ENS 41402: Difference between revisions
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| event date = 02/10/2005 23:00 EST | | event date = 02/10/2005 23:00 EST | ||
| last update date = 02/11/2005 | | last update date = 02/11/2005 | ||
| title = Technical Specification Required Shutdown Due | | title = Technical Specification Required Shutdown Due to Loss of Electrical Power Sources | ||
| event text = Event: At 23:00 [EST] on 2-10-05, Oconee Unit 1 initiated a plant shutdown as required by its Technical Specifications. Technical Specification 3.8.1 Condition M, Required Action M.1 requires Oconee Unit 1 to enter Mode 3 by 03:06 on 2-11-05 due to Keowee Hydro Unit 2 and CT-1 inoperable. Keowee Hydro Unit 2 is inoperable due to a planned outage, with restoration in progress. CT-1 is inoperable due to experiencing a lockout at 12:12 on 2-10-05 during testing to restore Keowee. | | event text = Event: At 23:00 [EST] on 2-10-05, Oconee Unit 1 initiated a plant shutdown as required by its Technical Specifications. Technical Specification 3.8.1 Condition M, Required Action M.1 requires Oconee Unit 1 to enter Mode 3 by 03:06 on 2-11-05 due to Keowee Hydro Unit 2 and CT-1 inoperable. Keowee Hydro Unit 2 is inoperable due to a planned outage, with restoration in progress. CT-1 is inoperable due to experiencing a lockout at 12:12 on 2-10-05 during testing to restore Keowee. | ||
Initial Safety Significance: Oconee Unit 1 is being shut down in accordance with Technical Specifications. Unit auxiliaries will be powered from the Standby busses and a Lee Combustion Turbine. When the turbine is tripped, the Unit will enter into the natural circulation mode of cooling due to loss of Reactor Coolant Pumps. | Initial Safety Significance: Oconee Unit 1 is being shut down in accordance with Technical Specifications. Unit auxiliaries will be powered from the Standby busses and a Lee Combustion Turbine. When the turbine is tripped, the Unit will enter into the natural circulation mode of cooling due to loss of Reactor Coolant Pumps. | ||
Latest revision as of 21:21, 1 March 2018
| Where | |
|---|---|
| Oconee South Carolina (NRC Region 2) | |
| Reporting | |
| 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
| Time - Person (Reporting Time:+-3.73 h-0.155 days <br />-0.0222 weeks <br />-0.00511 months <br />) | |
| Opened: | David Nix 00:16 Feb 11, 2005 |
| NRC Officer: | Mike Ripley |
| Last Updated: | Feb 11, 2005 |
| 41402 - NRC Website
| |