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MAfI ORNL/NOAC-231 Engineering Technology Division Nuclear Operations Analysis Center REVIEW OF THE OPERATING EXPERIENCE HISTORY THROUGH 1984 OF HADDAM NECK FOR THE NUCLEAR REGULATORY COMMISSION'S INTEGRATED SAFETY ASSESSMENT P,ROGRAM A. D. C. Kimmins V. D. Clemons Draft MAFI Prepared for the U.S. Nuclear Regulatory Commission Office of Nuclear Reactor Regulation Under Interagency Agreements DOE 40-554-75 NRC FIN No. A9469 Prepared by the OAK RIDGE NATIONAL LABORATORY Oak Ridge, Tennessee 37831 l                                            operated by l
MARTIN MARIETTA ENERGY SYSTEMS, INC.
t for the l                                    U.S. DEPARTMENT OF ENERGY j                          under Contract No. DE-AC05-840R21400 9607090593 860703          ''
PDR  ADOCK 05000213 P              PDR 1
 
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* y FOREWORD The work reported here was undertaken by the Nuclear Operations An-alysis Center (NOAC) at Oak Ridge National Laboratory on behalf of the Office of Nuclear Reactor Regulation (NRR) of the Nuclear Regulatory Commission (NRC).      The technical monitor for the proj ect was E.              M.
McKenna of the NRR Integrated Safety Assessment Directorate.
NOAC performs analysis tasks, as well as information gathering activities, for the NRC.        NOAC's activities involve many aspects of nu-clear power reactor operations and safety.
NOAC was established in 1981 to reflect the broadening and refocus-ing of the scope and activities of its predecessor, the Nuclear Safety Infor: nation Center. It conducts a number of tasks related to the analy-sis of nuclear power experience, including summaries of operation for U.S. power reactors, generic case studies, plant operating assessments, and risk assessments.
NOAC has designed and developed a number of major data bases that it operates and maintains for the NRC. These data bases collect diverse i        types of information on nuclear power reactors from the construction l
phase through routine and off-normal operation.                These data bases make extensive    use  of  reactor-operator-submitted            reports,  such as    the Licensee Event Reports.
NOAC also publishes staff studies and bibliographies, disseminates monthly nuclear power plant operating event reports, and prepares the Nuclear Safety Journal.          Direct all inquiries to Joel R.            Buchanan, Director, Nuclear Operations Analysis Center,                P.O. Box Y,  Oak Ridge National    Laboratory,  Oak      Ridge,        TN 37831,  Telephone  615-574-0393 (FTS:  624-0393).
 
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                                                      = .      .                                                a  f TABLE OF CONTENTS i
1 Page FOREWORD    .......................................................                                    I t
LIST OF TABLES      .................................................                                \/
l LIST OF FIGURES      ................................................                                Vi EXECUTIVE
 
==SUMMARY==
        ..............................................                            dU
!    ABSTRACT    .......................................................                                XV l
l    1. INTR 3 DUCTION    ...............................................                              I i
: 2. REVIEW METHODOLOGY          .........................................                          4 2.1 Availability and Capacity Factors                        ...... ...............            JI 2.2 Environmental Events                ..................................                    6 2.3 Forced Shutdowns and Power Reductions                          .................          6 2.4 Reportable Events            .....................................                      7 2.5 Evaluation of Operating Experience                        ....................          9
: 3. OPERATING EXPERIENCE REVIEW EVALUATION                      .....................            IO 3.1 General Plant Description                    .............................                /o 32 Evaluation Findings              ...................................                      10 33 Availability and Capacity Factors                        .....................            /1 3.4 Forced Shutdowns and Power Reductions                          ............... ..      11.
3.4.1    Systems Involved in Forced Shutdowns and l                          Power Reductions              ...............................                  SLI 1
l Steam and Power Systems                                          LJ 3.4.1.1                                                ...............
3.4.1.2      Electrical Power Systems                  ..............      %t 3.4.1.3      Instrumentation and Controls                    ... .... ... Of 3.5 Causes of Forced Shutdowns and Power Reductions                                ..... ..  ?dl l
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Page 3.6 Non-DBE Shutdowns      .....................................                        %7 3.7 DBE-Initiated Events          ..................................                    7. f 3.7.1    D2.2 - Feedwater system malfunctions that resulted in an increase in feedwater flow                    ......      IO 3.7.2    D2.2 - Loss of external electric load                  ..........        Io 3.7.3    D2.3 - Turbine trips        ...........................                  D 3.7.4    D2.6 - Coincident loss of onsite and offsite AC power to the station          ........................                R 3.7.5    D2.7 - Loss of normal feedwater flow ....'.......                        79 3.7.6    D3.1 - Single and multiple reactor coolant pump trips    .....................................                      7I 3.7.7    D4.3 - Control rod maloperation              ................            II 3.8 Reportable Events      .....................................                      3I 3.9 Systems Involved in Reportable Events                .................            If 3.9.1    Reactor Coolant Syssea          .........................              37
* 3.9 2 Electrical Power System              ........................              JT 3.9.3    Steam and Power System          .........................              4-8 3.9.4    Instrumentation and Controls            ...................            fl 3.9.5    Chemical and Volume Control System                .............        42.
3 9.6 Reactog                    System      ......................              43
: y. 9. 7 F,el H,,ggiwg, 5y:; fg,.,g .          ,  ,.      ,          . . . . . . 4.]
3.9 8 Engineered Safety Features Systems                    .............        Af 3.10 Causes of Reportable Events            ..........................              Of 3 11 Events of Environmental Importance                ...................            f7 3.12 Radioactive Release Events            ...........................                4~7 3.13 Nonradiological Events          ...............................                  f?
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s  e Page 3.14 Review of Significant Events        .........................            N 3.14.1  Loss of Offsite Power      ........................            b 3.14.2 Unanticipated Reactor Cooldown              ...............      [8' 3.14.3 Loss of Auxiliary Feedwater            ..................        [9 3.14.4 Failure of a Feedwater Regulating Valve                  ...... ET 3.14.5 Blocked Open Blowdown Lines            ..................        [O 3 14.6 Reactor Coolant Pump Failures            ................      S8 3.14.7  Pressurizer PORY Inadvertently Opened              ........ S 3.14.8 Boron Recovery Tank Ruptured            .................        52' 3.14.9  Radioactive Spill Resulted in Unplanned Release  ......................................
3.14.10 Control Rod Drives        ..........................
3.14.11 Contaminated Moisture Separator Tube Bundles Released From Site          ..................
3.14.12 Loss of Containment Control Air              ............. SI 3.14.13 Failure of Refueling Pool Seal              ..............    [8 3.15 Trends and Safety Implications of Forced Shutdowns and Power Reductions      .................................
3.16 Trends and Safety Implications of Reportable
                                                                                  '71 Events
: 4. CONCLUSIONS  ................................................                U APPENDIX A: Review of Forced Shutdowns and Power Reductions  ........................................              87 APPENDIX 3:  Review of Reportable Events        ......................./Ii REFERENCES  .....................................................              h edt.~)
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LIST OF IABLES Number 3.1    Availability and Capacity Factors for Haddam Neck                        ....      13 32      Forced Shutdown Summary for Haddam Neck                ..............            / 4 ct 3.3    Power Reduction Summary for,Haddam Neck                ..............            IS~
3.4    NSIC Primary Category Summary for Non-DBE Shutdowns at Haddam Neck    .......................................                      SL7
        ,        3.5    DBE Initiated Events Summary for Haddam Neck                    .........      1.8 3.6    Summary of Systems Involved in Reportable Events at Haddam Neck    .......................................                      $7 3.7    Causes of Reportable Events for Haddam Neck                    ..........      44 3.8    Summary of Radioactivity Released from Haddam Neck    ..........................................                      f'8 3.9    Unplanned Radioactive Releases at Haddam Neck                      ........ fk 3.10      Tabulation of Reports Categorized as Significant at Haddam Neck    .......................................                    S'/
3.11      Summary of Significant Event Categories at Haddam Neck    .......................................                    IlL-I
                                            .                    -          -    .. .              -            __ ~
 
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* LIST OF FIGURES Number 3.1  Haddam Neck Plant    ....................................                                Il 3.2  Availability and Capacity Factors for Haddam Neck                            ....      Ik 3.3  Yearly Totals of Forced Shutdowns            ....................                      Ib 3.3A  Interpreted Forced Shutdown Rate          . . . . . . . . . . . . . . . . . . . . . I7 3.4  Yearly Total of Power Reductions          .....................                        I8 3.4A  Interpreted Power Reduction Rate          .....................                      17 3.5  Steam and Power System Shutdowns          .....................                      28 3 5A  Interpreted Shutdown Rate with Steam and Power Systems as Causes      ..............................                          ll 3.6  Electric Power System Shutdowns          ......................                      L1L 3.7  Forced Shutdowns due to Maintenance and Testing                          ......      16~
3.8  DBE Initiated Shutdowns      ..............................                        1L9 3.9  Turbine Trip Shutdowns      ...............................                          Il 3.10  Yearly Totals of Reportable Events            ...................                    35 3.11  Shutdowns Due to Equipment Failures              ..................                  08' 3.11A Interpreted Shutdown Rate with Equipment Failure as Cause    .....................................                            Ik 3 12  Yearly Totals of Significant Events              ..................
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3.13  Yearly Totals of Conditionally Significant Events                            ....      <J 3.14  Yearly Totals of Significant and Conditionally Significant Events    ...................................                            2h 7-3 15  Yearly Totals of Losses of Electric Power                    ............            75 i    3.16  Yearly Totals of Control Rod Drives Problems                      .........        7 5P i
3.17  Yearly Totals of Charging Pump Problems                  ..............              7G 1
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REVIEW OF THE OPERATING HISTORY OF HADDAM NECK THROUGH 1984 EXECUTIVE
 
==SUMMARY==
 
The Systematic Evaluation Program Branch of the Nuclear Regulatory Commission (NRC) is conducting a pilot program for the Integrated Safety Assessment Program (ISAP), in which all pending licensing actions and safety issues for selected operating reactors will be evaluated.                        A new approach to addressing a growing need for order and efficiency in the
!                    implementation and resolution of licensing requirements for operating nuclear power plants is being evolved under this program.
f The new ISAP approach provides a structure for the regulatory man-agement of licensing requirements on a plant-specific basis. One objec-tive is to assure the implementation of the most ef fective safety mea-sures in the near-term, while using both NRC staff and licensee re-sources  efficiently.                To          accomplish this obj ective ,  ISAP will:
(1) evaluate all applicable issues related to plant safety in accordance with a pre-established scope; (2) identify cost-effective corrective ac-tions, where necessary, to enhance safety on a plant-specific basis; (3) establish a technical basis to judge implementation schedules; and (4) document the results of the evaluation so that the implementation schedule can be periodically updated, as necessary, to incorporate cor-rective actions for issues that may arise in the f..ture.
Tools utilized in the ISAP evaluation process include:                        (1) a de-terministic review of all pending licensing actions and safety issues; (2) a plant-specific Probabilistic Safety Analysis (PSA); and (3) an evaluation of plant operating experience and reliability data, including Yll
 
B  S licensee performance (e.g., from existing Safety Assessments of Licensee Performance (SALP) evaluations].
As part of the pilot program for ISAP, the NRC contracted with the Oak Ridge National Laboratory Nuclear Operations Analysis Center (NOAC) to perform operating history reviews for two plants that volunteered to be included: Millstone 1 and Haddam Neck Plants. These reviews will be used as an integral part of the ISAP evaluation process.                  Each review includes the collection and the evaluation of data on availability and capacity factors, forced shutdowns, forced power reductions, reportable events, environmental events, and radiological release events. The data is analyzed and evaluated to identify any trends and symptoms that will be important in the resolution of regulatory actions to be applied to the plant. Observations and conclusions which focus on the key findings l      of the review are provided.
The review of the Haddam Neck operating history incorporates the findings previously presented in the report generated under the Syste-matic Evaluation Program (SEP) NUREG-0826, " Integrated Plant Safety Assessment, Systematic Evaluation Program - Haddam Neck Plant".                        This new report updates those findings to include data for the years 1982 through 1984.
The operating history review focuses principally on evaluations of l
data which is divided into two segments:          (1) data on forced shutdowns and power reductions and (2) data on reportable events.          In the forced shutdown and power reduction segment, the review identifies Design Basis Events (DBEs) and recurring events that may be used as indicators of po-                            ,
tential operating ct.ncerns. DBEs are defined as tnose events delineated Vlil~
 
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i in the NRC's Standard Revieu Plan, and which result from failures in systems, equipment and operator actions that initiate system transients and challenge engineered safety features.          In the reportable event seg-ment, which includes environmental events and radiological release events, the review identifies significant events and recurring events that may also be used as indicators of potential operating concerns.
Significant events are classified as those events in which a degradation of safety margin occurs, such that safe operation cannot continue to be assured or in which challenges to the safety protection features of the plant resulted. Selection of significant events was accomplished using a set of criteria pre-established in the SEP reviews.            The findings of the review are summarized below.
Conclusions The Haddam Neck Plant has been generally operated in a safe and orderly manner. However the operating hist.ory reveals that there are a few areas with demonstrated deficiencies or indications of conditions relating to safety concerns.        There are no indications in the operating history that there are extended or repetitious problems that have re-suited in any significant safety consequence.
A visit to the plant confirmed inferences derived from the opera-tional review data that attention to safety is an operating character-istic. A tour of the plant left an impression of a clean and well main-tained operation. There was evidence of positive approaches to imple-menting lessons learned from experience.
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One indicator of the quality of performance of plant operations is the ability of a plant to achieve and maintain high levels of reli-ability in operation. This also results in a consequential direct bene-fit to safety. Haddam Neck has a history of higher than average avail-ability and capacity factors. Twice the plant has accomplished extended uninterrupted operating runs, the first for a period of 343 days ending in August 1977 which established a record, and the second for 401 days ending in August 1984.                  .
Adverse effects of the extended runs were not conclusively evident from analysis of the data.      While there was an observable increase in the number of maintenance-generated shutdowns subsequent to the 1977 run, the same characteristic was not observed in the final months of 1984. However, the rate of submittal of LERs af ter each run did in-crease, suggesting an increase in maintenance activities.
Apart from problems in the areas of off-site power, charging pumps, and control rod drives, in general any problems involving nuclear safety systems or equipment were found and resolved without the need of a con-sequent plant shutdown. Sixty-six percent of all shutdowns involving reportable events occurred before 1970, which supports the conclusion that there is an operational focus on preventing nuclear systems problems from resulting in forced shutdowns.
Trends and Symptoms Trends were discerned by examination of the data, and were more evident in the shutdown data than in the reportable event data.          It was concluded that the forced shutdown data showed a definite asymptotic W
_ _ _  _ _ _ _ _ _ _ _ _              1
 
trend of improvement.            However, this conclusion was dependent upon the            j l
premise that certain perturbations to the projected trend can be readily isolated, and correlated to an identifiable set of causes. Accordingly, it was determined that it would be necessary to conduct a broader examination of the operational history.              However, the scope of the effort and . the resources available became limiting factors which con-strained the depth to which this examination could be conducted.
It was concluded that the causes of perturbations which occurred in 1974, 1978, and 1981 may be related to (1) extensive turbine problems, (2) an extended operating run in 1977, and (3) efforts in response to TMI, respectively.      Actual symptoms of these perturbations were not di-rectly attributed to their theorized causes because of limitations in scope and resources.            No direct correlation with reportable event fre-quency was detected.              As another conclusion, it might be anticipated that the effects of major efforts applied to the repair or maintenance of plant components in one area may be evidenced in different and unex-pected areas.
In sunsaary, it was concluded from analysis of the trends that:
: 1. After an initial break-in period the overall performance of the plant was continuously improving with the exception of identified l
i l                          perturbations.
: 2. Major "refic" efforts resulted in perturbations to the plants' overall performance.
;                    3. Recovery from refits extended to one or two years, and probably be-l l                          cause of consequent increases in equipment failures.
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: 4. A perturbation as a result of a refit may not necessarily be evi-danced by problems directly related to that refit. Thus, the more important negative effects of refits may be caused by other reasons such as reduced attention by plant personnel to other areas not affected by the refits.      It should be noted, however, that the shutdown data did not provide any strong indications that plant personnel relaxed their attention to nuclear safety systems.
Three important symptoms were identified through examination of the reportable event data. These were determined from analysis of the sig-nificant events.
Loss of offsite power During the early history of the plants the significant events were dominated by the occurrence of five loss-of-offsite-power events. These were all attributed to problems with the design of the plant protective relaying. Subsequently corrective measures to the protective relays were implemented. However, there was a later recurrence of this problem and additional loss-of-offsite-power events occurred later on during the 1980s. Thus it was concluded that this constitutes an outstanding symptom of a problem which was safety significant.        Loss of offsite power is a precursor to station blackout, . which is a safety issue.
Haddam Neck sustained one actual station blackout during the period under review.
Control rod drive failures A significant number of control rod drop events were experienced during the first three years of operation.        These were determined to have been principally caused by faulty relays. Corrective measures were f                                                            ..
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applied and there was no further recurrence for 6 years.      However, as the plant grew older, control rod drive failures started to reoccur, for causes including separation of rod cluster control vanes, plastic deformation of coupling fingers, and other random equipment failures.
While no direct correlation to aging was made, it was concluded that this may be a factor in the perpetuation of control rod drive prob-less. The control rods are the principal mechanisms for reactivity con-trol and shutdown of the reactor, and thus serve an important safety function. Failure of the drive mechanisms to operate on improper opera-tion are safety concerns. Thus it was concluded that these failures of the control rod drives constitute an outstanding symptoms of a problem
;                      which has safety significance.
1 Charging pump failures The charging pumps became significantly undependable in the latter half of the review period. For the first 9 years no problems were re-ported. However problems started to occur in 1976 and continued through the later half of the review period, again suggestive that aging may be I
a factor. Equipment failures were reported to have been caused typ-ically by wear induced vibration, erosion, chemical solidification, and leaks. The changing pumps serve to inject chemical additions to the re-actor coolant system and also to provide backup to high pressure coolant inj ection should this be required subsequent to an accident, both of which are safety functions. It was concluded that recurrence of oper-ability problems in the charging pumps constitutes an outstanding symp-tom of a problem which has safety significance.
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Other symptoms
                                                                                            ~
It was concluded that causes of downtime were principally for main-tenance and testing, occurring mostly in balance of plant systems in-cluding the turbine generator system, main steam systems, and electric power systems.                In general nuclear systems did not contribute much to interruptions to plant operations.
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ABSTRACT
                                                                                                    ~
A review of the operating experience- of the Haddam Neck nuclear power plant was performed for the Nuclear Regulatory Commission's Inte-grated Safety Assessment Program (ISAP) by the Nuclear Operations An-alysis Center. The operating history of the plant from 1967 through 1984 was reviewed and atalyzed.        The findings of the review identified tre'nds and symptoms in the operating data that can be used as toois in the resolution and prioritization of the Haddam Neck ISAP issues.
The review includes evaluation of data collected on plant avail-ability and capacity factors, forced shutdowns, power reductions, re-portable events (reportable occurrence, licensee event reports, etc.),
and environmental considerations.          The methodology used is also dis-cussed. Data and information is presented in appendices.
It was concluded that the operating history shows the Haddam Neck Plant have generally been operated in a. safe and orderly manner, with trends that show continuous improvement.        Perturbations to these trends were correlated to theorized causes:          (1) an extensive turbine refit, (2) post-effects of an extended operating run, and (3) effects of efforts applied in response to TMI.          Three specific symptoms of con-tinuing saiety related problems were identified through:        (1) recurrence of loss of offsite power events, (2) control rod drive failures, and (3)
I charging pump failures.
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: 1. INTRODUCTION In the early 1980's the Nuclear Regulatory Commission (NRC) imple-mented a program of reviews of older operating commercial nuclear power plants. This program, called the Systematic Evaluation Program (SEP),
grew out of a concern that some older plants were licensed under regula-tions that may have been less stringent than those in existence today.
Specifically, SEP accomplished five objectives:
: 1. The program established documentation showing how, for each operat-ing plant reviewed, the plant specific criteria compare with cur-rent  criteria  on significant    safety issues,  and  provided a rationale for acceptable departures from these criteria.
: 2. The program provided the capability to make integrated and balanced decisions with respect to any required backficting.
: 3. The program was structured for early identification and resolution of any significant deficiencies.
: 4. The program assessed the safety adequacy of the design and opera-tion of currently licensed nuclear power plants.
: 5. The program used available resources efficiantly and minimized re-quirements for additional resources by NRC Jr industry.
Through SEP, the NRC recognized a need to provide order and effi-ciency in the implementation and resolution of regulatory requirements for operating nuclear plants. The experience gained from both SEP and the Interim Reliability Evaluation Program (IREP) enabled the NRC to develop a new and integrated approach called the Integrated Safety I
 
