At 23:00 [EST] on 2-10-05, Oconee Unit 1 initiated a plant shutdown as required by its Technical Specifications.  Technical Specification 3.8.1 Condition M, Required Action M.1 requires Oconee Unit 1 to enter Mode 3 by 03:06 on 2-11-05 due to Keowee Hydro Unit 2 and CT-1 inoperable.  Keowee Hydro Unit 2 is inoperable due to a planned outage, with restoration in progress.  CT-1 is inoperable due to experiencing a lockout at 12:12 on 2-10-05 during testing to restore Keowee.
| event text = Event:  At 23:00 [EST] on 2-10-05, Oconee Unit 1 initiated a plant shutdown as required by its Technical Specifications.  Technical Specification 3.8.1 Condition M, Required Action M.1 requires Oconee Unit 1 to enter Mode 3 by 03:06 on 2-11-05 due to Keowee Hydro Unit 2 and CT-1 inoperable.  Keowee Hydro Unit 2 is inoperable due to a planned outage, with restoration in progress.  CT-1 is inoperable due to experiencing a lockout at 12:12 on 2-10-05 during testing to restore Keowee.
Initial Safety Significance: Oconee Unit 1 is being shut down in accordance with Technical Specifications.  Unit auxiliaries will be powered from the Standby busses and a Lee Combustion Turbine.  When the turbine is tripped, the Unit will enter into the natural circulation mode of cooling due to loss of Reactor Coolant Pumps.   
Initial Safety Significance: Oconee Unit 1 is being shut down in accordance with Technical Specifications.  Unit auxiliaries will be powered from the Standby busses and a Lee Combustion Turbine.  When the turbine is tripped, the Unit will enter into the natural circulation mode of cooling due to loss of Reactor Coolant Pumps.   

Latest revision as of 21:21, 1 March 2018

ENS 41402 +/-
Where
Oconee Duke Energy icon.png
South Carolina (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Time - Person (Reporting Time:+-3.73 h-0.155 days <br />-0.0222 weeks <br />-0.00511 months <br />)
Opened: David Nix
00:16 Feb 11, 2005
NRC Officer: Mike Ripley
Last Updated: Feb 11, 2005
41402 - NRC Website
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