Assessment Program (ISAP).                                          In early 1985, the NRC implemented a pilot program for the ISAP which has examined two volunteer plants - Mill-stone 1 and Haddam Neck.
The features of ISAP lie in the integration of many different pro-grams currently applied to the management and regulation of operating nuclear plants.                  Through an integrated evaluation of these programs, ISAP will enable a balanced and cost effective approach to the manage-a ment of regulatory requirements on a specific basis for individual oper-ating plants.                    Evaluation tools for ISAP will typically include:
(1) the deterministic reviews of all pending licensing actions and safety issues; (2) a plant specific Probabilistic Safety Analysis (PSA);
and (3) an evaluation of plant operating experience.
In SEP it was found that plant Operating Experience Reviews contri-buted significant value to the program.                                            These reviews compiled and evaluated data on availability / capacity factors, forced shutdowns and i
reportable occurrences.                                    They provided additional perspective for the integrated assessment of the plant, and it was recognized that their contributions were equally as significant as those made by safety topic evaluations and risk analyses.
l Thus, operating experience reviews have been included as an in-tegral part of the ISAP evaluation process and are used to (1) confirm the adequacy of the data used in the plant specific PSA, and (2) high-light strengths and weaknesses in plant operation and maintenance which could be considered as factors for judging the adequacy of any proposed corrective actions to resolve an issue.
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                                                                                    ^.
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The NRC contracted with the Nuclear Operations Analysis Center, of the Oak Ridge National Laboratory, to perform the operating experience reviews for ISAP. This report presents the results of the operating ex-perience review of the Haddam Neck Nuclear Plant, and updates an earlier report published under the Systematic Evaluation Program, NUREG-0826,
              " Integrated Plant Safety Assessment, Systematic Evaluation Program -
Haddam Neck Plant." The review includes evaluation of data collected on availability and capacity factors, forced shutdowns, forced power reduc-tions, reportable events, environmental events, and radiological release events.
Section 2 of this report contains a brief description of the methodology employed in the review.              The technical approach is de-scribed, including identification of information sources, data collec-tion techniques, and data review procedures.
Section 3 contains the evaluations of the data.
Section 4 contains the conclusions derived from the evaluations of the data.
Appendices A and B contain the data presented both in tabular form with coded data, and in narrative form containing brief descriptions of I
!            event data as yearly sununaries.
3
: 2. REVIEW METHODOLOGY The objective of the review is to provide insights into the actual strengths and weaknesses of the design, operation and maintenance of the Haddam Neck plant.                            The results of the review will be used with other ISAP tasks, in an integrated approach to establish a manageable regula-tory baseline. From this baseline a plant specific "living schedule" of plant mdifications can be generated.
The evaluation of the operational histor? consisted of a four-step                  -
procets:                          (1) compiling information on plant operating events, including forced shutdowns and reportable occurrences, (2) screening the events to determine their significance, using selected criteria and guidelines (3) evaluating and categorizing events to facilitate a search for trends or symptoms in operating characteristics, and (4) preparing findings based on any observed trends or patterns identified in the data.
Data was compiled on the following tspects of operation:        avail-ability and capacity factors, events of environmental importance includ-ing radioactivity releases, forced shutdown and power reduction events, and reportable events.
The focus of this evaluation was on forced shutdowns and power re-ductions, and on reportable events.                        Availability and capacity factors, and information about environmental events are used to establish an overall perspective on plant operations.                        Procedures ,that assured con-sistency in the review were applied to the screening and categorizing of the information about these events.                    Af ter the screening and categoriz-ing, a safety significance assessment of the events was made , and the existence of any determinable trends or relationships was established.
                                                                    +
 
v 21 Availability and Capacity Factors Both reactor and unit availability factors were collected for      '.1 years of operation through 1984. Starting with 1974, the unit capacity factors, using the Design Electrical Rating (DER) in net megawatts (electric), and the Maximum Dependable Capacity (MDC) in net megawatts (electric), were compiled as well.      Data on capacity factors was not    -
available for earlier years.
Two availability and two capacity factors used in this report are defined as follows:
: 1. Reactor Availability =
hours reactor critical + reactor reserve shutdown hours 100 period hours
: 2. Unic Availability =
hours generator on line + unit reserve shutdown hours 100 period hours
: 3. DER Unit Capacity = not electrical enerEY Eenerated      100 period hours    DER not e ec r ca energy generated
: 4. MDC Unit Capacity = ne                                  100 period hours  MDC net The term " reactor reserve shutdown hours" represents the length of time the reactor is not critical (e.g. , the unit is shutdown for administra-tive or other similar reasons) when operation could have been contin-ued. The term " period hours" represent the total number of hours of the period under consideration.
!                                              (
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a              O 2.2 Environmental Events Significant or recurring environmental problems were summarized based on the review of forced shutdowns, power reductions, reportable events (environmental LERs), and other operating reports.                                  Routine ra-dioactivity releases were tabulated.                            Those releases where established limits were exceeded were reviewed in more detail.
2.3 Forced Shutdowns and Power Reductions Data on forced shutdown and power reduction events were collected and reviewed. Forced shutdowns are generally caused by equipment fail-ures or human errors that result in abnormal challenges to the unit 's operation. Power reductions in general result from some need for main-tenance or operations upgrade which does not require a full shutdown.
The power reductions and forced shutdowns are included in chronological sequence in Appendix A.
Each shutdown or power reduction was placed in one of two sets of significance categories.      The shutdown and power reductions were first evaluated against criteria for Design Basis Events (DBEs) delineated in Chap. 15 of the Standard Revisu Plan.2                            If the shutdown or power reduc-tion could not be categorized as a DBE initiator, then it was placed in one of the Nuclear Operations Analysis Center (NOAC) categories.                                    The l
l method of assigning significance to and the coding of events is des-
! cribed in more detail in Appendix A.
b
              ,            . - . _ . . - - _ _ , . - ~ _ _ . + .            _ _ - _ _ . _  .-__ ._        _-.__m  . . , _ _ . _  ,_
 
2.4  Reportable Events Information on operating events was collected from Licensee Event    ,
Reports (LERs) and LER predecessors (e.g., Abnormal Occurrence Reports (AORs), unusual event reports , and Reportable Occurrences (R0s)] .          This information was retrieved from the NOAC operational data files.              Any documents that contained LER-type information (such as equipment fail-ures or abnormal events) were coded so that they could be reviewed in the same manner as an LER. Primarily, this involved various types of operating reports and general correspondence for the early 1970s. Other 3
sources of information such as the NucIsar Safety Journal          and reports from the NRC Office for Analysis and Evaluation of Operational Data were also used.
Two sets of criteria, originally established in the SEP reviews, were used in determination of the significance of reportable events.
The first set addresses those events whose results include chal-1enges to the safety protection features of the plant. These events are termed " safety significant," and satisfy one or more of the following criteria:
Two or more failures occur in redundant systems during the same event
          -  Two or more failures due to a common cause occur during the same event
          -  Three or more failures occur during the same event
          -  Component failures occur that would have easily escaped detection by testing or examination
                                        'I
 
-    An event proceeds in a way significantly different from what would be expected
-    An event or operating condition occurs that is not enveloped by the plant design bases
-    An event occurs that could have been a greater threat to plant safety with (1) different plant conditions, (2) the advent of another credible occurrence, or (3) a different progression of occurrences
  -    Administrative, procedural, or operational errors are committed that resulted from a fundamental misunderstanding of plant per-formance or safety requirements Other The second set addresses events that have the potential to challenge the safety protection features of the plant.                These events, which might re-quire additional information or evaluation to determine their full im-plication, were termed " conditionally significant," and satisfy one or more of the following criteria:
    -  A single f ailure occurs in a nonredundant system
    -  Two apparently unrelated failures occur during the same event
    -  A problem results in a offsite radiation release or exposure to personnel
    -  A design or manufacturing deficiency is identified as the cause of                  i a failure or potential failure A problem results in a long ourage or major equipment damage T
 
An engineering safety feature actuation occurs during an event A particular occurrence is recognized as having a significant re-currence rate Other The methods for assigning significance to and for the coding of events are described in detail in Appendix B.
2.5 Evaluation of Operating Experience    -
The operating history of the plant was evaluated based on a review that involved screening, compiling, and categorizing data.        Judgments and conclusions were made regarding safety problems, operations, trends (recurring problems), or potential safety concerns.        Events were an-alyzed to determine their safety significance from the information pro-vided through the various operating reports and the review process. The Final Safety Analysis Report (FSAR) and conversations with plant person-nel provided specific plant and equipment details where necessary.
a l
i l
 
                                                                            . e
: 3. OPERATING EXPERIENCE REVIEW EVALUATION 31 General Plant Description The Haddam Neck Plant (also called Connecticut Yankee Nuclear Power Station) is a Westinghouse Electric Corporation pressurized water reac-tor plant of 582 W(e) net maximum dependable capacity (1,825 megawatts-thermal (MWt)] (Fig. 3.1). The licensee and operator of the plant is Northeast Utilities, which is a company formed by three of the eleven partners comprising the Yankee Atomic Power Company that originally built the plant. Stone and Webster was the architect-engineer and also the constructor of the plant.
The plant is located on the Connecticut River about twenty-one miles south of Hartford, Connecticut.        A " Facility Description and Safety Analysis Report" was submitted to the AEC on July 19, 1966, and the interim facility license, DPR-61, was issued on June 30, 1967. On December 31, 1969, the licensee applied for a Full Term Operating Li-conse, which was granted by the NRC on December 27, 1974.
32 Evaluation Findings The operational history data was evaluated as described in Sect. 2,
" Review Methodology". After the data was categorized, coded, and screened, searches were conducted to identify trends and symptoms or any other patterns in operating characteristics.      The findings from these evaluations are set forth below, and are presented in the following order:
: 1)  Availability and capacity factors
: 2)  Forced shutdowns and power reductions 10
 
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                                  /.                                                .-
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                                                                  .,                    .s                                    .-
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lf, O. /                  .
a
                                                                                                                                                                                                              ~
w                                      ;
3 II
 
o                      e
: 3)    Reportable events, including events of environmental importance and radioactivity releases.                                                                -
3.3 Availability and Capacity Factors The plant availability and capacity factors are shown for each year of operation through 1984 in Table 3.1 and on Fig. 3.2.                                                                                  Unit availabil-ity was good for all years except 1967, the first year of operation, and 1973, when extensive repairs to the turbine were performed. The cumula-tive unit availability (82.5%) was well above the industry average of
.                                                  63.0% at 1984 years end.
i 3.4 Forced Shutdowns and Power Reductions The Haddam Neck Plant experienced a total of 181 forces shutdowns and reported 64 power reductions from the start of operations in 1967 through 1984.                  Figures 3.3 and 3.4 present in graphic format the yearly i                                                  totals of forced shutdowns and the yearly totals of power reductions re-spectively.
t 3.4.1    Systems Involved in Forced Shutdowns and Power Reductions The majority of forced shutdowns over the operating history of the plant occurred principally in three groups of systems:                                                                                    steam and power i
conversion systems, electrical power systems and instrumentation and controls systems.                              Tables 3.2 and 3.3 summarize the systems involved in the forced shutdowns and the power reductions, respectively.                                                                                        Figure 3.5 displays steam and power system shutdowns, and                                                                            Fig. 3.6 displays elec-l trical power systems shutdowns.
I
(
i l.
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                        .. . - . ~ .
WP ,
Table 3.1. Availability and capacity f actors for Haddas Neck 1967  1968 1969 1970  1971  1972    1973  1974  1975    1976  1977  1978  1979 1980 1981 1982 1983 1984 Cumulatt Reactor availability            87.6    90.7 94.4 80.8  89.5  90.8    58.1  96.2  88.7    87.3  87.2    98.4  89.2 77.1 86.5 99.4 79.3 74.2  86.5 Outt availability              44.3    78.7 86.5 78.7  86.6  87.7    50.5  91.2  86.1    82.5  83.9    98.2  87.5 75.0 84.3 93.4 77.8 71.7  82.2 Unit capacity (tsc)(a              ND 8  ND  ND  ND    ND    ND    48.1  92.0  87.9    83.4  83.3    97.7  85.4 73.1 83.2 93.1 75.9 67.3  81.9d past capacity (DEk)b              ND    ND  ND  ND    ND    ND    44.3  84.8  82.6    79.8  79.7    93.5  81.7 69.9 79.9 89.0 74.2 65.8  76.Sd
      # MIC = Haminima dependable capacity.
bbER = Design electrical rating.
      #ND = No data available.
JCalculated with a weighted average.
* 2 S'k i
6
 
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s  t I                                                    AVAILABILITY AND CAPACITY FACTORS 100-A s      ***
aA r:
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sp 80_
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                                                //1 s T -1
 
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                  .s      . e          .      . ,      . .                                                                                                              . . ..                                                                    ,              .            ...
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2 2                                            . .
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                =                                  .        .                                                                                                  .                                                                                .          .
1 t
2              .              .                                                                                                                                                                                                  .
a S              .
    -.      1 n    :                            .                              n                                                                                                                                                            . .              .
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l              c 2              .                  .
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              =
2                            .                            .                                                                                                                                                                    .                                      .
s-l                      .                    . .                                                                                                                                                                                                .          .                .
l I
1                              .            . .                          .                                                                                                                                                                    .          . .              .
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                                                  * '          s                                                                                                                                                                            1                          .
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l g!    3-*2-
                                          -                                                          .                                                                          t                                                                                                        2 8 .1                                                                                                                                                                                                  3 if
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                            - .6 3 s-a .2      .31s.s ye    1.s :[2  : !
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i LsL L                                                                                                                          I
 
e
(
i Table 3 3. Feuer reductlene sammeery for unddam leeck 1967                  8%8 IM9 1970  8978    1972    1971    1974  1975      1976    1977 4978  1979 1980 1981 1982  8983 1984 Totale
: 1.          Power reJactions
: 1. Total number                  1                    5  8    5      8      9      $                                    2      S    3    3    8      I    I    64
: 2. Cause A. Elecis ic power (EA)                                                                                                  i                2    7          8    IS
: s. nelatenance or testine    1                    5  8    5      8      9      5                                    I      S    3    I    I      I        S3
: 3. system involved A. Elect ric power (EA)                            2  8    1      5                                                                                            32 B. Electric power (ES)                                            5                                                                                              I
      -                        C. Reactor (Cs)                                            2      I                                                            I        I                      $
seg                        D. Steam anJ Power Con-version (HJ) 4                              E. Turblue generator (HA)    8                                                                                                I              I                  3 F. m in steam supply (HB)                                          1                                                    I      2    8        8                  6 G. Main condensers (HC)                                    3      3      5      8                                                2    I    6                39 H. Cisculating water                                                              8                                                                              I system (HF)
: 3. ConJeumate and feeJ-                            2      1      1      4      3                                    I      I                              B3 water (HH)
                                .l . Nin stema system and controls (CC)
K. Reactus (kB)                                    1
: 5. . Caeeous radioactive                                                                                                                  3                      I waste (MR)
: 4. Total ns I,=r uf DBE related                                                                                                                                      6 power reJus tous (lac tuJeJ la totals in Part 1) if
 
YEARLY TOTALS OF FORCED SHUTDOWNS 30, 1
24,,
H      19 U 18, 12                                  11        11 9                              8
:            llliilliillY 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84
,                        YEAR OF OPERATION FIGURE 3.3 l
l 1
l lb l
 
INTERPRETED FORCED SHUTDOWN RATE
        .          30.
PROJECTED RNIE 24 S
H  IfL U
T                                ANOMALOUS PERTURBATIONS D
0  12                          A                  ,3 W
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                        .                  YEAR OF OPERATION FIGURE 3.3A 17
 
o YEARLY TOTALS OP POWER REDUCTIONS 10, 8_                                                8 H
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0                          0 0 0 0 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.4 i$
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l INTER!RETED PCIER REDUCTION RATE 10 _ ,
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      . 1 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.5
                                  '?. D
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INTERPRETED SHUTDOWN RATE WITH STEAM AND POWER SYSTEMS AS CAUSE 20 _
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PROJECTED RATE 3
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SHUTDOWNS CAUSED BY ELECTRIC POWER SYSTEMS 10_ .
9 8_
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67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.6 11 O
 
3.4.1 1  Steam and power systems. Two-thirds (66%) of the total downtime reported by Haddam Neck resulted from problems with the steam and power conversion group of systems. Ninety-nine forced shutdowns re-sulted from problems with these systems (Fig. 3.5).      Plant systems in-cluded in this group were turbine-generator system, condensers, steam generators, and feedwater systems. Most troublesome of these was the turbine generator system. In the first three years, problems with the turbine alone caused 1574 h downtime during 24 forced shutdowns.      From 1970 to 1973 this race fell to only ten outages involving turbine fail-
        . ures. In June 1973, the reactor shut down twice for a total of 4194 h to replace turbine blades. Again more blades were replaced in a March 1974 outage (660 h). Other periodic outages (6) occurring from 1975-1980 were for turbine balancing only. Overall, problems with the tur-bine generator and its controls accounted for 7533 h of downtime, over half of all outage time at Haddam Neck. The 56 outages for the turbine generator averaged over 120 h each, while the average outage for all other systems in the plant was about 60 h.
The condensers at Haddam Neck also caused some significant outage time. Fourteen forced shutdowns were required to plug tubes in the con-densers totaling 210 h.      Ten of these shutdowns occurred from 1970 l
through 1972.
The condensate and feedwater systems caused 720 h of outage in 22 shutdowns. Most shutdowns resulted from repairs to the steam generators and their feed pumps. Feedwater regulating valves also required minor l          repairs and adjustments. Since loss of feedwater control is classified as a DBE initiating event , these failures are discussed in more detail in Sect. 3.14.4.
l 13 l
5
 
3.4.1.2  Electrical Power Systems.                    The outages due to problems in the electrical power systems were generally short in duration.                                    Most shutdowns involved maintenance on the offsite transmission lines, and repairs to vital bus equipment.                      Problems in the electrical power sys-tems were the cause of 29 forced shutdowns at Haddam Neck (Fig. 3.6),
resulting in 648 h downtime.
The most significant shutdowns, from a safety point of view, re-l sulted from faults in the protective relaying which isolates the plant from offsite power.        These events resulted in seven reportable events which were classified as significant. They are discussed in more detail in Sect. 3.14.1.
3.4.1.3  Instrumentation and Controls.                            Problems with the instru-mentation and controls systems caused 24 shutdowns at Haddam Neck total-ing 332 h downtime.        Most of these outages occurring in early years of operation were caused by spurious scrans for unknown reasons.                                Thirteen shutdowns caused by instrumentation and controls systems problems re-sulted in reportable events, and according by additional consideration was given to them in the reportable event reviews (see Sect. 3 9.4).
3.5 Causes of Forced Shutdowns and Power Reductions Tables 3 2 and 3.3 summarize the causes of forced shutdowns and power reductions, respectively.                        Of the 12,681 h total downtime at Haddam Neck, 79% (9966 h) was caused by maintenance and testing (Fig.
3.7). As discussed previously, the primary cause of plant shutdowns was maintenance and testing.        The majority of shutdowns due to this cause were experienced as results of problems in the turbine generator, the M
f
                        ---      r
 
y
* U S  e SHUTDOWNS DUE TO MAINTENANCE AND TESTING 20_
16,    16 S
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0 W  8_
N S                6    6                6 4_                4 si              2 2 0                    I  5      0                  0 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.7
                                        '5
: i.  .
feedwater aystems, and the offsite power systems. Maintenance and test-ing accounted for seventy-nine percent of the total downtime.            The second largest cause of shutdowns or power. reductions was equipment failure. Seventeen percent of the downtime was attributed to equipment failure (2193).
The Haddam Neck Plant shut down twice (300 h total) for regulatory restrictions. On June 17, 1978, the plant shut down for 66 h to install heat shrunk sleeves on electric penetrations as requested by the NRC.
On September 29, 1979, the plant shut down for 234 h to inspect welds on the steam generator feed lines, also at the NRC's request.
There were 51 forced shutdowns which resulted in an LER.        These events were furthered revie,wed as reportable events (Sect. 3.8).          A total of 35 of these 51, or 65%, occurred in the first 3 years of opera-tions.
1 3.6 Non-DBE Shutdowns Table 3.4 summarizes the NSIC categories assigned to non-DBE shut-downs. Only the major categories are listed in this table.      Equipment failure accounted for 85% of the non-DBE shutdowns.      For the early oper-ating years (1968-1973), equipment failures were responsible for 93% of              )
l the shutdowns or power reductions.          All other NSIC categories con-l tributed to less than 5% of the non-DBE shutdowns.      No discernible time trends appeared in the compilation of non-DBE shutdowns.
3.7  DBE Initiated Shutdowns Of the total of forced shutdowns and powe      re etions reviewed for Haddam Neck,    thirty-five were identified as Doc initiated events 15
 
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DBE INITIATED SHUTDOWNS i                  6. 0, 5 5 4.8_
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T                                                                                                  '
l    l D                                              3                                      l 0                                            !                                        I l W    2.4 l3 4
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__    _ 0.0                0            0                    0 0                      l                      0 0 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.8 l
3
 
(Fig. 3.8). None of these events initiated any sequence that led to a significant safety hazard at the plant.      Table 3 5 lists the number of f
DBE initiating events at Haddam Neck for each year reviewed.      There are no discernible time trends in the number of DBE initiating events oc-curring at Haddam Neck. The following sections present a brief discus-sion of those shutdowns which were categorized as DBE initiating events.
3.7.1  D1.2 - Feedwater system malfunctions that resulted in an increase in feedwater flow only 2 of 35 DBE initiating events fell into this category.        In both instances, feedwater regulating control was lost and the water level rose in the steam generators.
On June 10, 1969, a broken feedwater regulating valve plug caused loss of control of feedwater and subsequent flooding of the No. 3 steam generator. The plug had dropped open allowing full feedwater flow to steam generator No. 3.    (See Sect. 3.14.4 for further details.)
On February 22, 1973, the connector between the No. 2 feedwater i
control valve stem and actuator loosened, permitting the valve to go fully open. This resulted in an uncontrolled increase in the No. 2 l
l    steam generator level.      No serious transient resulted from this DBE initiating event.
3.7.2  D2.2 - Loss of external electric load i
On December  3,  1977, a generator voltage regulator malfuaction caused the plant to shut down for 7 h.
3.7.3    D2.3 - Turbine trips.      Out of a total of 35 DBE initiating events, 21 were attributed to turbine trips (Fig. 3.9) .      These outages resulting from turbine trips were all relatively short.      Only 525 h of downtime accunulated from all the turbine trip outages.
                                          $0 l
l
 
    , _c_  _ _
SHUTDOWNS DUE TO TURBINE TRIPS 5_
4_                              .
H U
          '    3-            3 0                  ll y                  ::
N    2_            !j            2                        2  ,
l S
jj                                      l 1        1          .
1 p                                    p f  '
0        ii  !!!      0 0      0 0      0 il 0 0      '
OO 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.9 I
 
Six of the category D2.3 events were caused by failures of the tur-bine stop valves. On August 2,  1968, both turbine stop valves closed during a test of the lef t hand stop valve, tripping the turbine and then the reactor. A week later, on August 9,    the right hand stop valve closed following a planned closure of the left hand stop valve.        The first trip was caused by a stuck-open check valve in the oil discharge line from the right hand valve.      This caused oil from the left hand valve to drain through the right side, resulting in a closure of both valves. The plant was shut down to repair the valves. On August 5, the plant returned to service until August 9, when the right hand valve in-advertently closed following closure of the lef t hand valve. Failure of the right hand valve was attributed to loss of oil pressure in the valve auto-stop system.
On January 8 and March 29, 1969, problems with the right hand stop valve resurfaced. The first failure resulted from leaking oil in the auto-stop system. The second trip was due to failure of servo-motor cup valve. On July 14, 1975 the auto stop oil system began leaking, forcing
                    .                        the reactor down for three hours.
Additional turbine trips were caused by a variety of reasons. The l                                              turbine tripped three times on overspeed (August 2 and November 20, l
1980, and December 11, 1981).      The turbine governor system malfunc-tioned, tripping the reactor on two occasions (November 11 and 12,
!                                              1969). Maintenance errors during wiring modifications caused the tur-bine to trip on March 27, 1980. Oa March 28, 1968, the turbine tripped on an inadvertent activation of the turbine low vacuum trip signal. On July 5,  1975, the turbine tripped due to a broken oil pressure gauge
                                                              ~
3L
* t
                                                                                                    --      -  -r          ---  ,- -
                                                                                                                                        --r
 
line on the turbine. A constant voltage transformer failed causing a turbine trip to occur on September 21, 1972.          Repairs on the unit re-quired the plant to shut down for 85 h.        All of these turbine trips re-suited in relatively minor consequences and short outages.
On July 29, 1981, while reducing load, a turbine and reactor trip occurred due to a low pressure steam dump malfunction caused by OPC relay 63. While reducing power on December 11 to plug the B waterbox J                    condenser tubes and for scheduled turbine maintenance, erratic operation of the turbine control valves caused a turbine trip due to overspeed.
On December 22, 1981, a turbice and reactor trip occurred due to high pressure heater drain-tank level due to a failed fitting on control air system.
In 1982 there were two occurrences of a turbine trip.                                    On January 31, six blown fuses resulted in the loss of the generator field, causing the turbine to trip. It was determined tha't the fuses had blown as a l                    result of short circuits in the exciter.            Investigation showed that i
shims used for leveling inside the exciter casing had partially sheared l
off and th'at the excess metal had been blown into the wiring by the cooling fans, causing shorting between circuits. The shims were trimmed to prevent reoccurrence.
3.7.4  D2.6 - Coincident loss of onsite and offsite AC power to the station On April 27, 1968, a switching error activated a transfer trip re-lay, causing site feeder breakers to open.          This action isolated the plant from offsite power.          The reactor subsequently tripped and the three diesel generators started but failed to load. Thus, the plant was N
4
  -,y, ,,w,--,..,.    ,                          ,_                      - - - - - - - - - _ _ _ _ - _ _ _ _ _ _ - - -
 
without AC power for a brief period of time (25 min.) .        The resulting outage lasted only nine hours; however, the plant returned to full power without thoroughly testing the AC power system, a breach of regulatory specifications. Due to the safety implications of a total station blackout, this event is discussed in further detail as a reportable event, in Sect. 3 14.1.
3.7.5  D2.7 - Loss of normal feedwater flow Seven loss-of-normal-feedwater events occurred over the period of the operating history review.        Five of the seven failures involved loss of feedwater control.
On August 23, 1968, a feedwater regulating valve failed closed due to loss of control air.        The shutdown lasted less than two hours. A loss of feedwater control to steam generator No. 4 resulted from the failure of a solenoid on August 21, 1971. The solenoid was replaced and the unit returned to service in four hours.          No cause was found for failure of the solenoid.        On September 7, 1971, a momentary ground of a vital bus resulted in loss of control of feedwater to one of the four steam generator feedwater solenoids. Again, no specific cause was found for failure of the solenoid.        On February 1,1975, the plant shut down for 16 h to remedy low feed pump suction pressure. On February 29, 1981 l
the separation of a fitting on the control air header caused the loss of feedwater control. Low feed pump suction pressure was again the cause of a feedwater trip on November 8' 1982. The plant was returned to ser-vice af ter system components were verified to be operating properly.
i
 
  . o 3.7.6        D3.1 - Single and multiple reactor coolant pump trips Only one reactor coolant pump trip was experienced during the pe-riod under review. On September 10, 1976, a coolant pump shut down as a result of an operator error. The plant was shut down for seven hours.
3.7.7        D4.3 - Control rod maloperation on November 18, 1980, Haddam Neck experienced problems with two rod gripper coils, resulting in two dropped rods.          The plant shut down for 14 h to replace the coils.        Several control rod drive failures occurred; however, none caused serious problems.        Another occurrence of r'od drop was experienced on November 17, 1982.        The bank "C" rods dropped during rod motion checks for an undetermined cause.          Control rod drive anom-alles are discussed in more detail in Sect. 396 in the reportable events discussion.
38 Reportable Events A total of 342 reportable events that occurred at the Haddam Neck l    plant from the beginning of operations in 1967 through 1984 were re-l viewed.        Figure 3.10 presents in graphic format the yearly totals of re-portable events.
3.9 Systems Involved In Reportable Events A compilation of all reportable events by system and year is pre-l    sented in Table 3.6.        The systems listed in this table represent groups l
of systems related by function.        Systems which had no reports filed are omitted.        Most reportable events involved the following systems:    reac-tor coolant, electrical power, steam and power, instrumentation and con-trol, chemical and volume control, reactivity control, and engineered N
1 l          _ _ _ .
 
O 4 YEARLY TOTALS OF REPORTABLE EVENTS i
40_ ,
!                                                              31 32_
  ! 24,        D 23 i
16      16 11      11 E              i t                          i 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.10 t
 
Table 3.6                    Summary of systems involved in reportable events at fladdas Necit 1976  1977    1978  1979 1980 1981 1982  1983  1984  Total 1967 1968  1969                  1970    1971  1972  1973    1974    1975 System I    I    I    I    2            22 2        1 kerctor                                                                                    1  4      6                    2                                                                                      4    3      39 I      3      2      2        3    3    3    2 i  2                            5      3            2                                                                              60 ke.sctor cool.snt                                                                                                                                                        4      9        3    I        I    I    2    6 Instrinsentation an.1 controls                                                            7    9      4                      5      1      I      2      4 4    2    6    3      53 4              4      1        3    2    2 6                                    2      3 t:lec t r ic powei                                                                          7  3                                    1 2            3      2        6    2    5    6    3    9  to      56 I            3      3              1 Engineered safety teatures                                                                                                                                                      I        1 1      3 Fuel lianJilng .uul stos.sge                                                                                                                                                                        2                3    1      10
                                                                                                                                                    !        I    I      2              1    A Auxiliary water                                                                                                                                                                                    2    4    3    2    4      72 2      3      I      I      7    to      16    2 Ste.a ai:1 power                                                                            1  5      7                      2                                                                                                    C 2        1          1 Radiation protec tion                                                                                                                                                                    2          6    2          1          19 3      2              1 kaJioactive w.a s te m.au .sgemen t                                                                    2                                                                                            4    2          7            41 3      2            2      6      4    5                1 1    2                              1      1
                                                                                                                                                                                                            !              10      10 Auntliary process                                                                                                                                                                              i    !
I                                                                                            2      6 O t tier atuzillery systeins 1                    I                    i        1 No ayutem applicatale 41    21  27  24    11    36  40      400 6    9    18      15      6    28    37 Total                                                                      17  24    27                    16 s.1 J
l
 
O    O safety features. Problems with these various systems are discussed as follows.
391 Reactor Coolant System TM designation of reactor coolant system encompasses a broad range of heat transfer related equipment in the reactor.        This includes the reactor coolant pumps, pressurizers, relief valves, and support struc-tures for equipment in all four main cooling loops.
!            Reactor coolant pump (RCP) seal failures occurred three times at the plant (AO's 70-05, 77-19, 80-12). All of the failures affected only one of four reactor coolant pumps and the first two are considered sig-nificant (see Section 3 14.6).
Three inadvertent openings of the pressurizer PORV occurred at Haddam Neck. On August 13, 1979 (LER 79-10) a PORV and its isolation valve failed open due to failure of a bistable in the pressurizer pres-sure controller. Reactor pressure dropped from 2000 to 1950 psig. The signal was overridden.      This action closed both valves and prevented further    depressurization. This  event    is discussed        further    in Sect. 3.14.7. On February 4,  1980 the same valves opened again (LER 80-04). The PORV was open for about 2 min before it was manually closed. No cause was reported for the second event. On April 3,1981, l      the pressurizer relief and blocking valves opened due to a loose elec-trical connection (LER 81-03).
Control of the pressurizer spray valves and the PORV's was lost twice during 1983 due to the loss of containment control air. On Novem-ber 1 the containment control air was lost due to a maintenance error on 4
a filter (LER 33-20) . The filter was isolated and repaired.          Control P
 
9 - v e  O air was again lost on November 28 due to a broken air filter canister (LER 83-21). In both events, control air pressure was restored in less than one hour.
On August 19, 1970, a small fire was discovered and extinguished at the juncture of an RCP and the suction piping ( AO 70-08). Reactor power was reduced to 65% so that personnel could enter the loop areas to make repairs. Oil had dripped from the thermocouple conduit attached to the motor thrust bearing. The dripping oil contacted the 520'F coolant pipe and vaporized. As the v'apor emerged from the insulation around the pipe
                'it ignited. All insulation from the pump outlet to the center of the stop valve was replaced and the oil leak was stopped with epoxy.      (For further details , see Sect. 3.14.6).
3.9.2    Electrical Power System Fifty-three failures were reported for the electrical power sys-tems. Systems included in this designation are AC onsite power, offsite power, and energency generators.      Failures of the onsite AC power ac-counted for fourteen reportable events over the operating history of Haddam Neck. Eight of these events involved reactor trips due to fail-l                ure of the AC vital bus, five of which occurred in the first five months l                of operation.      Component failure was responsible for two of . the eight bus failures.      The remaining failures were caused by workers inadver-tently grounding the bus during maintenance. The bus and related equip-ment were replaced several times, the failures then ceased af ter 1968.
Seven loses of offsite power also occurred at Haddam Neck. These fail-ures are discussed further in Sect. 3.14.1.
73
 
3.9 3 Steam and Power System Most failures in the steam and power conversion systems were attri-buted to problems with the steam generators (HB system).                    Four failures of the steam generators were due to failures of hold down bolts and seismic supports.                  In all instances no cause was reported and the sup-ports were replaced.
Four leaks were reported at the junction of' the waste liquid steam generator blowdown discharge piping and the service water effluent line. The leaks were all caused by a rapid deterioration of the piping material where the hot blowdown water contacted the relatively cold ser-vice water effluent.                    In each of the first two failures (A0 76-13, A0 77-01) a small amount of tritium was releared, well below the allowable limits.      The leak recurred !n March 1978 (LER 78-03) and again in February 1980 (LER 80-07).                    Small amounts of tritium were released in the 1980 leakage.                    In each instance, the affected areas were replaced.
Repetitive failure of the piping is attributed to corrosion due to ther-mal shock.
Six reportable events occurred due to main steam isolation valve (MSIV) failures.
Four of the failures were caused by binding of the l valve gland packing.                    In each case the packing was adj usted and the valves operated satisfactorily. The fif th MSIV failure occurred on June 6, 1982 (LER 82-04).                    This valve failed to cycle during a shutdown due to a warped tail link.                  It was concluded that the tail link was damaged by a jacking device used during corrective maintenance in the September-November 1981 outage.                    The final MSIV failure occurred on August 23 ,
1984 (LER 84-16).                    An isolation valve in the main steam drain line i
bT 4 J
 
  ,        e failed to close during a test.        During subsequent maintenance of the valve, it was discovered that the valve suffered from a bent stem.        No cause for the damaged stem was determined.      The valve was repaired and ratested satisfactorily.
3.9.4  Instrumentation and Controls The instrumentation and controls system was responsille for 60 re-portable events at Haddam Neck.      This high number of events is due to the function of the system as a safeguard for more serious occur-rences. Twenty-six of the events resulted in reactor trips. The causes of the reactor trips are split evenly between equipment malfunction (9 events), maintenance or operator error (8 events), and unknot.n causes (9 events). Most of the reactor trips (21 events) occurred during the first four years of the plant operation.
Two of the events that involved the instrumentation and controls system were classified significant to safety.      The first event occurred l
l
'              on October 12, 1970 (A0 70-09).      A reactor trip occurred due to an er-roneous loss of flow signal.      Following the reactor trip, one of the steam dump valves failed to close due to the valve positioner being out of adj ustment. The second event occurred on August 25, 1978 (LER 78-18). An FM transceiver caused a rod drop alarm.      Following the rod drop alarm, the turbine load runback alarm failed to initiate due to a closed pressure switch isolation valve.        The isolation valve disabled the turbine load runback feature.      Further details on these two events can be found in Sects. 3 14.2 and 3.14.10.      On January 18, 1974, ins tru-ment sensing lines froze due to cold weather ( A0 74-02).        The frozen lines caused two main steam line high flow alarms and subsequent reactor
 
                                                                                $    D trip. Plant personnel implemented a number of changes to prevent recur-rence. This event was classified conditionally significant because ac-curate and reliable information from instrumentation is essential for safe plant operation. Frozen sensing lines could produce misleading and erroneous information to an operator.      The remaining failures reported for this system produced no serious consequences.
3.9.5    Chemical and Volume Control System Thirty-six reportable events were caused by failures of the chem-          -
ical and volume control system (CVCS).        Eighteen of the failures re-ported for this system involved leaks while two of the leaks resulted in unplanned releases of radioactive material. 5Act of the events reported on the CVCS were due to failures of the charging pumps.          Since the charging pumps also serve as the high pressure injection pumps, these failures are discussed in greater detail in Sect. 3.16.
On May 3, 1969 the Boron Recovery Distillate tank ruptured due to an improper valve lineup (A0 69-06).          Approximately 200 gallons of radioactive distillate were spilled in the surrounding area. This event was classified significant to plant safety and is discussed further in Sect. 3 14.8.
on July 15 , 1969 all offsite power was lost during switching i
l changes involving the 115 kV supply lines.        Subaequently, one diesel generator failed to start and one charging pump failed to run.      Due to the safety significance of this event, it to discussed in detail in Sect. 3.14.1.
                                        .12.,
* s 3.9 6 ReactC./t              . _ System The reactog                    . system Wa.S involved in 22 of the report-able events that occurred over the operating history of Haddam Neck.
Fifteen of these reports involved failures of the control rod drive                    ,
(CRD) systa.a. Due to the safety implications of problems with the CRD system, these failures are all discussed in more detail in Sect. 3 15.
During the May 1970 refueling outage two radial vanes in a control assembly were found to be cracked.          Each of the radial vanes to which the control rods were attached had broken loose from the hub assembly.
This is discussed in greater depth in Sect. 3.14.10.
: 3. 9. 7 he / bd/MG W!kM -
On August 21,      1984 the reactor cavity seal ring failed (LER 84-13). The failure occurred 18 hours before refueling was scheduled to begin. During the 20 minutes following the seal failure,          200,000 gal-lons of radioactive water drained from the reactor cavity to the lower levels of the containment building.          The original all-metal seal had been replaced with an inadequately
* designed seal that included flexible rubber boots. Although the seal failure did not pose an actual threat to safety, the consequences of the seal failure could have been severe had refueling operations already begun.          The event is discussed in de-tail in Sect. 3.14.12.
3.9,  Engineered Safety Features Systems The engineered safety features (ESF) systems were involved in 56 of the reportable events that occurred at Haddam Neck. The ESF systems in-clude both structural and mechanical equipment which perform both pas-sive and active safety functions.          Included under the ESF designation are the reactor containment structure, containment isolation and control equipment, emergency core cooling system, and other saf ety equipment.
2
 
o Five containment isolation valve failures involved check valves for the Component Cooling Water (CCW) system.        All of the failures occurred during the last four years of the operating history under review.            In each event the check valves failed to seal properly due to rust / scale deposits in the valves.
Failures involving the containment air recirculation system ac-counted for t.lu4 events. Half of the events ' involved the recirculation dampers and their associated control linkage.          Four other events in-volved the service water supply to the fan coolers.          The air recircula-l tion system is needed for heat removal from the containment atmosphere I
during both normal operation and following a loss of coolant incident.
l                              3.10 Causes of Reportable Events Table 3.7 pres _ents a summary of causes of reportable events at Haddam Neck. No causes were reported for several events in 1967-1973.
Over 60% (20t}) of all reportable events at the plant were attributed to incipient failure.      Incipient failures are failures in which only the component itself is held accountable.        This includes set point drifts, wear out, and many failures for which no cause could be determined.
Over the operating experience reviewed, human error was responsible l      for 36% (126) of all reportable events.        Human error can be classified i
into two categories:    (1) in-plant personnel (maintenance, operator, and installation errors), and (2) out-of-plant personnel (administrative, design, and fabrication errors).        In-plant personnel accounted for 65%
of the human errors (82 events) while out-of-plant personnel accounted for 35% (44 events).      The mos t common human error found in the report-able events was naintenance error.
hb
 
Table 3.7    Causes of reportable events for Haddam Neck cause        67          68                    69  70    71    72    73  74  75  76  77  78  79  80  81  82 83 84 Total Adrainis t ra t ive                                      1                      2        I    1        1    1    3  4      1  3    j8 Design                                                        1              ,1    1        2    1    5    2    4  1  1  2  3    24 Fabrication                                                                                        2        1                        3 Inherent failure      9            13                  15    8    4    4      8  9    3  12  24  23  10  11  12  7 19 18  ;209 Installation                                    1                    1          2        1  2    3    3    4    2  1            do Lightning                                                1    l                                                                      A is Maintenance            6                    6            2    1          3    1  1        2    3    2    1    1      1  3  3    36 Operator              1                                  4                1              1    1        5    1    4  3  1    5    27 7
Weather                                                              1              2        3                            1 Unknown            g                        3          1                                                                            4 Total          16            23                  24  11    6      8  14  13    6  23  33  39  20  25 21  10 26 33  350
* Sac Eyty fS lAny'ohsf /H2C YlMN 046 C/ll/Jf.
 
3 11  Events of Environmental Importance Haddam Neck reported 53 events of environmental significance through the 18 years of operating experience.          The reports covered un-planned releases of radioactivity (24 events), excessive doses to work-ers (4 events), fish impingement on intake filter screens (18 events), a high rate of change of the discharge temperature (6 events), and a high discharge canal PR (1 event).
3.12 Radioactive Release Events A summary of radioactivity releaces for Haddam Neck is shown in Table 3.8.      The table lists the airborne and liquid releases and the solid waste ' shipped for the years 1967 to 1984.
Haddam Neck reported 2f unplanned releases of radioactive gases or liquids, shown in Table 3.9.      In addition, a shipment of solid waste was released prior to a health physics review.            Of all releases, solid, liquid, and gaseous, human errors caused 16 of them.            Operator errors caused six releases, administrative caused four,                      installa-C^used IfuttC                            pad MAtaf&avec cwowa' oNF '
tiond    j design errors        caused two.f' In all releases, the workers received less than the maximum permissible dose.
Four events , though not releases, dealt with the overexposure of plant personnol.      In the fourth quarter of 1973, two men had quarterly exposure readings of 3.03 and 3.66 rem.        During the 1975 refueling out-
  . age, a maintenance worker was overexposed while installing a scismic re-straint system. A dosimeter read 2.19 rem exposure while a film badge read an exposure of 3.Il rem.          Another overexposure occurred due to inadequate recording procedures in        F. arch 1979. The final personnel 47
 
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Table 3.9.      Unplanned radioactive releases at Haddam Neck Report    Event Cause                                              Description of release Number    Date A06906    050369                H    Baron recovery tank ruptured due to improper valve lineup, small release resulted.
A06907    050669              D    500 gal rad liquid spilled on baron recovery area, small release resulted.
041871                H    Radioactive iodine released due to operator error with penetration seals. Workers exposed to a release of 700 nC1 1-131.
A01202    051972                N    Unplanned release (1.9 Ci of Xe) from domineraliser due to operator error.
A07306    062173                D    Unplanned airborne release (0.238 C1) due to leak in purification system valve.
A07307    062373                A    Unplanned release of radioactive liquid when letdown system placed in service.
A073tl      110l73              D    Valve on RWST thermosiphon leaked radiontive water through a bad diaphragm.
Leaked into a local storm sewer.
A07407    042674                D    Unplanned radioactive release from auxiliary building exhaust f an due to leak in diaphragm in hydrogen supply regulatory.
1.ER7608  033076                E    Unplanned release of radioactive gas (11.59 C1). Two rupture disks in vaste gas tank failed due to damage during installation.
LER7613    061576                D    Small leak in wall of safety injection cubicle due to deterioration of steam generator blowdown piping.
LER7701    121476              D    Small leak in liquid waste line. Tritium activity in external sump increased.
ETS7708    110477              C    A river effluent monitor sample pump was not operating while 21 tanks were drained.
LER7721    091877              D    Unplanned release'of 7.44 C1 radioactive gas Shen a diaphragm ruptured in a waste M                                  ETS7810    090078              D gas decay tank.
Tritium level in river sample exceeds limit.
EER7906    121679              B    A level control valve relay failed, 15.8 C1 released in 10 minutes via che stack.
LER8003E  042880              D      Unplanned radioactive release occurred when when a desassifier rupture disk flange cracked. Instantaneous rolesse limits were not exceeded.
IER8004E  051980            A      Tritium activity exceeds release limit due to large volume of processing water for upcoming refueling outage.
LER8002E  050480            A      Radioactive release limite exceeded when an ion exchanger was replaced. Cases released were I.7 and 2.6 times the tech spec limits.
1.ER8005E  052880            B      A waste gas system valve opened releasing I.7 C1 of Xenon in etz minutes.
LER800?E  092680            H      An operator opened the wrong valve, 1.3 C1 released via the stack.
LER8013    092680            N        Technician made a sampling error allowing radioactive gas to be released.
Technician received a 9 mres exposure.
1.ER8100S  042283          A        Contaminated tube bundles were released f rom ette ptf or to health physica review.
LER8100E  081681            N        Noble gas release rate exceeded limite due to operator error.
LER8tl5    091781          E        Radioactivity (0.533 oci) released via cracked exhaust duct to stack.
PNo-I-63  090683            D        3.3 C1 of Noble asses released to stack when relief valve on the waste gas surge
                                                                        -95                                  tank lifted.
0 6'76 6 N 2 74        b              % str s4t 4 cay Ysw< Ryfunt ds:rK hs/k OWC
                                                                                                            *to,mccrygg y gg w yg 7pg)
LenA: sN Mcy c/c ht/ dwg rsu fo coxa *od &
AO 77M GM/ f                          vooo y/ sf &po%.we /sa un/d A'C/MOY w ho see /s us fy sd 4"M M/M                            *CN*              O E7~.5 7/d6 fo217/      .D                                        '                                                            ,
                                                                                                            /-s        i/
coyevenAnd.cass/c                              Hn4 44          f*
s~gy.e hnr LEA &b7 o;o?So p                                                                                                            '
at            /s Shun lf4k /N 0 y f j6/ Y ss'E<                                Yb                        -
L[d h%lf) /Od$J }                    "m m mp ,YA xo H A v c V4/vf                                                  -      .
 
overexposure occurred on October 13, 1984.          One worker received a high exposure (quarterly reading of 2.8 rem) because an unqualified health physics technician was assigned to the work area.          Table 3.9 provides a list of the unplanned radioactive releases at Haddam Neck.
3.13 Nonradiological Events From 1976 to 1981, Haddam Neck experienced 11 instances of exces-sive fish impingement on the intake screens. The problem was attributed to an unusually large fish population during those years.          Other events of environmental concern include a rapid change of the discharge temper-ature (6 events), hypochlorite inadvertently released into the river (1 events), chlorine discharged into the river (          event), and the dis-charge canal reaching a high PH level (1 event).# No events of environ-g ene nepaa/rd mental importance                    during the last three years (1982-1984) of the review.
h        OcG/NN/N4 /A/ /YN3 Y/0 l*4 YJO N T C                Af//4 llC /A/V/MMAt Y*4 /
Awd toA Y1At yen /* 7'y Arqtt/k(Mov$ taMc Ay *sd:errswaWtwYA M' Mp aa 7'ed A ffA.
3 14 Review of Significant Events                  -
Each reportable event was screened, using various criteria, as an additional step in the evaluation process.          A tabulation of the signi-ficant events by year at Haddam Neck are given in Table 3.10.            Events with serious safety implications are described in detail in the follow-ing sections. Table 3.11 presents a summary of these events.            The events which were classified as significant are:
: 1. losses of offsite power (7),
: 2. unanticipated reactor cooldowns (2),
l        .          _ _ . .__        . _ _ . _      - _ _ _ _
 
Table 3.10. Tabulation of reporte categorized as significant at Haddam Neck Significance N      date                                                    Event description                    Section A06707  9/22/67          S3              Inadvertent opening of all lo steam dump valves A06807  4/27/68          S3,57            Maintenance crew inadvertently opened site feeder breakers -
All three DCs loaded then tripped of f - Total station
                              .                    blackout A06906    5/3/69          S8              8oron recovery tank ruptures A06907    5/6/69          58              500 gal rad liquid spilled in boron recovery area A06938    6/10/69          57              High level in steam gen No. 3 due to broken feedvater flow-control valve-reactor tripped A06909    7/15/69    53jS7                Loss of offette power, I DC f ailed to load. I charging pump failed to run A06910    8/2/69          S7              Complete loss of offsite power due to lightning strike on ta'ephone relay A07008    8/19/70          S7              Small fire near RCP due to leaking oil A07009  10/12/70      5),S7                Loss of feedwater flow and steam dump valve out of positidA f - reactor tripped A07403    1/19/74    53jS7                Loss of offsite power during ice storm - Su pumps on oc did u-                                              not start automatically d  LER7634  6/24/76          S7              Totaljoesofoffsitepower-RHRflowlost3 times l    LER7616  7/5/76          S2              80th aux feedwater pumps f all - Common cause failure of both pumpe due to faulty check valve LER1789  8/21/77          S3              RCP seal f alla during operation, causing other 2 seals to fail LER7818  8/25/78          S8                FM transceiver caused dropped rod alare, followed by failure of load runback signal LER7822  12/29/78    53j56.S8              Air supply valves to isolation valves blocked open, loss of l                                                  blowdown and loss of cc.itainment high pressure isolation l    LER7910  8/13/79          S7              Pressuriser /80RV inadvertently opens LER8100S  4/22/81          S8              Contaminated tube bundles released from site prior to health physica review LER8320  11/1/83          S2              Loss of containment control air due to incorrect o-ring LER8321  11/28/83          S2              loss of containment control air due to broken air filter canister PNO-I-    3/15/83          S7              Improper latching between control rod dri,ve shaf ts and rod l      8320                                      control cluster assemblies LER8409  8/l/84          S2,55            Total lose of offsite power due to inadvertent closing of breaker LEB8413  8/21/84          S7              Failure of the refueling pool seal due to improper design LER8414  8/24/84          S7              Total loss of offsite power due to maintenance error i
e
                                                                                                                            =
 
  )
t l
I Table 3.lf          Summary of significant event categories at Haddam Neck l
D "III"""'"  67                        68  69    70                71 72 73    74  75 76 77  78        79 80        81  82 83 84    Total category St                                                                                                                                      O S2                                            I                                      1                                      2  1  $'
S3        1                          1  l                                      l        1        1                                  6 S4                                                                                                                                      0
,                          vg                          SS                                                                        e                                                      1      1 in                      S6                                                                                                  1                                  1 l
S7                                  1  3      2                              1    1                  1                  1  2    1 ;2.
l                                                      S8                                      2                                                          2                  1                5 S9                                                                                                                                      0 i                                                        Total  1                        2  6      3                0  0  0      ,A  0  2  1      ll      1  0          1  0  3  4    30 I
I l
I i
j t                                                                                                                              *
)
: 3. loss of auxiliary feedwater (1),
: 4. failure of feedwater regulating valve (1),
: 5. blocked open steam generator blowdown lines (1),
: 6. reactor coolant pump (2),
: 7. pressurizer PORV inadvertently opened (1),
: 8. boron recovery tank ruptured (1),
: 9. radioactive spill resulted in unplanned release (1),
: 10. control rod drive problems (2)
: 11. shipped moisture separator tube bundles with contamination in ex-cess of limits to unlicensed metal processing center (1)
: 12. loss of containment control air (2), and
: 13. failure of refueling pool seal (1).
3.14.1  Loss of Offsite Power. Offsite power was lost seven times at Haddam Neck. Five failures involved the design of the protective re-laying system for offsite power to the plant. The loss of offsite power event are individually discussed below:
(1) Loss of offsite nower, April 27, 1968. While restoring a 115 kV outside line on April 27, 1968, a switching procedure was used which degraded a transfer trip relay, causing both offsite feeder breakers to open (A0 68-07). All offsite power to the plant was lost. The trip signals were not cancelled for some time because the operators responsi-ble for the task were occupied with the diesel generators and could not hear the telephone ringing outside the diesal room.
Upon loss of offsite power all three diesels started but failed to load and had to be shut down.      The reactor was held just suberitical while the diesels were autonatically phased and loaded, and the reactor
                                $~3
 
    =
was brought critical several hours later.                                                The reactor was restarted without a test of the diesels or an adequate review of the significance of this event.
The most significant feature of this event was the failure of the utility to report the simultaneous loss of all three diesels during a loss of offsite power.                                        No cause for the tripping of all three diesels was found. To help prevent recurrence of this event, diesel performance tests during a simulated loss of offsite power are carried out during planned shutdowns.
The loss of communication between the grid operators and auxiliary operators could have been avoided if the telephone would have had a visual signal besides the normal ring.                                              A flashing light was placed in the diesel room to indicate incoming calls and alleviate this problem.
(2) Loss of offsite power, July 15, 1969.                                                On July 15, 1969, the Haddam Neck reactor was shutdown during switching changes involving 115 kV offsite power (A0 69-09).                                              Normally two 115 kV lines are available, each as a backup for the other. Both are equipped with devices that re-spond to a line fault by disconnecting the other line, which scrams the reactor and trips the turbine.                                              Also, each device has t trip defeat switch.            The switching order did not contain instructions to defeat the trip. Therefore, when one line was removed from service, the other line tripped and offsite power was lost.                                              One diesel generator started and loaded immediately, but the others momentarily delayed loading.                                                                              As the reactor                                          coolant temperature      decreased,    the  pressurizer                            level dropped.                                  This fully opened the flow control valve on one of the charging pumps when this pump was starting.                                              The pump was shut down by 5
4
                                                                                ,__ _                ,_          _..,_..._.____.,,,____a.,_,-o_.m_,.      ,
 
its thermal-overload protection system.                                                                                Shortly af ter shutdown the reactor coolant pressure rose to 2270 psi.                                                                                        Two electromatic relief valves opened to prevent higher pressurization.                                                                                            Even though these problems occurred, all plant systems functioned normally to place the I                                              plant in hot standby condition.                                                                              After 9 min the offsite lines were reistored and the plant restarted.                                                                                During startup, one of the four i                                                reactor coolant pumps had to be shut down due to a failed seal.                                                                                              With 4
three reactor coolant pumps in service, the plant load was increased to 425 W(e).
The plant protective relaying scheme was                                                                        reviewed after the April 27, 1968, loss of offsite power.                                                                                It was noted that new circuitry had been designed but not yet installed.                                                                                This change would have pro-hibited loss of power by the switching errors committed.                                                                                        Also, all op-
;                                                erating personnel were instructed as to proper line switching procedure.
(3) Loss of offsite power. August 2                                                              1969.        During an electrical storm on August 2,1969, the relays for all four power circuit breakers
;                                                  in the 345 kV switchyard, as well as breakers on other interconnecting lines, opened (A0 69-10).                                                                The reactor automatically scrammad and the turbine tripped on the loss of offsite power.                                                                                      All plant systems func-tioned to shut the plant down.                                                                                  The 345 kV switchgear control was shifted from remote to local and all tie breakers were re-closed.                                                                                                      A lightning strike in the vicinity of the 345 kV switchyard caused offsite power to be lost.                                                                  The lightning strike also caused the loss of the telephone lines that are used for transmitting relay signals, control signals, communications, etc. between the station and the switchyard.
((
    ,-.,-m--, .-.--.,,_ .,,,,.-. , , . . - , , , _ , , _ . , . , , _ _ , . , _ _ , , , _ , , , _ . . , _ _ , , , , , , , , , , .                . , _ _ . . _ _ . ,.      . , , , _                  , , . , , , _ . ,    , , _ _ , _ . , , _ , ,
 
(4) Loss of offsite powe r , January 19 , 1974.      An ice storm on January 19, 1974 caused a total loss of station service power at Haddam Neck (A0 74-03). One of the transmission lines providing station power tripped due to a faulted lightning arrestor on an adjacent line.      The second transmission line then tripped due to improper blocking relay operation. Both diesel generators started, but one failed to run. The diesel generator's service water pump failed to start automatically due to a malfunction of the pump breaker undervoltage , device. The diesel generator's service water pump was manually started.-
(5) Loss of offsite power, June 24, 1976.      While the reacror was shutdown for refueling on June 24, 1976, a total loss of 115 kV station service power occurred on three separate occasions (LER 76-14) .      In-vestigations revealed that backup protective relaying from one of the lines was getting its potential signal from the wrong line due to a de-sign error. During the loss of offsite power, RHR flow was lost 'three times. The first time flow was lost for 30 s, the second and third times flow was lost for 10 s.
Problems with the protective relaying at Haddam Neck are discussed further in Sect. 3.1.6.
(6) Loss of offsite power, August 1,    1984. While the reactor was critical at 0% power a total loss of normal offsite power occurred.
This event was initiated by the inadvertent closing of a 4 kV circuit breaker during final check out steps prior to removal from its switch-gear cubicle. The operator had disconnected DC control power for the open breaker and was attempting to lift the manual "open" plunger in order to verify the "open" condition. Due to the close proximity of the
 
open and close plungers behind plexiglass covers and due to the large high voltage glover, the operator inadvertently actuated the close plunger. Closure of this breaker created an overload on the offsite power supplies. The subsequent voltage dip was sufficient to initiate load-shed of the nonsafeguard 4 kV buses by opening the bus tie and supply breakers, thereby disconnecting the overload and the offsite power supplies. The plant was in a total loss of offsite power condi-tion for 10 minutes.
(7) Loss of offsite power, August 24, 1984. While in the refueling mode a total loss of normal of fsite power was initiated by starting a large pump. Power was being supplied by one offsite line and station service transformer. Automatically, both diesel generators started and unnecessary loads were shed. The automatic closure of one diesel gen-erator output circuit breaker was delayed about 20 mins.      Differential relay current transformer wire was found pulled from its terminal lug.
l    Inrush current of starting the pump appeared as an internal transformer i    fault causing isolation of the station service transformer.      The wire pull occurred earlier the same day when maintenance activities were per-l
!    formed in close proximicy. Also, a diesel voltage re    ator was left l
slightly below the breaker voltage permissive relay s,      t when it had been previously shutdown. The relay eventual closed due to vibration of resetting nearby relays and/or voltage and frequency operating varia-tions. Corrective actions include:  (1) a station directive to limit access near electrical equipment panels, (2) revision of operating pro-l l
cedures to adjust diesel voltage regulator well above the permissive I
setpoint prior to shutdown, (3) inspections for other open terminations, I
(7 l
1-
 
(4) initiation of procedure and training enhancements, (5) initiation of permissive setpoint evaluations.
3.14.2 Unanticipated Reactor Cooldown The reactor cooldown rate was unanticipated and excessive on two occasions at Haddam Neck. The first occurred on September 22, 1967 when the reactor coolant temperature dropped 90*F in 5 min (A0 67-07).'    While pulling vacuum on the main condenser, all 10 steam dump valves opened when the low vacuum trip was cleared. It was later discovered that the average temperature signal was locked at 570*F.      Af ter the steam dump valves opened, steam flow increased and the reactor coolant system cooled down 90*F to 525'F in 5 min.      The transient was terminated by closing the nonreturn valves in the main steam lines.      The average tem-perature signal was locked in at 570*F on September 21.        At the time, personnel were calibrating instruments in the reactor control and pro-taction circuit. Once the low vacuum block was cleared, steam dump was initiated due to the 570*F average temperature signal.
The second unanticipated reactor cooldown occurred on October 12, 1970, when the reactor scrammed from full power (A0 70-09).        Following the scram, the turbine shut down and ten steam dump valves opened to re-lease steam directly to the turbine condenser. As pressure decreased, all but one of these valves closed. As a result, heat continued to be removed from the system, cooling the reactor 40*F in 9 min.          It was determined that no detrimental effects to the reactor vessel or other pressure systems occurred.
The reactor scram was caused by a spurious low-flow signal from one loop. Components were replaced to prevent recurrence of the scram. The g*q JW
 
t steam dump valve failed to close because the valve-positioner-coil stop was out of adjustment. The stop was repaired and the remaining valves were inspected for the same problem and properly adjusted.
3.14.3 Loss ot Auxiliary Feedwater During plant startup on July 5,1976 both auxiliary feed pumps were
  , found to be vapor bound ( A0 76-16). The reactor was shut down immedi-ately. The pumps were vented, tested satisfactorily, and returned to service.            ,
This event was classified significant because of the common cause failure attributable te back-leakage from the number three steam genera-tor through a check valvo in the feed line. The faulty check valve was removed, cleaned, and replaced. No further changes to the valve were I
implemented. To prevent recurrence of this incident, temperature sens-ing devices were installed at the check valve to detect back flow into the auxiliary feedwater system. This event was originally submitted as l  an LER 76-16 but was withdrawn later because it did not violate a tech-nical specification. Apparently the event was withdrawn as an LER because the reactor was only at 1% power.      Operation of the auxiliary feedwater system was not required.
3.14.4 Failure of a Feedwater Regulating Valve On June 10, 1969, low feedwater pump suction pressure caused the 1A i  feedwater pump to trip (A0 69-08). Since the specific cause was not l
obvious, a rapid load reduction was made in order to reduce the feed-l  water requirements and restore suction pressure.      The water level in steam generator No. 3 continued to rise. A =anual override of the feed-water regulator failed to reduce the rate of water level increase in the 57
 
steam generator.          The steam generator isolation valve was given a close signal, however the valve requires 3 min to close completely.              Since the water level in the steam generator was approaching a level that would result in gross carryover, the reactor and turbine were manually tripped. The eventual closure of the isolation valve prevented flooding of the steam generator and normal shutdown procedures were followed to j
place the plant in hot standby.
The transient was caused by the valve plug which broke off the stem of the feedwater reguisting valve. Since the valve was reverse seating, the plug dropped open allowing full feedwater flow to the steam gen-erator.
3 14.5 Blocked Open Blowdown Lines On December 29, 1978, an air supply valve failed, closing isolation trip valves on all four steam generator blowdown lines (LER 78-22). The operator subsequently reset and blocked open the air supply valve to re-store blowdown.          This action was deemed inappropriate because it would have prevented the valves from closing in the event of a steam generator tube rupture, providing a potential release path for radioactivity. The
!                  valves were blocked open for 2 h.            The operator did not realize the sig-nificance of blocking open the air supply valve.            In this condition the plant would have had only one valve available for containment isola-tion. A revision of procedures was implemented to prevent recurrence of this event.
3.14.6  Reactor Coolant Pump Failures On August 19, 1970 (A0 70-06), a small fire was discovered and ex-tinguished at the j uncture of a reactor coolant pump and the suction c
b0
 
t piping.            Since the reactor was. at full power, the fire fighting was done from outside the reactor-coolant-loop area.                                      Reactor power was then re-                -
duced to 65% of full power so that personnel could enter the loop area to determine the cause of the fire and make repairs.                                                  Oil had dripped from the thermocouple conduit attached to the motor thrust bearing. The permanent insular. ion on the piping immediately below the fire area had
                                                                                                                    ~
recently been removed for in-service inspection and had been replaced
                                                                                        ~
with temporary insulation that was not completely sealed to the adjacent insulation.                The oil ran down an outside cover of the insulation, en-tered the joint, seeped through the insulation, contacted the 520*F coolant pipe, and vaporized.                        As the vapor emerged from the insulation, it spontaneously ignited.                        The oil leak was stopped with epoxy, and all visibly damaged insulation was replaced.                              Af ter cleanup of the oil in the area, the loop was placed in service, and full-power operation was resumed.                Six days later, oil was discovered on the surface of the new insulation.                Once more the loop was removed from service. There was no indication of any damage other than to the insulation.                                                      To prevent future occurrences drop pans were installed under all four reactor-coolant-pump motors, and checks for oil during in-service inspections are now required.7 On August 21, 1977 (12R 77-19), an operator noticed seal pressure fluctuations in reactor coolant pump (RCP) No. 2.                                      The pump was shutdown due to indications of a seal failure.                        Visual inspection confirmed the f ailure and an estimated 4020 gal. had leaked from the seals. The No. I seal failed during operation and caused the No. 2 and No. 3 seals to be damaged. The full system pressure and high temperature through seal No.
                                                            /#
t
 
I apparently caused flashing between the No. 2 seal runner support and pump shaft.      This resulted in a slight bulging of the No. 2 seal runner support sides.      Westinghouse modified the runner support by drilling two holes in it to allow any pressure buildup to be relieved.                                                                All three seals were replaced. At the time of the vent, the other three RCPs were available.
3.14.7    Pressurizer PORV Inadvertently Opened The pressurizer PORV opened inadvertently on three separate occa-sions at Haddam Neck.        The PORV. opened twice as a result of a spurious signal. The resulting pressure drops were 20 psi (April 3,1981) and 24 psi (February 4, 1980).      On August 13, 1979, the PORV and its isolation valve opened when the bistable in the pressurizer pressure controller failed (LER 79-10).        The pressure dropped 50 psi (from 2000 to 1950 psig) before the PORV could be shut.                                          The operator overrode the signal to the isolation valve stopping the depressurization.                                                              A light in the bistable shorted causing the failure.                                                    The bistable was changed to a solid state design to improve its reliability.
3.14.8    Boron Recovery Tank Ruptured The boron recovery tank was filled solid on May 3,1969 due to an improper valve lineup (A0 69-06).                                          The tank became pressurized and cracked at the heat seam.        Approximately 200 gal. of distillate was re-leased to .the surrounding yard area before the valve line-up was cor-rected. A total of 20,000 gal. of fresh water was used in flushing the area. The run-off collected in a yard storm drain which drains to in the plant discharge canal.
f 7,
      , - - . , , , .-          -.      -              .-    - - . - . - . - - , , - , . . . _ . . - _ , , _ . , , . . . . , . . , , . . .    .n  , , - - -- - - - - - -.
 
3 14.9 Spill Resulted in Unplanned Release on May 5, 1969, 500 gal. of radioactive liquid waste was discharged from the boron recovery evaporator (A0 69-07).            The borated water drained into the floor drains and emptied into the aerated drain tanks.      However, due to a broken nipple on the bottoms pump, some borated water was discharged onto the floor.          The discharge was not noticed until 2 h later due to the small size of the gage line and the low discharge pressure of the bottoms pump.        Some flashing occurred and caused steam vapor in the boron recovery area.        Also, a portion of the l
concentrate cooled suf ficiently to solidify before reaching the floor drains.      After the area cooled, decontamination efforts began.            All solidified boric acid was collected and drumed.          The surrounding area was flushed with water, draining to the aerated drain tanks.            Radiation levels in the recovery area were 10-15 mrem.        The estimated release of I-131 from the vapor was 1.85 x 10 2 C1.          The estimated release of tritium was 2 36 C1.
3.14.10 Control Rod Drives Zero power physics tests on March 15, 1983, (PNO-1-83-2C) discov-ered that four Control Rod Drive Shafts and Rod Control Cluster As-i semblies (CRDS-RCCA) assemblies were unlatched.          Investigation showed that the CRDSs had been improperly latched to the RCCAs during reactor reassembly. The coupling fingers on the four CRDSs were plastically de- ,*
formed (spread), which greatly increased the chance of installing the CRDS with one coupling finger outside of the RCCA hub.          This would occur if the CRDS is oriented during installation so that the coupling fingers o3
 
are positioned between the guide sheaths during insertion into the RCCA hub.
All CRDSs were removed from the reactor and inspected.                The coupl-ings in the four improperly latched CRDSs were rebuilt. The coupling in a fif th CRDS was rebuilt because of latching difficulties that had been experienced during inspection.              CRDSs will be inspected for deformed coupling fingers during future refuelings to ensure proper operation.
Three of the RCCAs that were paired with three of the faulty CRDSs 1
were replaced; the fourth RCCA was acceptable for reuse.                          Five addi-tional RCCA hubs were inspected and determined to be acceptable for for continued operation.
The CRDSs were reinstalled using a revised installation procedure that emphasizes proper orientation of the CRDS to the RCCA while latch-ing.          The Westinghouse Electric Corporation provided appropriate input to these procedures.
The connect / disconnect CRDS buttons were examined for proper height to confirm correct installation and latching.                    All CRDS were measured for correct height.            RCCA drag tests were performed that verified proper latching and alignment.
On August 25, 1978, the use of an FM radio in the control room caused a dropped rod / rod stop alarm (LER 78-18).                The alarm should have initiated a turbine load runback followed by a matching reactor power reduction as well as an automatic cod withdrawal stop signal. The auto-matic rod withdrawal stop signal actuated but a turbine load runback reactor power reduction was not observed.                      Investigation revealed a closed pressure switch isolation va'.ve which disabled the turbine load l
 
runback feature. The procedures were revised to include this valve on a i                                                                                        l checklist to assure that it is returned to its normal position upon com-l pletion of maintenance and/or calibration.                                          '
The reactor core is protected by redundant signals.        One is the I
turbine load runback and the other is the automatic rod withdrawal stop signal. The automatic rod withdrawal stop signal actuated.      This would have protected the reactor core if an actual dropped rod had occurred.
3 14.11 Contaminated Moisture Separator Tube Bundles Released From Site On April 22, 1981, two moisture separator reheater tube bundles were shipped from Haddam Neck to a metals waste processor.      The bundles consisted of 43,000 pounds of copper-nickel alloy material with an ac-i  civity of 10 2 C1. The material was off-site for 18 h. The amount of activity was in excess of the exempt quantities in 10 CFR Schedule B.
Additionally, the metal waste processor did not have a license to re-ceive these materials.
When it was noticed that the tube bundles had lef t the site, the metal processing company was notified and CYAP00 health physics person-nel were dispatched to recover the material. Procedures were revised to include plant management review and any necessary health physics review and authorization prior to the release of all materials that could con-1
~
tain or be contaminated with radioactive materials.
3 14.12 Loss of Containment Control Air The first loss of containment control air occurred on November 1, 1983 (LER 83-20). The result was a loss of control of the pressurizer spray valves and pressurizer power operated relief valves.      Maintenance
                                        $3
 
    .    ~
0    '
had installed an incorrect o-ring on a control air filter canister. The filter canister was improperly installed which led to the loss of con-trol air. The correct o-ring was installed and the filter returned to service.                            ,
The second loss of containment control air occurred on November 28, 1983. Control of the pressurizer spray valves and power operated relief valves was again lost. A filter canister had failed due to worn threads on the filter cap. A new type of filter canister was used to replace the broken canister.
3 14.13 Failure of Refueling Pool Seal On August 21, 1984, (LER 84-013) the refueling pool seal failed while the reactor refueling cavity was flooded in preparation for re-fueling. This failure resulted in the draining of approximately 200,000 gallons of borated water from the refueling cavity to the reactor vessel flange in about 20 minutes.
Water flooded the lower levels of the Containment Building.        At time of the event, the reactor vessel head had been moved to its lay down area, the spent fuel pool in the Fuel Building was isolated from the refueling cavity, the reactor vessel upper internals were still in place, and no movement of fuel was being conducted.
l The cause of the failure was an improper seal design. Corrective actions include:    (1) installation of a redesigned seal, (2) installa-tion of a cofferdam in the fuel transfer canal, and (3) development of i          emergency operating procedures.
l I
d i
I
 
1 3.15 Trends and Safety Implications of Forced Shutdowns and Power Reductions                                      I i
l Data on both the forced shutdowns and the power reductions was an-
                                                                                      )
alyzed with the obj ective of determining any trends on patterns.          In general, the data tends to show a time trend towards incremental in-provement each year. However, the data also evidences three distinct perturbations, clearly displayed in the interpreted forced shutdown fre-quency plot presented in Fig. 3.3A.      Although examination of the shut-down data itself did not lead to any direct cause or causes for each perturbation, other generalized causes may be related.
The first perturbation occurred around 1973 and 1974.        The fre-quency of forced shutdowns increased to twf :e the rate of the previous two years, counter to the trend established 1968 through 1973.*      In 1975 and 1976 the rate dropped again to follow the previously established trend. At the same time that this observed perturbation occurred the plant experienced extensive problems with the turbine.
Concurrently, the frequency of forced shutdowns occurring as a re-sult of equipment failures was showing an excellent trend in improved performance, falling from 10 events in 1968 to 1 event in 1973.      In 1974 the f requency jumped back up to 6 and then a f avourable trend was re-established. This data is presented in Fig. 3.11, and Fig. 3.11 A shows the interpreted data which suggests a saw-tooth pattern.
A second perturbation can be seen on the shutdown frequency curve occurring about 1977 through 1978. As with the 1974 data the frequency doubled over a period of 2 years and then returned to a rate that can be projected from the initial trend. Relational causes are not as clear in S7
 
o-SHUTDOWNS DUE TO EQUIPMENT FAILURES 10_ ,
10 9                                  9 8_                                                8 H
U      6,                        6 W      4_                                4  4 S                      3 3                      3 2                      2                                2 0              llE  ,
l            .
67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.11 t
 
INTERPRETED SHUTDOWN RATE WITH EQUIPMENT FAILURE AS CAUSE 10 -  -
PROJECTED RATE 8-('g 6                                                                l  \
ANOMALOUS                    l
                                                                                }
U                                  PERTURBATIONS                l    g T      6                                                        I D                                  O                          I
{
O W
l\
i
                                                \
I I
N      4-                                \
r            l l                                      g S
1
                                                    \      l\\s        l
                                                      \                i          l I          \l      \                  l i_                                      d        \    l            t
                                                                    \  l            1 0
6'8              7'4          7'7          81              8k
                                                                                                  ~
YEAR OF OPERATION FIGURE 3.11A
 
this case, although the plant had just completed an extended uninter-rupted run of 343 days in August 1977.            Subsequent to this run a number of BOP problems occurred and then reoccurred, suggesting difficulty in effecting problem solutions. Again, examining the shutdown due to equipment failure frequencies shown in Fig. 3.11A there is seen to be a minor perturbation effect from this cause.
A third perturbation is seen around 1981 and 1982, when the shut-down frequency increased by a factor of two before falling back to a projectable rate. In this time period a number of efforts were being applied in response to the TMI effort.            Again the saw tooth pattern in the equipment failure induced shutdown rate may be seen, although in 4
this case with a much enhanced recovery rate.
Other tests for trends or patterns in the shutdown data, such as the DBE turbine trip frequency, or in the average duration of shutdown either gave random results or further emphasized the existence of the perturbations.
The data on reported power reductions generated a completely dif-ferent pattern. This annual rate plots to two distinct " humps" with a zero rate occurring in the years 1974 through 1977.                No discernable correlations were found from examination of the interpreted power reduc-I tion rate plot shown in Fig. 3.4A.
The data showed that causes of downtime were principally for main-
;              tenance and testing, occurring mostly in the balance of plant systems including the turbine-generator system, main steam systems, and electric power systems.
ld
 
l These findings may be interpreted as follows:
;              1. The overall performance of the plant is continuing to improve.
: 2. Major " refit" efforts result in perturbations in the plants' over-all performance.
: 3. Recovery from refits may extend one or two years, as a result of subsequent increase in equipment failures.
: 4. A perturbation as a result of a refit may not necessarily be evi-denced by problems directly related to that refit.                                  Thus, the more.
important negative effects of the refit may lie in reduced at-tention by plant personnel to areas not affected by it.                                  It should be noted, however, that the shutdown data attention to nuclear safety systems.
: 5. Salance of plant systems were the major causes of interruptions to plant operation, mainly for repair and maintenance.
3.16 Trends and Safety Implications of Reportable Events As an additional step in the overall evaluation process, the re-portable events were examined to detect discernible trends that might indicate potential safety problems.                                      Figure 3 12 presents the yearly 4
totals of significant events at Haddam Neck. The plot does not show any discernable trends.                                        Figure 3.13 shows the yearly totals of condi-tionally significant events while Figure 3.14 shows the yearly totals of both significant and conditionally significant events.                                      Both of these plots show a large number of events during the early years, 1967 through 1969 followed by a significant decrease during 1970 to 1972 due to the increase in experience in operating the plant.                                    Peaks in the number of i                                                                                71
 
YEARLY TOTALS OF SIGNIFICANT EVENTS 5,              5 N
U 11 4_
b E
R 3_
F E  2-2                2  2 V
E N
,          T  1      1      1                1        1        1    1 S                                                    ll
                    '                                                ,l 0        , ,
0 0 0        0              l 0  "        0 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.12
                                                '7'L
 
9 e
* m 1EARLY TOTALS OF CONDITIONALLY SIGNIFICANT EVENTS 25_
N U                                                                    21 M          20-i B                                                                                                    19 E
R 15_                                                                  15 0
F                                                                  12 E          10-V                                              9                          8          I E                                                              7          '
N              6 6                                                              l T                              '
                                                                              !                              5 l
5-l ll, 4                              '
t S
2  :
3                        O        4 4l li,'
                                                                      ;i j
I                                          l 1 i    pg        l l1 EEdB                lE!..l O              il,                  ,,  ,
i -
67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.13 73
 
;    g          8 e          4 YEARLY TOTALS OF SIGNIFICANT AND CONDITIONALLY SIGNIFICANT EVENTS 25_
N                                                                                                                  22 M          20, 15, F
E          10,                                                  10 E                                            7 7                                                                7 I                                                      3                  4 0                            R! E        bh                  b              .              .
67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.14 k
 
events can be seen in 1973, 1978, 1980, and 1984.          Specific trends and problems    were  identified    in  the  following    safety-related    areas:
(1) offsite power, (2) control rod drives, and (3) charging pumps.
These are discussed below:
(1)    Offsite power. Offsite power was lost seven times to the Haddam Neck plant.      Figure 3.15 shows the time distribution of these events. No real trend was discerned from this plot.        Five failures in-volved the design of protective relaying system for offsite power co the plant. The first two failures (A0 68-07, A0 69-09) were caused by oper~
ators f ailing to block out protective relaying during switching proced-ures. The protective relaying functioned as designed and isolated the plant from the grid.        The next two trips (A0 69-10, A0 74-03) were I
caused by adverse weather, that is, lightning and ice storms.              Again, the protective relaying functioned as designed but should not have cut off station service power.      During the latter loss of offsite power (A0 l
74-03), one of the service water pumps failed to start automatically and had to be manually started.      Failure of tne pump to . start automatically was caused by a faulty relay.          The fifth loss of offsite power (LER 76-14) occurred during refueling when it was discovered that the protec-tion for one transmission line was getting its power from the other line. This caused protective relaying to trip out one line due to the fault on another.      Protective relaying was improved during July 1976 ending this series of events.
l Off site power was los t twice during August 1984.          Both events are attributed to personnel errors in the switchgear room.            The plant will construct a new switchgear room during the 1989 refueling outage.
l I
mr l                                          /2 I
 
YEARLY TOTALS OF LOSSES OF OFFSITE POWER 5_                              ,
N i
U M 4_
B E
R 3~
0 F
E 2~        2 V
E N
T 1
          ~
1                  1      1 S        !:                          i II                        li i        0  0  !!  0 0 0 0          0    i0 0 0 0 0 0 0 l                                                          -
67 59 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84
.l YEAR OF OPERATION FIGURE 3.15 i s' 1
i
 
(2)  _ Control rod drives. Fif teen events (in Fig. 3.16) involved the control rod drive system. Rods dropped into the core on seven sepa-rate    occasions    (A0 68-07,  A0 68-15,  A0 69-11,  A0 69-18,    A0 70-01, A0 70-03, and LER 80-16). Dropped rods are a safety consideration since the consequences are flux depressions in the core.          All but one. of the dropped rods occurred before 1971.          No rods were dropped during 1971 A m fo net r/ m tesoefost O rpf.
through 1979.      Faulty relays caused five of the rod drops. A Causes were not reported for the remaining events.
Control    rods  became  inoperable on four      (A0 68-22,    A0 69-05, A0 69-13, and A0 69-14) occasions. Inoperable rods are a serious safety concern since control rod movement is responsible for reactor control.
All instances of control rod inoperability occurred within the first 2-years of operation.
One failure (LER 77-27) involved the separation of a rod cluster control vane.      The cause was a faulty bias joint. PNO-1-83-20 reported improper latching between contror rod drive shafts and rod control cluster assemblies. The coupling fingers had plastica 11y deformed. The remaining failure events involved a failure to withdraw rods during a test (LER 83-25) due to a switch failure and a failure of a control rod drive slave cycle.
(3)    Charging pumps. Fourteen failures of the charging pumps at Haddam Neck were reported over the operating history reviewed (Fig.
3.17).      The plant has two centrifugal charging pumps which are used in the chemical and volume control system to charge the coolant loops dur-ing startup and transient conditions.          During loss of coolant accidents the pumps serve as part of a high pressure coolant injection system.
77
 
YEARLY TOTALS OF CONTROL ROD DRIVE EVENTS 5,        5 N
U M      4_
B i          E R
3~    3 0
F E      2~
V E              ??
N              :
T      1,    jj                              1        1    1 s            :jj l      - l 1
4i 0  0  b          0 0 0 0 0 0              0 0 i    0 -
0 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OEERATION FIGURE 3.16 78
 
YEARLY TOTALS OF CHARGING PUMP EVENTS 5_
N U                    4-                                                                                              4 a
B E
R                    3, O
F 2,
Y i
E N                    1_                                                                          1 1
T                                                                                                    ;;                                    ;;-
S                                                                                                    !!                                    !!
o                        oo oo o oooo                                        !!                eo                  !L          o 67 68 69 70 71 72 73 74 75 76 77 78 79 80 81 82 83 84 YEAR OF OPERATION FIGURE 3.17
.l
 
U
.      s The charging pumps also provide water to reactor coolant pump seals.                    In addition to the two centrifugal pumps, there is a positive displacement paens//y no ytu/n~* sd pump *'            the system.
On January 24, 1976 a charging pump outboard seal leaked due to an                    ,
o-ring failure (LER 76-05). The o-ring was replaced.
Seven  failures  occurred  from Apri l  1977  to        May          1978  (see Fig. 3.1%, a period of little over a year.        On April 4,              1977 the 1A charging pump failed due to cracks on the pump shaf e (LER 77-05).                    The
        . shaft was replaced.      The cracks were caused by the thrust collar rot being perfectly square on the shaf t.
On April 26, 1977 a small weep developed on the 1A charging pump seal housing (LER 77-06). The housing was replaced. Two days later the pump was placed back in operation when it failed again (LER 77-07).
This failure was caused by misalignment between pump and motor during replacement.
Later that year, the IB chargitig pump bypass isolation valve failed and was replaced (LER 77-16).      On May 4, 1978, the same IB pump valve failed and was replaced (LER 78-07) only to fail again four days later (LER 78-08).      The valves were being eroded by high velocity water flow. The valve was replaced with another type and the problems dis-appeared.
On May 31, 1978, the IB charging pump's pressure gauge isolation valve leaked near a weld (LER 78-12).        The weld was repaired and the pump placed back in service.      This failure brought to an end the first set of events.
O
 
Two failures occurred in 1981. Both failures were due to excessive vibration.      On July 4, 1981, two nipples on the charging pump cracked and leaked oil (LER 81-10).      The leak was on the charging pump oil lubricating system which is not capable of being isolated.          Charging      ,
pump vibration levels became excessive on November 19, 1981 (LER 81-19). The vibration was caused by a worn key and worn parts of the thrust bearing.
6ne failure occurred in 1982 (LER 82-09). A pinhole leak occurred on October 15, 1982 in a pipe joint next to a charging pump throttle valve. This leak resulted in a small release of radioactive coolant to the auxiliary building. The pipe joint was repaired.
Three failures occurred in 1983.      In one event an operator was unable to rotate charging pump 1A by hand (LER 83-09).        Subsequently, solidified boric acid was removed from the pump.        In another event a charging pump was declared inoperable (LE2 83-16) due to broken wires on a motor bearing thermocouple. The*last failure (LER 83-18) involved the IB charging pump which had a leaky outboard pump seal. The seal was re-placed.
ec      /9 7f y  & j ''- fia AYT.I                  _    -Q
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                                  = 'f4                            .e .cz SI
 
4
: 4. CONCLUSIONS 4.1 Overall Plant Operating Experience The Haddam Neck Plant has been generally operated in a safe and
!                    orderly manner.                                    However the operating history reveals that there are a few areas with demonstrated deficiencies or indications of conditions relating to safety concerns.                                          There are no indications in the operating history that there are extended or repetitious problems that have re-suited in any significant safety consequence.
A visit to the plant confirmed inferences derived from the opera-tional review data that attention to safety is an operating character-l 1stic. A tour of the plant left an impression of a clean and well main-tained operation.                                        There was evidence of positive approaches to imple-menting lessons learned from experience.
One indicator of the quality of performance of plant operations is the ability of a plant to achieve and maintain high levels of reli-ability in operation. This also results in a consequential direct bena-fit to safety.                                  Haddas Neck has a history of higher than average avail-ability and capacity factors. Twice the plant has accomplished extended                                                                          l uninterrupted operating runs, the first for a period of 343 days ending i                      in August 1977 which established a record, and the second for 401 days ending in August 1984.
Adverse effects of the extended runs were not conclusively evident a
!                      from analysis of the data.                                            While there was an observable increase in the number of maintenance-generated shutdowns subsequent to the 1977 run, the same characteristic was not observed in the final months of I
i 1
l 1
  - ,..--,  .  -...n,,-,-..-,_,_-,_..-,_,-,,..~........-,.....-.._.,,,..s,.-__,
                                                          -                                                        +,..n.,-        **      ~+--st~~n-- -,-g----------
 
0 1
1984.                  However, the race of submittal of LERs af ter each run did in-crease, suggesting an increase in maintenance activities.
Apart from problems in the areas of off-site power, charging pumps, and control rod drives, in general any problems involving nuclear safety a
systems or equipment were found and resolved without the need of a con-4 sequent plant shutdown.                                      Sixty-six percent of all shutdowns involving
!            reportable events occurred before 1970, which supports the conclusion that there is an operational focus on preventing nuclear systems l            problems from resulting in forced shutdowns.
l
,                                                                        4.2 Trends and Symptoms f
l
]
Trends were discerned by examination of the data, and were more 1
evident in the shutdown data than in the reportable event data.                                          It was concluded that the forced shutdown data showed a definite asymptotic trend of improvement.                                      However, this conclusion was dependent upon the                i i            premise that certain perturbations to the projected trend can be readily isolated, and correlated to an identifiable set of causes. Accordingly, i.
it was determined that it would be necessary to conduct a broader examination of the operational history.                                              However, the scope of the t
l            effort and the resources available became limiting factors which con-I strained the depth to which this examination could be conducted.
It was concluded that the causes of perturbations which occurred in 1974, 1978, and 1981 may be related to (1) extensive turbine problems, f            (2) an extended operating run in 1977, and (3) efforts in response to TMI, respectively.                                      Actual symptoms of these perturbations were not di-rectly attributed to their theorized causes because of limitations in JD
 
scope and resources. No direct correlation with reportable event fre-quency was detected.      As another conclusion, it might be anticipated that the effects of major efforts applied to the repair or maintenance of plant components in one area may be evidenced in different and unex-pscted areas.
In summary, it was concluded from analysis of the trends that:
: 1. After an initial break-in period the overall performance of the plant was continuously improving with the exception of identified perturbations.
: 2. Major "refic" efforts resulted in perturbations to the plants' overall performance.
: 3. Recovery from refits extended to one or two years, and probably because of consequent increases in equipment failures.
: 4. A purturbation as a result of a refit may not necessarily be evi-danced by problems directly related to that refit. Thus, the more important negative effects of refits may be caused by other reasons such as reduced attention by plant personnel to other areas not affected by the refits.      It should be noted, however, that the shutdown data did not provida any strong indications that plant personnel relaxed their attention to nuclear safety systems.
Three important symptoms were identified through examination of the
,i      reportable event data.      These were determined from analysis of the significant events.
t.oss of of fsite power D
l              During the early history of the plants the significant events were f        dominated by the occurrence of five loss-of-offsite-power events. These 5
 
o  ,
were all attributed to problems with the design of the plant protective relaying. Subsequently corrective measures to the protective relays were implemented. However, there was a later recurrence of this problem and additional loss-of-offsite-power events occurred later on during the 1980s. Thus it was concluded that this constitutes an outstanding symp-ton of a problem which was sa'fety significant. Loss of offsite power is a precursor to station blackout, which is a safety issue.      Haddam Neck sustained one actual station blackout during the period under review.
Control rod drive failures A significant number of control rod drop events were experienced during the first three years of operation.      These were determined to have been principally caused by faulty relays. Corrective measures were applied and there was no further recurrence for 6 years.      However, as the plant grew older, control rod drive failures started to reoccur, for causes including separation of rod cluster control vanes, plastic deformation of coupling fingers, and other random equipment failures.
While no direct correlation to aging was made, it was concluded that this may be a factor in the perpetuation of control rod drive prob-l l
1 ems. The control rods are the principal mechanisms for reactivity con-trol and shutdown of the reactor, and thus serve an important safety function. Failure of the drive mechanisms to operate on improper opera-tion are safety concerns. Thus it was concluded that these failures of the control rod drives constitute an outstanding symptoms of a problem which has safety significance.
                                      ?S
 
i Charging pump failures The charging pumps became significantly undependable in the latter half of the review period.                  For the first 9 years no problems were re-      ;
4 ported. However problems started to occur in 1976 and continued through the later half of the review period, again suggestive that aging may be a factor.                  Equipment failures were reported to have been caused typ-
                                                            ~
ically by wear induced vibrat1on, erosion, chemical solidification, and 4
leaks. The changing pumps serve to inj ect chemical additions to the reactor coolant system and also to provide backup to high pressure coolant injection should this be required subsequent to an accident, both of which are safety functions.                It was concluded that recurrence of operability problems in the charging pumps constitutes an outstanding
;              symptom of a problem which has safety significance.
4 Other symptoms j
It was concluded that causes of downtime were principally for main-j              tenance and testing, occurring mostly in balance of plant systems in-ciuding the turbine generator system, main steam systems, and electric power systems.                  In general nuclear systems did not contribute auch to interruptions to plant operations.
i i
I l
i i
l
 
APPENDIX A REVIEW OF FORCED SHUTDOWNS AND POWER REDUCTIONS This appendix presents the Heddam Neck data on shutdowns and power reductions in narrative and tabular format and lists the information sources. It describes how the information was encoded and how sig-nificance screening criteria were applied.
A.1  Scope
,      Da ta collected in this review includes inf orma tion about each
;  forced shutdown and power reduction that occurred between 1970 and
, 1984. The data is presented in narrative Yearly Summaries (Section A.4) and Tabular Summaries (Table A.1). Forced shutdowns result from equip-i ment failures that present an abnormal challenge to the unit's opera-t tion. Scheduled shutdowns for refueling and maintenance were not in-cluded. However, if the utility scheduled a refueling or maintenance
;  outage to coincide with a shutdown that resulted from an abnormal event, that shutdown was included even though the utility reported it as sched-1
:  uled. That portion of the outage time caused by the abnormal event was attributed to the shutdown and included in the compilations.
Information on power reductions provides additional de tail to a previous or subsequent shutdown, or indicates a safety significant trend. The power reductions were included in the proper chronological l
l  sequence with the shutdowns in the data tables for the forced shutdowns and power reductions (Table A.1).
37
 
A.2  De ta Sources The review of the forced shutdowns and power reductions included data from clm following sources.
: 1. Nuotear Power Plant Operating Experience for 19XX, for the years 197 H 984.
: 2. NUREG-0020 series (Gray Books).20                  ,
: 3. Annual or semiannual reports from the time of startup through                                                  ,
1977. For 1977 through 1984, monthly operating reports were used because the utility was no longer required to file annual re-ports.      The review of power reductions used primarily the annual,
  ,              semiannual, and monthly reports.
When LERs describing shutdowns and power reductions were available, their event descriptions gave additional informa tion and helped to sup-port significance screening.
A.3  Significance Screening                                                            _
Shutdowns and power reductions were evaluated against design basis events  (DBEs)                found in Chap.        15 of      the Scandaztf Revisu Plan 2 (Table A.5).              DBEs are those postulated disturbances in process vari-ables or failures and malfunctions of equipment that plants are designed
,          to kithstand.                  Licensees issue the results of their analyses of these
,          events in safety analysis reports.
Generic design-basis initiating events such as " Increase in Hea t Removal by the Secondary System" or " Decrease in Reactor Coolant System Flow Ra te ," were used as primary flags for reviewing the forced shut-downs (and power reductions).                      Once the generic type of event was 55
 
iden tified, the particular initiating event was determined from the de-tails associated with the shutdown.                                                  For example, if the reactor shuts down as a result of an increase in heat removal because a feedwater reg-ulator valve failed open, the event falls into the category of generic Type 1 DBEs.                    Based on the specific initia ting event (valve failed open), the event is classified as a 1.2 DBE "Feedwater System Malfunc-tion that Results in an Increase in Feedwater Flow." Some shutdowns were readily identifiable as specific DBEs, such as the tripping of a main coolant pump, classified as a 3.1 DBE.                                                    Once categorized as a DBE, the shutdown was considered significant regardless of the resulting effect on the plant (because a DBE had been initiated) .
Loss of flow from one feedwater loop was considered sufficient to qualify as a 2.7 DBE                                              " loss of normal feedwater flow." The closure of a main steam isolation valve in one loop was considered sufficient to qualify as a 2.4 DBE                                                      " inadvertent closure of main steam isolation valves."
Those shutdowns that were not classified DBEs were assigned to NOAC defined categories (Table A.6) inorder to provide more information on i
che failure or error associated wich the shutdown.                                                                      Wich these ca te-                                                  1
;          gories, more specific types of errors and failures could be examined, 1
I through the tabular stannaries , to focus the reviewer's attention on l
;          probles areas (safety related or not) that were not revealed through the 1
i          DBE categories.
Table A.1 of this Appendix provides a tabular summary of informa-tion about forced shutdowns and forced power reductions at Haddam
!          Neck. More information is available about these shutdowns tha t were i
1
  - __ _,      _      _ _ _ _ _ _ _ . . - _ _ . _ _ _ - , , , . . _ _ . . _ . _ _ . _ _ _ .            ___...-_,.,____7.__-._.              . . - _ _ _ _ , - . _ - _ . _ - _ _ _ . _ . . . , .
 
    ~
also reportable even ts; in such instances, this additional information may be found in Appendix B.
A.4 Yearly Summaries for Heddam Neck A discussion of the shutdowns and power the reductions occurrir.g in each of the years,1967 through 1984, follows:
1967 The Haddam Neck Plant went critical on July 24, 1967.      Electrical output of 50 W commenced on August 1.        By December the plant reached full power output of 450 W(e) . Nineteen forced shutdowns and one power reduction occurred in the first few months of operation.        Five of the shutdowns were necessita ted by maintenance on the turbine control valves, which accounted for 17% of the total downtime in 1967. Problems with power distribution equipment caused nine shutdowns.      These repairs accounted for only 10% of the downtime for the year.
Reactor trip systems caused two forced shutdowns, totalling 32 h down time. Repairs to the reactor coolant systems caused three forced shutdowns, accounting for 1184 h of downtime, 1008 h of which occurred on August 21 to repair leaking pressurizar relief valves.
The only forced power reduction that year occurred on October 30 to inspect turbine control valves. Power was reduced for 81 h to perform this inspection.
1968 The greatest number of forced shutdowns (30) for any one year oc-curred in 1968. Thirteen of these involved reportable events. Problems continued with the turbine control system.      The plant shut down eight times for a total of 740 h to resolve these problems.
N
 
a  .
Repairs to steam generators required 454 h of downtime in a single outage beginning on April 1. The plant shut down for 272 h on March 1 to replace the reheater drain tank and to repair the moisture separator.
Three power reductions occurred this year (1) for repairs to:
(1) a feed pump discharge valve; (2) a feedwa ter flow orifice, and 1
(3) one of the two transmission lines.
1969 Twenty power reductions and eight forced shutdown occurred in 1969. The plant shut down six times for a total of 513 h for repairs to            I the turbine control system. Repairs on the turbine control system ac-counted for about 40% of the total downtime for the year.      On April 11 the plant shut down for 456 h for t.urbine valve repairs and modifica-tions. The only other lengthy shutdown occurred on May 1, when the main generator was repaired (258 h).
Power was reduced eight times for total of 177 h to perform main-tenance on the 345 kV transmission lines.
1970 Fifteen forced shutdown for a total of 416 h occurred in 1970.
Over 25 % (109 h) of the downtime was incurred to repair damage stemming from a first on the insulation of one of the four reactor coolant loops. The fire resulted from lubricating oil spilling onto hot piping insulation. This event generated abnormal occurrence A0-70-9-8 and is further discussed in Sect. 3.14.6.
Five of the forced shutdowns were due to problems with the steam generators and with the feedwater control sys tem. The longest shutdown of the year occurred on September 10 when the plant shut down for 65 h to replace the packing glands in the reactor coolant pucips .
                                    .I
 
Five forced power reductions occurred, two in Augus t , to replace insulation damaged in the oil fire.      The remaining power reductions were required for repairs to a circulating water pump, for replacing a ses-tion service transformer, and for repairs to a feedwater control valve.
1971 Nine forced shutdowns and eight power reductions occurred in 1971. The main condenser caused three shutdowns early in the year.
Main condenser problems continued through 1972 and 1973, requiring plug-ging of many tubes.      Feedwater control problems forced the plant down on three occasions for a total of 45 h.          Feedwater control problems are discussed in more detail in Sect. 3.14,4 .
On June 7, the plant shut down for 52 h to investigate the source of grounding of the 4.16 kV buses.        On October 23, repairs to the steam generator feed ptanp check valve required 47 h of downtime for the plant.
The eight power reductions occurring in 1971 were relatively brief. Most of them were caused by problems with one of the condensers.
1972                                                                                      .
Haddam Neck shut down seven times in 1972 for a total of 279 h.
Three maj or outages occurred during the year.                  On September 21, the plant went down for 85 h to repair the main trans f ormer.                On November 23, the plant shut dom for 73 h to repair the turbine control system.
On July 14, repairs on the leaking primary and secondary safety valves
;        consumed 63 h of downtime.      Several short outages occurred late in the year to plug condenser tubes.
Nine forced power reductions occurred during 1972.                Five of them occurred to plug tubes in a leaking condenser, the other four were 31
 
required to replace a reheater drains tank and to repair a steam genera-i tor feedwater pump.
1973 Seven outages occurred in 1973, resulting in 4338 h downtime for the plant. The plant shut dom for five months, starting July 8, to re-solve turbine vibration problems.      The 3828 h outage was the longest in the history of che plant.      Both lower pressure turbines required exten-sive modifications.      Due to the lengthy maintenance outage, refueling
;            was done during that shutdom period.      This did not lengthen the outage time , however. Just prior to the major turbine repair outage, the plant shut dom for 366 h to replace an entire row of blades on one of the low
;            pressure turbines.
Five power reductions occurred this year to plug more tubes in the condenser and to repair the reheater drains tank.
1974 Fourteen forced shutdowns occurred in 1974, causing a loss of 771 i            operating hours. Turbine problems accounted for 90% of the total down time (695 h) accurred over seven outages. One of these outages occurred l            on March 23, when the plant shut dom for 660 h to repair broken turbine blades.
1975 Only five forced shutdowns occurred for a total of 70 h downtime in 1975. The longest outage of the year (39 h), besides refueling, oc-
,            curred on March 26 when the packing gland on the letdown system stop i
valve had to be replaced due to excess leakage.
i3
 
1976 The high plant availability established in 1975 continued into 1976, with only 80 h lost to forced outages.        Almost half of the down-time was incurred by repairs to a broken steam baffle in one of the moisture separators.      A 17 h outage occurred on January 22 when several instrumenta tion  sensing    lines  froze  causing  the reactor    to    trip (LER 76-1).
1977 Twelve forced shutdowns resulting in 289 h of downtime occurred in 1977. No outages occurred until August 19 when the plant shut down for 70 h to repair a leaky feedwa ter heater and to perform general mainten-ance. The only other lengthy outages of the year occurred in le.te December. The plant shut down five times for a total of 83 h for tur-bine balancing during that month.
1978 Fourteen forced shutdowns occurred in 1978 for a total downtime of 332 h. About 90% of the downtime resulted from malfunctions in three systems:    (1) the moisture separators; (2) steam generator feedwater system, and (3) the onsite electric AC power system.
Three major outages, totaling 119 h, were needed to effect repairs to the moisture separa tors and reheaters.        Most of this time was re-quired for the rewelding of baffle places on the separatoro.            Repairs eroded drain piping on the moisture separator reheaters were also com-placed.
The steam generator feedwater system repairs required two shutdowns f or a total of 91 h of down tice.      Both outages were needed for repairs to the B steam generator feed pump.
Y
 
The longest outage of the year occurred on June 17 when the plant shut down for 66 h to install heat shrunk sleeves on the electrical pen-etrations. A 23 h outage was required on March 24 to replace the elec-trical terminal block in the containment.
One power reduction occurred in 1978 for repairs to a steam genera-tor feed pumps.
1979 Four shutdowns resulted in 268 h downtime in 1979.      On September 29 the plant shut dem for 234 h to inspect the welds on the steam genera-tor feed line nozzles. The remaining outages were relatively brief and were insignificant with respect to plant operations.
Five power reductions for a total of 243 h occurred in 1979.        Ra-pairs on a leaking reactor coolant pump seal accounted for 168 h at re-duced power hours.
1980 In 1980, there were six outages resulting in a total of 188 h of down time. The plant shut dom for 44 h in February to plug tubes in' main condenser unter boxes. Turbine balancing accounted for 65 h of downtime starting on September 27.
No other outages exceeded 20 h in dura clon.
Power was reduced three times for a total of 64 h in 1980.      Two re-ductions were required to pitg leaking condenter tubes, and the third was required to repair a steam generator feed ptanp.
95
 
1981 In 1981, there were 11 forced shutdowns and 3 power reductions re-sulting in a total of 248 h of downtime.      On December 11, while reducing power for turbine maia tenance and the plugging of tubes in        'B' con-denser, erratic operation of the turbine control valves caused a turbine overspeed trip. The unit remained shut down for 82 h. the reactor was manually scrammed on August 23 in order to repair a valve packing leak which required 47 h downtime before the unit could be returned to ser-vice. On July 29, while reducing power, a low pressure steam dump mal-function caused by OPC relay 63, resulted in a reactor and turbine trip and a down time of 39 h.      The reactor scrammed during APRM functional testing on October 1, requiring 31 h of downtime.
On February 27, the plant tripped on a loss of feedwater control due to a loose control air header fitting.      On December 22, the reactor and turbine tripped on high pressure heater drain tank level as a result of a failed fitting on the control air system.          On Sep tember 10, a spurious closure of the right hand turbine stop valve resulted in a plant trip.
The other outages and power redoctions, none of which incurred more than 5 h downtime, involved a steam generator low level alarm, flooding of a feedwa ter heater, a steam leak on MOV36, a transfer of reactor coolant pump suction to the station service water, and hood reductions due to valve steam leakage resulting in three loop operation, off-gas activities, and condenser tube plugging.
5
 
1982 Seven forced shutdowns for a coul of 407.5 h occurred in 1982. Of these seven, five occurred as results of failures in the turbine genera-tor systems and in the electrical power systems accounting for 395.4 h of downtime. Only 12.1 h forced shutdown was caused by problems in the reactor systems.
The turbine and reactor tripped twice as a result of short circuit problems in the generator exciter for 150.7 hs down time.      Moisture in the main transformer oil, occurring as a result of leaks, caused another 195.1 h downtime. The pin holding the disc to the stem in a turbine trip valve sheared, so tha t the valve would not open.      39.2 h was re-quired for repairs.
Two events, one involving operation error and one involving a rod drop for unknown reason, occurred in the reactor systems. While the rod drop event was classified as a design basis event, neither event caused any significant result.
Power was reduced 8 times, mostly to repair leaks in the condenser tubes. Also repairs were conducted on a vibrating steam generator pump, and a steam generator leak. A monthly turbine stop valve test was con-ducted.
1983 A total of only 33.6 h of downtime was incurred as a result of four forced shutdowns in 1983. Of these, 9.9 h was required in one shutdown for an overspeed turbine trip test.        The other three shutdowns were variously caused an inadvertent loss of power supply as a result of man-ually resulting control switches, spurious instrument cutput and a feed regula ting valve operation. No significant results were experienced.
97
 
One load reduction was required to repair leaks on a steam genera-tion level indicator.
1984 Again, in 1984 there were only four forced shutdowns, resulting in 86.0 h of downtime 79.0 h accumulated in three shutdowns caused by prob-less in main generator hydrogen system. Two other problems resulting in shutdows were a cycling voltage regulator and flow control of a reactor coolant pump.
One power reduction was required to repair leaks in the feedwater system.
 
Table A1  1967 Forc2d Sh:tdsens and Power Rodrctions far Heddan Meck DBE (D) /
N SIC (N)
Duration Power    Reportable                                                                              Shutd own System    Com ponent      Event Dato                        (lit s)  (1)  Event            Description                                              Cause Method        Involv ed  Involved      Category 7/25/1967                NA              A0-67-1    Inadvertent actuation of                                              D        3          ED      RELAYI        N5.1 l                                                      over-voltage relay in the rod power supply j 7/20/1967                  NA              A0-67-2    Reactor trip due to a spike la the                                    A        3          IA      INSTRO        N2.4 intermediate range start-up circuit 8/07/1967                174      9    AO-67-3    Replacement of penis on all reactor                                  B        1          CD      PURPI          N 1.1. 4 coolant pumps, repairs to main steam lian leaks and turbine control valves 8/15/1967                2        9                Turbine trip due to overcurrent                                      A        3          Eb RELAYI        D2.3 protective relaying on 309 service station transformer 5/22/1805                2        7                Slippage of asia steam isolation                                      A        3          HB      INSTRU        N1.1.4 valve off the upper limit switch energizing the main steam line trip valve closure circuit 8/17/1967                6        9    A0-67-4    Accidential gronading of the vital                                    B        3          EB      ELECON        N5.2 bus during calibration of reactor control system 8/19/1967                11        9                Lightning striking 345 Kr line in                                    H        ,3          EA      ELECON        E 9. 2 s witchyard 8/19/1967                0        7                Excessive vibration at generator                                      B        3          HA      GENE 3A        N1.1.4 exciter 8/21/1967                1000      22              Repair leaking pressurizer safety                                    B        1          CA      VALVEI        N 1.1. 4 valves and spray valves 10/02/1967                15      9                Repair bloma gasket on left hand                                      D        1          RA      PIPEII        N1.1.4 turbino stop valva pressure equalizing line 10/05/1967                130      22  Ao-67-8    No. 1 vital bus inverter power                                        A        3          ED      INSTRU        N1.1.4 supply to all primary giant instrumentstion was in terrupted 10/10/1967                32            Ao-67-9    Turbine control valve failed to                                      A        3          IA      VALVEI        N1.1.4      a close 10/13/1967                54        7    A0-67-10  Dlown fuse in power su gply f rom No.                                A        3          Ep      INSTRU        N1.1.4 1 vital bus inverter                                                                                                          -
kk                                                                                                    -
 
Table A1  1967 Forc:d Shutd2tn3 a:d Powtr Radictic D f r Hcddza Beck-(Continwd)                        -
    -      ----------------------                  .        =..              ----- --    --      _=--_      ---        --=-
DDE(D) /- -
NSIC (N)
Duration Power  Reportable                                                  Shutdown    System      Co m ponent  Event Date                    (!!rs)  (%)  Event            Description                      Cause Method        Involved    Involved    Category I
10/16/1967            3        30  10-67-12  Inadvertent grounding of vital bus        B        3          EB        ELECON      N 5.1 while trouble shooting an irregularity in the power supply 10/25/1967            120      43  10-67-13  Blown fuse in the power supply to          A        3          ED        INSTRU      N1.1.4 the coincidenter 10/30/1967                      43              Power redu: tion. To inspect all          B        5          HA        VALVEI      N1.1.4 f our turbine control valves 11/04/1967          36        43              Repaired steam leak on No. 1              B        1          HA        PIPEII      N1.1.4 control valve - sain steam turbine Icad-in line 11/10/1967          25        65              Installed nov level control valves        B        1          HH        VALVEI      N1.1.4 on reheater drain tanks 11/18/1967          2        70  Ao-67-15  Inadvertent granading of the vital        B        3          ED        ELECON      N5.1 bus while troubleshooting 11/20/1967          177      75              Bemoval anS re-lastallation of            B        1          HA        VALVEI      N 1.1. 4 turbine control valves e
L l00
 
Tahlo A1                    1968 Forced Shutdoens and Power Radsctions far Hadden Nick-(Chntinnd)
DBE(D) /
h SIC (N)
Duration Power      Reportable                                                                        Shutdova  System                  Com ponent            Eve nt ato                              (llr n)  (1)      Event                                Description                        Cause Nethod        Involved                Involved        Catego ry 1/12/1960                      242      70                                      Repai ed pressurizer safety,                  B        1                        C1      VALVEI          N1.1.4 feedwater check, and steam line isolation trip valves 2/09/1963                      0        45        10-68-2                      Power red uction, sepairing leak on          B        5                        EH      VALVEI          N1.1.4 In feed pump discharge check valve 2/14/1968                      5        85        A0-68-4                      Reactor coolant pump bus feeder              A        3                        EC      CETBRK          N1.1.4 circuit breaker tripped open 3/01/1963                      272      85                                      Installed new coheater drain tank            B        1                        MH      TURBIN          N 1.1. 4 and repaired solsture separa to r desister sections 3/12/1963                      49        68                                      Repaired steam leak on high                  8        1                        HA      TU R BIN        N 1.1. 4 pressure turbine flange 3/15/19(8                      298      17                                      Repaired steam leak on high      ,          B        1                        HE      TURBIN          N1.1.4 pressure turbine flange 3/20/1963                      1        10        A0-68-8                      Inadvertent acteation of turbine              G        3                        Ik      INSTRO          31.1.4 low vacuum trip signal 3/29/1963                      32        17                                      Removed bijk pressure turbine upper          B        1                        HA      TURBIN          N1.1.4 cylinder for repair 4/01/1963                      4b4      0                                      Installed 4 steam generator seal              B        1                        CC      VESSEL          N 1.1. 3 welded aanway diaphrams 4/27/1968                      9        65        10-68-7                      A switching procedurc bas used                G        3                        EA      CKTBBK          D2.6 which unguarded a traarfer trip relay causing the site low side breakers ta open 5/03/1963                      0        52                                      Power reduction. Repairing weld              B        5                        HH      PIP EIR        51.1.4 leak in 82 feedvater line flow o rifico 5/04/1968                      4        52        A0-60-0                      Automatic reactor trip caused by              A        3                        IA      INSTRU          N 1.1. 4 f also overpower trip signals on two power range channels 5/19/1963                      0        52                                      Power reduction. For maintena nce            B        5                        EA      EL ECOM        N 1.1. 4            -
on 345 Kr transmission line 6/05/1968                      96        43                                      Repaired turbine control valves and          B        1                        HA      VALVEI          N1.1.4 high pressure turbine gland seals
* Inl
 
Table A1    1968 Forced Shutdowns and Power Redrctio2s for Haddas Neck -(Contixued)
                                                                                      .e ~4
                                                                                                                      .                                                                      . c DBE (D) /
N SIC (N)
Duration    Po'ver          Reporta ble                                                  Shutdown      System        Component  Event Date                                    (Ifrs)      (X )            Event                    Description            Cause Method            Involved      Involved  Category 6/10/1963                        6          85              10-68-10      A salfua: tion la loop 1 flow            A      3            IA          IN STRU  N2.3 transmitter caused the flow signal to fail low 6/16/1963                        4        ' h'i                            Repaired pinhole leak in 83 feed          B      1            CD          V&LVEI    N1.1.4 line check valve 7/05/1963                      29          52                            Replaced steam generator feed pump      B        1            HH          PD M PII  N1.1.4 nochanical seals 7/19/1968                        51          83                            Repaired turbine control valve            B      1            51          VALVEI    N1.1.4 0/02/1968                        65          70              10-68-12      Both turbine,,stoo ,waj wrs clo sed -    1      1            51          YALVEI    D2.3 tripping tne turonne 0/09/1968                        87          70              10-68-13      Right hand turbine stop valve            A      3            UA          VALVEI    D2.3 closed 0/23/1968                        2          70              t o- 6 8- 14  & failed closed feedvater                A      3            RH          VALVEI    D2.7 regulating valve resulted in a steam / feed flow mismatch 8/29/1968                        55          70                            Rebuilding turbine control and stop      B      1            BA          VALVEI    N1.1.4 valves 9/01/1968                        115        0                              Repair leaking spray valve bonnet        B      1            SF          VALVEI    N 1.1. 4 9/21/1968                        6          85                            Replaced test solenoid dump valve        B      1            HA          VALV0P    N1.1.4 in the auto-stop oil s ystem from the right hand turbine stop valve 11/17/1968                            0          52                            Power reduction. For maintenance        B        5            EA          ELECOM    N 1.1. 4 on 345 Ky transmission line 11/10/1968                            12          85              A0-6 8- 16    1D scram breaker opened without          A      3            In          CETBRK    N 1.1. 4 apparent cause, tripping the plant l 11/22/1963                                      0          61                            Power redu: Lion. Reactor physics        B      5            RB          CONROD    N 1.1. 4 testing - 3etermination of rod worth l 11/20/1968                                      71          10                            Shutdown ta plug leaking tubes in        B      1            HC          PIPEII    N 1.1.1 l
l main condenser l                                                                                                                        l O2-1
 
i Table A1                1968 Farc2d Shttdsens cad Pecer Rsducticas fcr Mcddam Ecck-(Coitirued) l _            __        __                    _.                    _--                    -----.        _      -                          --          . . .
DDE (D) /
N SIC (N)
Duration Power            Reportable                                                                      Shutd own    System          Component    Event Date                          (lic a)      (%)                  Event                        Descrip tion                  Cause Nethod          Involved        Involved    Category 12/01/1968                26        0                                              Installing new circulating water        B        1          HP            PIP EII      N 1.1.1 varming line
                                                                                                      ~
i 12/09/1969                  4        85            A0-68-19                        1B scram breaker opened without          A        3          IA            CKTBRK      N1.1.4 apparent reason, tripplag the plant 12/17/1968                10        85            40-68-21                        1D scram breaker opened without          A        3          IA            CKTBRK      N1.1.4 apparent reason, tripplag the plant 12/25/1963                14        85            10-68-23                        IB scram breaker opened without          &        3          IA            CET BRK      N 1.1. 4 apparent reason, tripping the plant 12/27/1969                50        85                                            Investigation of the unexplained        B        1          IA            ZZZZZZ      N1.1.4 plant trips e
9 e
105                                                                            -
 
utes. ; e, g
)                                                                                                                              _
DBE(:)/
N SIC (N ),  ,
Duration Power  Reportable                                                    Shutdown System            Co m ponent    Event Data              (Hrs)  (K) ,  Event                Description                    cause Method    Involved          Involved      Category 1
I 1/08/1969      5      07      A0-69-2      1D trip breaker opened - tripping          A      3        IA              CKT ERK        N1.1.4 the plant              ,
1/08/1969      2        100    no-69-3      uhile repairing an oil leak, the          A      2        HA              VALTOP        D2.3 gage line on the turbine auto-stop system was broken, causing the closure of the right hand turbine stop valve 1/18/1969      0      51                    Power redaction. Maintenance on            B      5        EA              ELECON        N1.1.4 345 Ky treassission lime e
1/19/1969      0      51                    Power reduction. Maintenance on            B      5        EA              EL ECON        N 1.1. 4        l l                                    .          345 KV transmission lite l
l  1/25/1969      0      51                    Power reduction. Maintenance on            B      5        EA              ELECON        N1.1.4 345 Ky transmission line l
1 2/02/1969      0      51                    Power reduction. Maintenance on            b      5        EA              ELECON        N1.1.4          l l                                                345 KT transmission lite 2/09/1969      0        51                  Power redaction. Maintenance on            E      5        EA              ELECON        N1.1.4 345 KT transmission line 2/14/1969      0      51                    Power reduction. Raintenance on            B      5        EA              ELECON        N 1.1. 4 345 Kw transmission lire 2/22/1969      0      51                    Power redaction. Maintenance on            B      5        EA              ELECON        N1.1.4 345 KV transmission lite 3/29/1969      7        100                  Right hand stop valve closed, due          A      2        HA              VALTOP        D2.3 to failure of servo-motor cup valve 4/11/1969      456      100                  Turbine valve modifications and            B      1        HA              VALTEI        N1.1.1 repairs 5/01/1969      250    0                    Disassembly and repair of main            B      1        HA              GENERA        N 1.1. 4 genera tor 6/06/1969      53      04                  Repaired generator hydrogen leak          B      1        HA              GENERA        N1.1.4 04    An-6 9-8      Broken feedvater regulating valve                2        IIH              VALTEI        DI.2 6/10/1969      18                                                                      A plug causing flooding cf 83 steam generator 7/15/1969      5        03    AO- 6 9- 9    While switching outside the plant          H      3        BA              CKTDRK        M9.1 to remove one 115 Er line froe service,                        ,
a procedural error allowed both incoming lines to trip IO+
 
Tahle A1  1969 Forcad Shitdoens aRd Power Rsductions far Haddsa Meck-(Continued) r
                                          ,                                                                                                        DBE(D)/
N SIC (N)
Dur.ition Power      Reportable                                                    . Shutdown    System        Comyonent  Event Datu                          (Hrs)  (%)            Event            Description                  cause Method        Involved      Involved  Catego ry
                                                                      ,        .n-7/10/1969                50        83                        Installed new seals in 84 reactor        B      1            CD            PU N P11 N1.1.4 coolant pump 0/02/1969                7          83      A0-69-10          Electrical stora opened all four          H      3            BA          CKTBBK    N9.2 power circuit breakers in 345 Ev yard 0/10/1969                0        83      10-69-11          Manual trip due to two dropped            A      2            RB            REL ATI  N 1.1. 4 control rods because of malfunction in-out relays 0/30/1969                41        83      A0-69-12          Replaced resistance temperature          B      1            ID            INSTRO  N 1.1. 4 detectors in loops 83 and 84 9/01/1969                  15      0      AO-69-13          843 control rod stickieg during          A      3            RB          COMROD    N1.1.4 power increase 9/06/1969                39        83                        Installed five thimble plugs in          B      1            HH            PI P EII N1.1.4 leaky tubes in IB feedsater , heater 10/06/1969                  13      03                        Repaired relief valve ca turbine          B      1            HA            VALVEI  N1.1.4 governor oil pump 10/10/1969                50        63                        Repaired tube leaks in 3B feedwater      B      1            HH            PIPEII  N1.1.4 heater 11/11/1969                  3        100    An-69-15          Steam / feed / level mismatch due to      G      3            HA            VALVE 1  D2.3 inadvertent opening of turbine governor oil system relief valve 11/12/1969                  32      100    An-69-16          Steam / feed / level aisaatch due to      A      3            HA            VALVEI  D2.3 malf unction in turbine governor oil system relief valve sten 11/10/1969                  3        100    An-69-17          The primary electric protection          A      3            EB            RELAYI  N1.1.4 relay tripped due to scisture in terminal box causing a short circuit                                                                                          ,
11/20/1969                42        100    A0-69-18          Manual trip due to two dropped            A      2            RH            INSTRU  N 1.1. 4
* control rods caused by a faulty capacitor in 811 rod botton                                                                      .:
bistable drawer
                                                                                                                                                              ~
l e f."
 
Tchle A1  1969 FcrcId Shttdat:2a exd Posco Rrdtetio~as frr if addIQ Nock -(Continued)                    .
DBE (D) /
N SIC (N)
Duration Pow er  Reportable                                                  Shutdown    System      Component  Event Datu                (Itcs)  (%)    Event            Descrip tion                    Cause Method        Involved    Involved. Category 12/06/1969        0        56                Power reduction. Maintenance on            B        5          EA        ELECON    N 1.1. 4 345 KT transmission line 4
9 9
0 106
 
Tablo 11                          1970 P:rced Shutdo::sa ccd Pouer Radicticca fcr Bcadoa Neck-(Continusd)
DBE (D) /
sSIc ts)
Duratiou Power  Reportable                                                                          Shatdown  Systee      Com pon ent  Event Dats                                                                          Ints)  (5)  Event                                      Descrip tion                  Cause nothod      Involved    Involved    Category 3/21/1970                                                        16      78                                      Repair leaking 11 stea s gene ra tor      B      1        BB        TALTEI      N1.1.4 f eed pump discharge valve 3/25/1970                                                        4      78                                      Repair leak in 83 staae generator          B      1        RB        PIPEII      M1.1.4 feedwater line drain 4/02/1970                                                          3      75    10-70-3                            Banual trip due to more than one          A      2          BB      RELAYI      E 1.1. 4 dropped control rod caused by a f aulty contact la a 'ccattel in' relay l                        4/14/1970                                                        5      75                                      Sepair steam leak in 83 feedwater          B      1        HH        PIPEII      N1.1.4 l                                                                                                                                            flow control orifice senslag line 1
I                        6/27/1970                                                          al      63                                      Balancing tarbine and adjusting            B      1        BA        TU R BIE    N 1.1. 2 l                                                                                                                                            turbine controls 7/19/1970                                                          10      100                                      Loss of condenser vacuma dee to            B      1        BC        BTEICE      N1.1.4 plugged gland seal seal steam s trainer 8/09/1970                                                        47      70                                      Replaced as turbine stcp valve            B      1        HA        TALTEI      N1.1.4 shaft 8/17/1970                                                        1      100  AO-70-1                            Lightning struck terminal box la          1      3        BA        CETBBK      E9.2 345 Es suitchyard, trigging plant 8/19/1970                                                        0      75    10-70-8                            Power reduction. To replace                B      5        CB        PIPEII      N1.1.4 insulation on 84 reactcr coolant
[                                                                                                                                            loop
\'
8/25/1970                                                        0      65    10-70-8                            Power reduction. To replace                B      5        CB        PIPEII      M1.1.4 insulation on 84 reactcr coolant loop                        .
0/30/1970                                                        4      75    10-70-8                            Returning isolated loog 4 to              B      1        CB        EEEEEZ      N1.1.4 service after repairs 9/01/1970                                                        9      100                                      Replaced valve packing glands la          B      1        CB        VALTRI      E 1.1. 4 reactor coolant loops 9/10/1970                                                        65      100                                      Replaced valve packing glands in          B      1        CB        TALTEI      N1.1.4 reactor coolant loops 9/24/1970                                                        0      47                                      Pouer redoction. Replace faulty            B      5        EA        TRANSF      N1.1.4 station service transf creer 102                                                                      -
 
                                                                                                                                ~
Table A1  1970 Forced Shatdowns and Power Reductions for Hadden Neck-(Contis.ued)
DBE (D) /
uSIc(E)
Duration Power  Reportable                                                Shetdown  System      Component  Event Date          illes)  (%)  Event            Descrip tion                Cause Bethod      Involved    Involved  Category 10/12/1970  6        100  10-70-9    Bosentary decrease la reactor            1      3          IA        IESTRO    31.1.4 coolant flow indication tripped plant 10/23/1970  13      100              Operator Liceassag exans                E      1          BI        ZZZZZE    E8.3 10/26/1970  8        100  10-70-11  Investigation of pressurizer level      B      1          CA        INSTRO    N1.1.4 probles 11/24/1970  0        70              Power reduction. Dae to loss of          B      5          BC        PURPII    N1.1.4 "Da circulating water gump 11/25/1970  0        70              Power reduction. . To repair ' flange    B      5          HH        TALTEI    31.1.4 leak in 83 feeduater ccattol valve 12/03/1970  6        100              Plant trip caused by suitching the      G      3          EB        ELECOE    N2.2 semi-vital bus power supply to a f anited source 10hi
 
Tablo Als    1971 F:rc d Shutdocac c:d Poser Ecoscticte frr Mcdd 0 Neck-(Continu1d)
DBE(D)/
NSIC (E)
Duration Power  Reportable                                                    Shutdown      Systen                  Co mpon ent          Event Datu          (Hrs)    (1)    Event              Descrip tion                  Cause Method            Involved                Involved            Category 1/03/1971  0      70                  Power reduction. Identification of      B        5              BC                  HTEICH              B1.1.4 malm condenser tube leaks 1/04/1971  0      90                  Power redaction. To repair              B        5-              HH                  YAL10P              N1.1.4 feedwater heater valve positioners 1/31/1971  0      70                  Power reduction. . Idealfication of      B        5-            HC                  HTEICH              N1.1.4 main condenser tube le aks 2/01/1971  0      70                  Power reduction. To plug main            B        5              BC                  HTEICH              M1.1.4 condenser tube leaks 2/02/1971  0      70                  Poser reduction. To repair steam        B        5              HB                  PIPEII              E1.1.4 generator feed pump seal cooling water bose connection 2/06/1971  0      70                  Poser reduction. To cceplete work        B        5              EA                  EL ECON            N1.1.4 on transmission ilmes 3/19/1971  0        70                  Power reduction. To perform              E        5              BB                  ELECON              M1.1.4 transmission line mala tenance 5/28/1971  8        90                  Repair leaking high pressure            B        1              HA                  TUERIN              N1.1.4 turbine inspection par t 6/07/1971  S2      100-                Shutdova to hot standby to identify      B        1              EA                  ELECOE              E2.2 source of 4.16 It ground 6/11/1971  13      100-                Failed light source casses reactor      A        3              11                  INSTRU              N 2.1 trip 7/12/1971  36      100                nanual turbine trip to investigate      E        2              PC                  PDHPII              M1.1.4 cause of leak in heater drains and pump suction 0/21/1971  4        100                Loss of solenoid valve la 84            A        3              HH                  TALTEI              D2.7 feedvater control systes resulting in closure of 94 feedsater control valve, causlag steam /f eed flow mismatch coincident with low level in steam generator 0/21/1971  25      6                  Plugging leaking tubes in 11 and 1B      B        2              HH                  HTEICH              N1.1.4      ,
feedvater heaters
( 0'I                                                                                                  .
 
Table A1  1971 Forced Shutdowns and Power Reductions for Hadden Neck -(Continued)
DBE (D) /
i                                                                                                                          usIc ts) i              Duration Power  Reportable                                                Shutdous  Systen      Congonent  Event Date            (lles)    (5)  Event            Description                  Cause Bethod        Involved    Involved  Category I
I'  9/07/1971    18        100            A momentery around on the vital          3      3          IA bus, camsd by as adjustment of the                                    INSDEU    D2.7 low neutros level alars motpoint needle on source range chamael ett resulted in loss of control of feedwater to steam generator 10/23/1971    47        70              Repairing steam generator feed penp      B      1        55        YALTEI    N1.1.4 check valve 12/02/1971    23        100  10-71-1    A fallare la the T                      A        3        EN        TALTEI    D 2.7 average /feedwater over-ride solenoid operating valve closed 82 f eedvater control valve causing steam / feed flow mismatch coincident with lov level la 82 steam generator 12/16/1971    0          52              Power redaction. Repairing leaking      B        5        BM        TALTEI    N1.1.4 feedvater regulating velve upper bonnet gadget II0
 
Table A1      1972 Esrcrd Shutdarne and Pouer Reductions for fladdoc Neck -((butinued)
                =      - - - - - - - - - - - - - - - - - - _ =                                                                                                        ----        --
DDE (D) /
H SIC (N)
Duration P ow er                Reportable                                                  Shutdown    System      Co m ponent  Event Date                                                                                                                          (itrs)  (%)  Event              Description                  Cause Method        Involv ed    Involved    Ca tegory 1/22/1972                                                                                                                20      100                automatic reactor / turbine trip        A        3          IA        INSTRU      D2.3 caused by failed light source in the 8 2 reactor coolant loop flow indicator
;                  2/18/1972                                                                                                                0        70                  Power reduction. Plugging main          D        5          ffC        IITEICII    N1.1.4 condenser leaking tuber 2/27/1972                                                                                                                21      100                Steam / feed flow mismatch coincident    G        3,        EB        INSTRU      26.1 with lov level in 84 s team generator due to loss cf on-site power caused by error of test department personnel 3/03/1972                                                                                                                0        93                  Power reduction. Decrease in i3          D        5          till      VALVEI      N1.1.4 steam generator feed pump suction due to sheared valve pcshtioner on heater drains tank normal level                                              .
control valve 3/08/1972                                                                                                                0        50                  Power reduction. Plugsing main          B        5          HC        IITEICll    N 1.1. 4 condenser tube leaks 3/23/1972                                                                                                                0        62                  Power reduction. Plugsing main          D        5          IIC N      HT EICII    N1.1.4 condenser tube leaks 3/25/1972                                                                                                                0        50                  Power red uction. Replacing heater      D        5          Illi      VALVEI      N1.1.4 d rains tank normal level control valver packing 4/14/1972                                                                                                                0        50                  Power reduction. Repacking heater        B        5          Hit        VALVEI      N 1.1. 4 d rains tank normal level control valve 4/29/1972                                                                                                                0        50                  Powder reduct ion. Repacking heater    D        5          Illi      VALVEI      N1.1.4 d rain tank normal level control valve 5/22/1972                                                                                                                12      100                Repaired steam leak on 84 foedvater      B        1          lill      VALVEI      N1.1.4 bypass check valve 7/14/1972                                                                                                                63      0                  Ropair leaking primary and                D      1          CD        V A LVEI    N1.1.4 secondary safety valves                                                                      ,
7/17/1972                                                                                                                5        0                  Turbine balancing                        B        1          HA        TURBIN      N 1.1. 4    .
(Il                                                              .
 
                                                                                                                                                        =
Tablo A1      1972 Forced Shutdowns and Power keductions for Hadden Neck -(Continued)
DBE(D)/
N SIC (N)
Duration Power        Reportable                                                  Shutdown  System      Component  Event Datu                    (llrs)        (%)  Event                Description                  Cause Method        Involved    Involved  Ca tego ry 9/21/1972          85            100                Turbine / reactor trip due to a loss      1      3        ED        TRANSF    D2.3 of a constant voltage transformer 11/23/1972          73            0                  Repaired turbine lef t hand stop          D      1        HA        VALTEI    N1.1.4 valve 12/15/1972          0            70                  Reduced power. Plugging leaking          B      5        HC        HTEICH    N 1.1. 4 condenser tubes *                                  -
12/21/1972          0            70                  Power reduction. Plugging leaking        B      5        ..C        HTEICH    N1.1.4 condenser tubes 1
O e
ll1-
 
Table A1                                                                                                          1973 Forc d Shttdm:ns and Power Rc4uctions for Hadds:3 Nec k -(Contlaued)
_---------=                                                                _=_                                                                                                                                                                                                                                                                .
DBE(D)/
NSIC (N)
Duration Power                          Reportable                                                                                                                                                                                                                                                  Shutdown System  Co m ponent  Event
,            Da to                                                                    (Hru)            (%)                                    Event                                                                                                                                                                              Description                                  cause Hethod    Involved Involved    Ca tego ry 1/09/1973                                                      0              70                                                                                                                                              Power reduction. Plugsing main                                                                                                B      5        HC    HTEICH      N1.1.4 -
condenser tube leaks 1/25/1973                                                      0              52                                                                                                                                              Power reduction. Replacing level                                                                                              e      5        HH    YALVEI      N1.1.4 column lower isolation valve on B reheater drains tank 2/11/1973                                                      0              70      .                                                                                                                                        Power reduction. To permit                                                                                                    B      5        HP    HECFDN      N1.1.4 shutdown of BED circulating water pumps while a shear pia was                                                                                                                              ,
;                                                                                                                                                                                                                                                    replaced on B traveling water i                                                                                                                                                                                                                                                    screen 2/22/1973                                                      9              100                    Ao-73-2                                                                                                                Connector between 82 fcedvater                                                                                                  A      2        HH    YALVEI      D1.2 control valve stem and actua tor loosened, permitting tie valve to go fully open resulting in an uncontrolled invrease Ja 82 steam generator level 2/24/1973                                                      47            100                                                                                                                                            Nelded a broken steam inlet baffle                                                                                            B      1        HH    HTEICH      N1.1.4 plate on D soisture segarator reheater 4/02/1973                                                      0              52                                                                                                                                              Power reduction. Repacking heater                                                                                              B      5        HH    VALVEI      N1.1.4 drains tank normal level control valve 4/08/1973                                                      0              52                                                                                                                                              Power reduction. Renoied heater                                                                                                B      5        HH    VALVEI      N 1.1.4 d rains tank normal level control valve and replaced it with a temporary spool piece 6/02/1973                                                      366            100                                                                                                                                            Planned shutdown due tc turbine                                                                                                B      1        HA    TU R BI N  N1.1.4 vibration - replaced all sixth row blades 7/08/1973                                                      3023          100                                                                                                                                            Planned shutdova to in vesti' gate                                                                                            B      1        HA    TUDDIN      N1.1.4 increased turbino vibration.
Replaced 'both low pressure turbine rotors 12/21/1973                                                        0              0                                                                                                                                              Turbine balancing                                                                                                              B      4-      HA    TUREIN      N 1.1. 4 12/21/1973                                                        16            0                                                                                                                                              Added balance weights to                                                                                                      B      4        HA    TU R BIN    N 1.1. 4 t urbine/g enerator                                                                                                                                                            -
If 3                                                .
 
e  .
Table A1  1973 Forced Shutdowns and Power Reductions for Hadden Neck-(Continued)
DDE (D) /
N SIC (N)
Duration Power  Reportable          .
Shutdown  System      Component  Event Date              (Hrs)  (1)    Event            Descrip tion                Cause Nethod        Involved    Involved  Ca tego ry 12/29/1973      64      100              Performed additionai                    B        1        HA        TUR BIN  N 1.1. 4 turbine / generator balancing
                      )
II+
 
Tabio A1                                                              1974 Forced Shutdowns and Power Reductions for Hadden Neck -(Continued)
                                                                                                                                                                                                                                        . DDE (D) /
N SIC (N)
Duration Power                                Reportable                                                                                                            Shutdown        Systen  Coatonent  Event Date                            (Hrs)                                  (%)  Event                                                                        D escrip tion                Cause Bothod            Involved Involved  Category 1/10/1974                  7                                      50                                                                          Frozen sensing lines tc steam flow      A      3              IA    INSTR 0  M 9. 2 transmitters produced spurious signal 1/19/1974                  5                                      50  10-74-2                                                                Ice stora shorted protective relays      A      3              EA    RELAYI    M9.2 causing loss of of f-site poder 1/19/1974                  4                                      50  10-74-3                                                                operator inadvertently shut down        G        3              HF    PURPIX    N6.1 two circulatin) water gunps                                                                  .
supplying the same con denser 2/16/1974                  12                                      50                                                                          Repaired leaking flange on 84            A      1              UH    VALVEI    N1.1.4
    ,                                                                                                                                                      feedwater control valve 1/23/1974                  660                                    50                                                                          Increasing vibration in turbine due      A      1              HA    TURBIN    N1.1.4 to broken blades 4/30/1974                  4                                      50                                                                          Vibra tion in turbine                    B      2              UA    TU R BIN  N 1.1. 4 4/20/1974                  4                                      50                                                                          Vibration in turbine                    B      2              HA    TU B BIN  N 1.1.4 e
O/20/1974                  4                                      50                                                                          Vibration in turbine                    B      2              HA    TU R BIN  N 1.1. 4
        ,4/20/1974                  8                                      50                                                                          Vibration in turbine                    B      2              HA    TU R BIN  N1.1.4 4/20/1974                  6                                      50                                                                          Vibration in turbine                    B      2              UA    TUR BIN  N1.1.4 6/24/1974                  9                                      50                                                                          Defective capacitor in Loop 82 flow      A      3              IA    INSTBU    N1.1.4 transmitter initiated reactor trip                -
signal 9/08/1974                  9                                      50                                                                          Sepaired turbine eccentricity            A      1              HA    TU R BIN  N1.1.4 12/08/1974                    12                                    80                                                                          Lightning f aulted tranraission          H      3              EA    ELECON    N9.2 lines causing generator load rejection
                                                                                                                                                                                                                                                          ~
U5
 
                                                                                                                                                                                            .)
Table A1. 1975 Forced Skatdowns and Power Redactions for Hadden Neck-((butinued)
                  --------        _ = .            _                                  ----------        --  ----      ---------------          -
DB E (D) /
MS?C(u)
Duration P ow er                  Reportable                                                  Shutdova      System      Co mpon ent        Event Dats                          (Hrs)            (1)            Event                  Descrip tion                Cause Method          Involved    Involved          Category
  --------------                                        --          -                                  a                                          __-                -
2/01/1975                16              0                          Trip from low feed pump section            1          3        HH        PUR PII          D2.7 pressere 3/26/1975                39              50              10-75-1    Packing gland leakage from letdown        1          3        CB        TALTEI            31.1.4
                                                      ,                  system stop valve to the valve sten leakoff header was in escess of adelaistrative limits                                -
7/05/1975                5                50                          Dait forced off line by broken oil        &          3        RA        PIPEII            D 2. 3 pressure gange line on turbine 7/14/1975                3                50                          Onit forcel off ilme by leaking            &          3        R1        PIPEII            D2.3 auto-stop 11ae on turbine
,  12/06/1975                7                80                          Repaired leaking tebes in feeduater        B            1        HH        HfEICE            E 1.1. 4 heaters Ilb
 
Tablo 11  1976 Forcad Shutdowns and Power Reductions for Hadden Neck-(Continued)
DE E (D) /
N SIC (N)
Du 4 tion P ow er              Reportable                                                  Shutdown  Systea        Co m ponent  Event Date                              (Ilcs)                (%)      Event            Description                  Cause Nethod        Involv ed    Involved    Category
---------------- _                                    ==---      __ --            -----                                                    _              _
1/22/1976                    17                  100    LER-76-1    Frozen senslag line caused steam        A        3          IA        PIPEII      N9.2 line break signals which tripped unit off line 4/02/1976                  37                    100                  Broken steam faffle in D moisure        A        ,1          HH        VESSEL      N1.1.4 separator. Welded back to original condition 4/38/1976                  6                    70                  Spurious signal from the low            A        3          IA        INSTRU      N 2.4 pressure scram calcula tors 0/01/1976                    13                  100                  Lightning strike on 345 Ky line          H        3          EA        ELE CON    N9.k resulting in plant trip 9/10/1976                  7                    100                  Unit trip caused by coclant pu mp      G        3          CB        PUR PII    N 6.1 shutdown due to operator error o
O e
II)                                                                      ,
 
I i
Table A1  1977 Forced Shutdowns and Power Reductions for Hadden Neck-(Continued)
DDE(D)/
M SIC (N)
Duration Power  Reportable                                              Shutdown  System      Comtonent            Event        '
Datu                (!!r s)  (%)  Event            Description                Cause Method        Involved. Involved              Category
, C/19/1977          140      70              Feedvater heater leak corrected          B      1        HH        llTEICH            N1.1.4 general plant asiatenarce during o utage                                              s 9/10/1977      11        100              Generator voltage rege]ator              A      3        HA        GENERA              N1.1.4 aalfunction 10/09/1977      7        100              Turbine load mismatch caused- by a      A      3        HA          VALVEI            N 2.1 control valve malfunction 12/01/1977      5        0    LER-77-26  Niring error la main steam line          A      3        HB          ELECON            N5.1 trip valve circuitry 4    12/03/1977      7        100              Generator voltage regulator              A      3        HA          GENERA            N1.1.4 malf unction
'12/10/1977          31        100              Generator voltage regulator probten      B      4        la        GENERA            N1.1.4
.;                                              investigation i
! 12/14/1977          14        90              Turbine balance                          B      4        NA        TU R BIN          N1.1.4 12/15/1977      18        10              Turbine balance                          B      4        HA        TURBIN            N1.1.4 12/17/1977      22        90              Turbine balance                          B      4        HA        TU R BIN          N1.1.4 12/27/1977      7        90              Turbine balance                          B      4        HA        TU R BIN          N 1.1. 4 12/10/1977      22        100              Turbine balance                          B      4        HA        TU R BIN          N 1.1. 4 Its-
 
Table A1  1970 ForcId Shutdsens anil P:ccr its4uctions fcr Ildloa Neck-(Contirued)
                                                                          -u DDE(D)/
N SIC (N)
Duration Power          Reportable                                                Shutdown    System      Component  Event Date                    (Ilt s)  (%)      Event              Description                  Cause Method        Involved    Involved  Category 1/01/1970          12          0                  Plant trip due to stuck relay              A      3          IA        INSTRU    N 2.1 1/02/1970          7            100                Balancing turbine                          B      1 '        HA        TURDIN    N1.1.4 1/09/1970          27          100                Revelded a loose floor plate in B          B      1          Hil      llTEICH  N1.1.4 moisture separator reheater 1/20/1970          51          100                Repairing B steam generator feed            D      1          HD        PUHEII    N1.1.4 pump bearing 2/13/1978          42          00                  Revelded haffle plates in the              B      1          Hit      VESSEL    N1.1.4 moisture separators 3/24/1970          23          100      LER-78-2  Replacing electrical tcrainal block        F      1          EU        ELECON    N1.1.4 enclosure in the containment 3/30/1973          6            50                  Reactor was shut down to comply            H      1          CD        PIPEII    N1.1.4 with procedure for placing an isolated loop back in service 4/30/1978          6            100                Nhile bringing an isolated loop            B      3          IA        INSTRU    N1.1.4 into service, t he 8 2 s team generator experienced a mismatch of steam flow with feed flow coinciden t with low ficv in steam genera tor 5/01/1978          3          100                Nhile turning 4160Y bus voltaetor          A      3          IA        INSTRU    N2.2 f ound "of f" to positior 1 5 2 f uses supplying loop Nc. 1 a nd No.
2 flow indication blev causing loss of flow reactor trip 6/04/1978          30          1.00                Nelding looso ,baf fle plate on B          B      1          IIA      TESSEL    N1.1.4 aoisture separator rebeater l  6/17/1970          66          100                Plant design ch ange No. 270                D      1          ED        ELECON    N 1.1. 4 l                                                      required the installation of heat shrunk sleeves on elec trical penetrations 7/30/1978          0            60                  Power reduction. Replacing heater          D    5          Illi      'UnPII P        N1.1.4
* drain tank. pump seal
                                                                                                                                                  ~
8/20/1970          12          100                Repaired leaking, crodtd dra in            A    2          lill      PIPIII    N 1.1. 4 piping on moistere separator                                                                  .
reheaters
 
Table A1  1978 Forced Shutdowns and Power Re luct ions for fladlem Neck-(Continued)
          - _ - - - - - - - - = _                                                                ,
                                                                                                                                      .            DDE(D)/
N SIC (N)
Duration Power          Reportable                                                Shutdown    Systen      Component  Event Date                                  (firs)  (%)  Event            Description                  Cause Method          Involved    Involved  Category 9/14/1978                        0        52              Power reduction. For saintenance          A        5          IIB      PUMPII. N1.1.4 on B steam generator f eed pu mp 11/02/1978                        3        100              Low pressure pressurizer trip due        B        3          IA        INSTRO    N2.4 to false signal while instrumentation check la progress e
4 i                                                                                      l'LD
 
Table A1    1979 Forced Shutdonna and Power Reductions for Hadden Neck-(Continued)
DBE(D)/
NSIC (M)
Duration Power    Reportable                                                                                                                                          Shutdown  System        Co m ponent    Event
,                    DSte                                                                            (Hrs)    (1)  Event                                                            Description                                                    Cause Method              Involved      Involved      Category 3/12/1979                                                        1      0                    saintenance on electrical equipment                                                                                                B  9        ED            EL ECON      N1.1.4 3/12/1979                                                          3        0                    Turbine balance                                                                                                                    B  9        HA          TURBIN        N1.1.4 3/14/1979                                                        0        40                  Power reduction. Replacing 811                                                                                                      B  5        HH          PUN PII        M1.1.4 condensate puay 3/17/1979                                                        0        52                  Power redaction. Repairing turbine                                                                                                  B  5        HA          TURBIN        N1.1.4 flange leak S/18/1979                                                          0        52                  Power redaction. eplacing outboard                                                                                                  B  5        HD          PDH PII        N1.1.4 pump seal on 11 steam generator j                                                                                                                                feed peep 6/02/1979                                                          0        60                  Power reduction. Repairing leak on                                                                                                  B  5        HD          FESSEL        N 1.1. 4 84 steam generator hand hole 7/14/1979                                                          0        62                  Power redactica. Shutdbva of 83                                                                                                    B  5        CB          PUN PII        N3.1 loop because of leaking seal on 83 reactor coolaat pump 7/21/1979                                                          30      60                  51ssatch os low pressure steam damp                                                                                                A  3        HE-          INSTED        N2.4 systen 9/29/1979                                                          234      100                  Check weld area of 5/G feed line                                                                                                    D  1        HH          PIPEII        M 8. 3 nozzles for cracks e
Ill/                                                                                                                    .
1
 
i a
1 Table A1        1980 Forced Shutdowns and Power Reductions for Hadden Neck-(Continwd) 1 DBE (D) /
a SIC (N)
Duration power                Reportable                                                      Shutdown    System      Com ponent    Event i
Date                      (Hrs)    (5)                  Even t                  Descrip tion                cause Nethod        Involved      Involved  Oategory 3/19/1980          0        60                                      Power reduction. Plugging two          B        5        HC          PIPEII    31.1.4 tubes each le mala condenser water i                                                                                              boxes C & D l
l l
3/20/1980          0        22                                      Power reduction. Plugging two          B        5        BC          STEIC8    N1.1.4 tubes in main condenser water bor B 3/27/1980          11        100                                    Reactor and techine trip was            B        3        RI          ELECON    D2.3 experlesced declag/ wiring modification per SUREG 0578 4/26/1980          0        56          ,                          Power redactica. . Nater la lobe        B        5        RB          PURPII    N1.1.4 system of sala steam generator feed pump                                          ,
8/02/1980          19      5                                      Reactor and turbine trip due to        G        3        RA          INSTRU    D2.3 overspeed trip setting improperly adjusted 1                          8/05/1980          15      51                                      Shutdova in order to tie la Loop 2      F        1        CB          PDEPII    B1.1.4 i                                                                                              af ter 42 reactor coolant pump l                                                                                              repair
;                          9/27/1980          65        8                                      Turbine balance                        B        1        R&          TO R BIN  N1.1.4 11/18/1983            14      31                    LER-80-16        While stopplag in control back          A        2        RB          CEDRVE    D4.3 l                                                                                              rods, one step, both audible and l                                                                                              visual alaras indicated two dropped
!                                                                                              rods - notable gripper coils were at fault 11/20/1983            33        15                                    Rechanical overspeed device on H.P. H        3        HA          INSTRO    E5.2 turbine out of adjuntaent -
adjusted device and came back on 11ae 11.lt
 
i Table A1    1981 Forcad Shutdssns aad Po:ct Esductions fer Haddzo Neck-(Cortinued)
                                                          ',    ,                                                                                                                      DD E (D) /
NSIC (N)
Duration Pow er                  Reportable                                                    Shutdown            System    Co m ponent  Event Date                            ,
(Hrs),        (%)                Event.              Descrirlion                    cause Method              Involved  Involved    Category
      -                      =--------                                                                . - - - -    -                              _                    -            -
1/04/1981                        5                100                            Steam generator low level alara              A    2                HB      TESSEL      N3.2 1/05/1981                        ~2                                              Flooding of feedwater beater                  A    2                MH      HTEICH      N1.1.4 2/27/1981                          10              100                            Plant trip due to coattol air                A    1                PA      PIPEII      D 2. 7 header fitting amparation which caused loss of feedwater control 3/09/1981                                          100-80                        Power red action for valve test and          B    5                BC      HTEICH      W1.1.4 tube plugging La condenser "Ba, "C"
)                                                                                          water box 7/25/1981                                          100-75                        Power reduction and three loop                A    5                CD      TALTEI      N 3.1 oleration due to valve sten leak 7/29/1981                          39              25                            Reactor and turbine trip while                H    3                HE      RELAY 1    D2.1 coming down la power to bring plant o f f-line.      Trip due to low pressure steam dump aalfunction caused by OPC relay 63 8/23/1981                          47                                            Reactor shutdova to repair valve              A    2                RI      VALTEI      N3.1 packing leak
                                                                                                                                                                                    ~
9/10/1981                          10              95                            Plant manually tripped due to                A    2                HA      VALVEI      N1.1.4 spurious right hand turbine stop valve closure 10/01/1981                          31              10                            acactor scran during AERR                    B    3                IA      INSTRO      N1.1.4 f unctional test 10/02/1981                          0              10                            Power reduction due to offgas                A    5                MD      UNK NNN    N1.1 activities l      11/12/1981                          5                                              Reactor and turbine samually                  A    1                CB      PU R PII    N6.1 tripped while attemptire to transfer reactor coolant pumps to station service water 12/11/1981                          82              90                            Nhile reducing power to plug ' B'            A    3                HA      T A LYEI    D2.3 waterbox candenser tubes and for scheduled turbine main tenance,                                                                          .
erratic operation of t urbine ontrol valves caused turbine everspeed                                                                      .
trip 12,3
* 1
 
l Table 11  1981 Forced Skatdowns and Power Reductions for Haddes Neck-(Continued)
_                  =----_-_-___                                                  ____.                                          ______                                          _______
DDE (D) /
NSIC (N)
Duration Power        Boportable                                                                Shutdown    System          Co m ponent  Event Date                                                                    (Itrs)  (%)                            Event          Description                  Cause Bethod          Involv ed      Involved    Category
___-_-------=-_                                                                                                      __
12/22/1981                                                          12      100                                    Reactor and turbine trip from high      1        3              PA        PIPEZI      D2.3 pressure heater drain tank level due to failed fitting on control air systen 12/23/1981                                                            5                                                Turbine generator off line to          A        1              HD        FALTEI      N 3. 2 repair staan leak on MCY36 114
 
Table A1    1902 Forcsd Shttdowns and Power Reductions fcr Heddsc Neck-(Cortinued)
DB E (D) /
HbIC (N)
Duration Power  Reportable                                                Shutdown  System        Co m pon ent  Event
* Date                    (Hrs)  (%)    Event              Description                  Cause Method        Involved      Involved    Category 1/12/1982        0                        Load reduction due to condenser in        A        5        HC          HTEICH      N1.1.4
                                                - (leakage) 1/21/1982        0                        Reduced power to plug tubes in "D"        A        5        HC          HTEXCH      N1.1.4 and "B" waterboxes 1/31/1982        18                        Turbine and reactor trip. Trip            A        3        ZZ          ZZZ ZZZ      D2.3 caused by loss of generator field.
Located six blown f uses on main exciter 3/04/1962        0                        Reduced power for repair of leaking        A        5        HC          HTEICH      N1.1.4 condensor tubes 4/24/1902        0                        Reduce power to repair: (A)                A        5        CH          PD H PII    N 1.1. 4 Vibration on 1B steam Senera tor feed pump; (B) Leaking steam generator inspection hand hold on 8 3 SG; (C) Check for tube leaks in all four waterboxes S/14/1982        0                        Load decrease to 400 MUE to check          A        5        HC          HTEICH      K1.1.4 for condenser tube leakage 6/04/19C2          132.7                    Reactor 5 turb trip due to short          A        3        HA          GENERA      D2.3 circuit in exciter. Ecpaired short c ircuit. Also, 81 RSIT would not close. Repaired and retested valve 7/01/1982        0                        Load decrease to repair extraction        A        5        HB          TU R BI N    N1.1.4 line leak on H.P. turbine 9/17/1982        195.1        82-06/3L  Moisture in main trans former oil.        B        1'      EB          TRANSF      N1.1.4 Filtered oil, repaired leaks, tested and returned to service.
Also found battery plates had swelled resulting in cracking of casing. Replaced battery 9/20/1902        0                        Reduced power to plug condenser            A        5        HC          HTEICH      N1.1.4 t ubes                                                                                              ,
11/08/1982          10.4                    Main feel pump trip. Cue to loss      A        3      HD          PU H PIX    D 2.1      ,
of suction. Verified system componemtn operating properly                                                                      .
IM
 
l l
l l
Table A1      1982 Forced Shutdowns and Power Reductions for Hadden Neck-(Continued)
_                - __            -----                =            __          --------------                      --
DBE(D)/
NSIC (N)
Du rat i on Power    Reportable                                                      Shutdown  Systes                Co m pon ent    Event Dato                    (Hrs)        (1)    Event                Descrip tion                  Cause Method        Involv ed            Involved        Category 11/13/1982            39.2                                Turbine right hand trit valve would      A        1            HA              MECFUN          N1.1.4 not open. The pia . holding the disc to the sten sheared and was replaced 11/17/1982            9.8                                Bank "C" rods dropped during rod          A        2            IA              CBDRDE          D4. 3 action checks. Cause undete rmined 11/17/1982            2.3                                FCP transfer greater than 10%            G        3            CB                PUNPII          N6.1 power. Discussed with opera tors 12/12/1982          0                                  Load reduction for monthly turbine        B        5            HA              VALTEI          N1.2.4 stop valve test 9 / 2_6
 
                                                                                                                                                      \
i l
l 1
Table A1  1903 Forced Shutdowns and Power Reductions for Hadden Neck -(Continued)
DDE(D)/
NSIC(N)
Duration Power                                                Reportable                                                Shutdown    System      Co m pon ent    Event Date                                                (Hrs)          (%)                                          Event            Description                  Cause Bethod        Involved    Involved        Category 4/12/1983                                9.9                                                                    overspeed turbine trip test              C        2          HA        TUEBIN          N1.2.4 4/12/1983                                4.0                                                                    Inadvertent loss of poher to RCP        G        3          CD        CKT BRK        #2.2 bus attempting to reset control switch position flags 5/31/1983                                7.4                                                                    Spurious p3ver range instrument          H        4          IE        INSTRO          N 2. 4 spike 6/10/1983                                11.5                                                                    82 feed rojulating valvo failed          A        2          HH        HECFUN          N1.1.4 open - repaired leakage 7/07/1981                              0                                                                      Load reduction to repair leak on        A        5          CC        VALVEI          N1.1.4 steam 9enerator level Indication isolation valve I17 If                                                                            .
 
                                                                                                                                                                                    ~.
Table A1      1984 Forced Shutdovas and Power Roductions for Hadden Neck-(ibntinnd)
DDE (D) /
N SIC (N) i                                        Duration P ow er            Reportable                                                  Shutdown  System        Co m ponent  Event Date                                                (lles)  (1)      Event                Description                Cause Method        Involved      Involved    Category l                __---------- .                              ---                                                                                      --_
!        5/05/1984                            0                                    6" drain line from MSR to heater      B        5          HJ          PIPEXI      N1.1.4 d rains tank developed a leak.
Beduced power to 65% to repair leak
. 11/09/1984                                    12.0                                High hydrogen temperature deviation    A        1          EB          GENERA      N1.1.4 11/10/1984                                  55.9                                  Took generator off line for            B        1          EB          GE N ER A  N1.1.4 hydrogen seal repair and turbine overspeed trip test 11/15/1984                                    11.1                  84-026        nanual trip - reduce Icad due to      A        2          EB          G E N ER A  N2.2 i
voltage regulator cycling
!  11/20/1984                                  7.0                    84-025        Loss of f13e laadvertent shutdown      G        3          ZZ          IIIIII      N 3.1 of number three reactor coolant Pump l
I 4
1 e
                                                                                                      ' l (1L3'
 
Table A.2. Codes used for classifying the causes of forced shutdowns and power reductions and also for classifying the methods of shutdown Causes A    Equipment failure B    Maintenance or testing
* C    Refueling D    Regulatory restriction E    Operator training and license exams                            .
F    Adminis tra tive G    Operational error H    Other Methods 1    Manual 2    Manual scram C[
3    Automatic scram                                                                  --
4    Continuation 5    Load reduction 9    Other 1
 
e    s a
Table A.3.                                  Systems involved in forced shutdowns and power reductions System                                                Code Reactor                                                                                                                  RX Reacter vessel internals                                                                                              RA Reactivity control systems                                                                                            RB Reactor core                                                                                                        RC Reactor coolant and connected systems                                                                                    CX Reactor vessels and appurtenances                                                                                    CA Coolant recirculation systems and controls                                                                          CB Main steam systems and controls                                                                                      CC Main steam isolation systems and controls                                                                            CD Reactor core isolation cooling systems and controls                                                                  CE Residual heat removal systems and controls                                                                          CF Reactor coolant cleanup systems and controls                                                                          CG Feedwater systems and controls                                                                                      CH Reactor coolant pressure boundary leakage detection systems                                                          CI Other coolant subsystems and their controls                                                                          CJ Engineered safety features                                                                                              SX i
~
Reactor containment systems                                                                                          SA                  o Containment heat removal systems and controls                                                                        SB                  en Containment air purification and cleanup systems and controls                                                        SC Containment isolation systems and controls                                                                          SD Containment combustible control systems and controls                                                                  SE Emergency core cooling systems and controls                                                                          SF Control room habitability systems and controls                                                                        SG Other engineered safety feature systems and their controls                                                            SH Instrumentation and controls                                                                                            IX Reactor trip systems                                                                                                IA Engineered safety feature instrument systems                                                                          IB Systems required for safe shutdown                                                                                    IC Safety-related display instrumentation                                                                                ID Other instrument systems required for safety                                                                          IE Other instrument systems not required for safety                                                                      IF Electric power systems                                                                                                  EX Offsite power systems and controls                                                                                  EA l                AC onsite power systems and controls                                                                                  EB DC onsite power systems and controls                                                                                EC Onsite power systems and controls (composite ac and de)                                                              ED Emergency generator systems and controls                                                                            EE i                Emergency lighting systems and controls                                                                              EF
!                Other electric power systems and controls                                                                            EG l
l i
 
                                                                                            . i Table A.3 (continued)
System                      Code Fuel storage handling systems                                    FX New fuel storage facilities                                  FA Spent-fuel storage facilities                                FB Spent-fuel pool cooling and cleanup systems and controls      FC Fuel handling systems                                        FD Auxiliary water systems                                          WX Station service water systems and controls                    WA Cooling systems for reactor auxiliaries and controls          WB j                      Demineralized water makeup systems and controls              WC Potable and sanitary water systems and controls              WD Ultimate heat sink facilities                                WE Condensate storage facilities                                WF Other auxiliary water systems and controls                    WG Auxiliary process systems                                        PX Compressed air systems and controls                          PA Process sampling systems                                      PB
,                      Chemical, volume control, and liquid poison systems and      PC l
controls l                      Failed-fuel detection systems                                PD        Os 4
Other auxiliary process systems and controls                  PE        -
Other auxiliary systems                                          AX Air conditioning, heating, cooling, and ventilation sys tems  AA and controls Fire protection systems and controls                          AB Communication systems                                        AC Other auxiliary systems and controls                          AD Steam and power conversion systems                              HX Turbine-generators and controls                              HA Main steam supply systems and controls (other than CC)        HB Main condenser systems and controls                          HC
,                      Turbine gland sealing systems and controls                    ED l
Turbine bypass systems and controls                          HE Circulating water systems and controls                        HF Condensate cleanup systems and controls                      HG Condensate and feedwater systems and controls (other than CH) HH Steam generator blowdown systems and controls                HI Other features of steam and power conversion systems (not    HJ included elsewhere) 1
  - - - =  ,w.,,w-  -  ,w.-..-,.  ,,.w_,,.__-.
 
        , e -              -
a  .
Table A.3 (continued)
System                        Code Radioactive waste management systems                            MK Liquid radioactive waste management systems                  MA Gaseous radioactive waste management systems                MB Process and effluent radiological monitoring systems        MC Solid radioactive waste msnagement systems                  MD Radiation protection systems                                    BX Area monitoring systems                                      BA Airborne radioactivity monitoring systems                    BB m
l e
I
 
                                                                                        .      o Table A.4. Components involved in forced shutdowns and power reductions Component type                    Component type includes          Code Accumulators                        Scram accumulators, safety injection  ACCUMU tanks, surge tanks, holdup / storage tanks Air dryers                                                                  AIRDRY Annunciator modules                  Alarms, bells, buzzers, claxons,      ANNUNC horns, gongs, sirens Batteries and chargers              Chargers, dry cells, wet cells,        BATTRY storage cells Blowers                              Compressors, gas circulators, fans,    BLOWER Ventilators Circuit closers /interruptors        Circuit breakers, contactors, Con-    CKIBRK
                                -      trollers, starters, switches (other than sensors), switchgear Control rods                        Poison curtains                        CONROD Control rod drive mechanisms                                                CRDRVE wN Demineralizers                      Ion exchangers                        DEMINX
{}
Electrical conductors                Bus, cable, wire                      ELECON Engines, internal combustion        Butane, diesel, gasoline, natural      ENGINE gas, and propane engines Filters                              Strainers, screens                    FILTER Fuel eleents                                                                FUELXX Generators                          Inverters                              GENERA Heaters, electric                    Heat tracers                          HEATER Heat exchangers                      Condensers, coolers, evaporators,      HTEXCH regenerative heat exchangers, steam generators, fan coil units Instrumentation and controls        Control 11ers, sensors / detectors /  INSTRU elements, indicators, dif ferentials integrators (totalizers), power suppl 11es, recorders, switches, transmitters, computation modules Mechanical function units            Mechanical controllers, governors,    MECFUN gear boxes, varidrives, couplings Mo tors                              Electric motors, hydraulic motors,    MOTORX Pneumatic (air) motors, servomotors
 
Table A.4 (continued)
Component type                    Component type includes              Code Penetrations, primary containment    Air locks, personnel access, fuel          PENETR handling, equipment access, elec-trical, instrument line, process P iiP ng Pipes, fittings                                                                  PIPEXX Pumps                                                                            PUMPXX Rec 6mbiners                                                                    RECOMB Relays                              Switchgear                                  RELAYX Shock suppressors and supports      Hangers, supports, sway braces /            SUPORT stabilizers, snubbers, antivaibra-tion devices Transformers                                                                    TRANSF Turbines                            Steam turbines, gas turbines, hydro        TURBIN turbines Valves                              Valves, dampers                              VALVEX Valve operators                    Explosive, squib                            VALV0P                [(~
Vessels, pressure                    Containment vessels, dry wells,            VESSEL pressure suppression chambers, pressurizers, reactor vessels Other components                                                                XXXXXX Codes not applicable                                                            ZZZZZZ f
l l
1 i
 
_~_.                      .  . _ . .                  -- -              _ _ _ . - _____ _
                                                .                                                                                  '\
i Table A.S.      Initiating event descriptions for DBEs as listed in Chap. 15. Standard Reviso Plan (Revision 3) i
: 1.      Increase in heat removal by the secondary system j                                      1.1 Feedwater system malfunction that results in a decrease in feedwater temperature                                                                  {
1.2 Feedwater system malfunction that results in an increase in feedwater flow 1.3 Steam pressure regulator malfunction or failure that results in                            l l                                            increasing steam flow l                                      1.4 Inadvertent opening of a steam generator relief or safety valve                            l l                                      1.5 Spectrum of steam system piping failures inside and outside of i                                            containment in a pressurized-water reactor (PWR)                                        i l                                      1.6 Startup of idle recirculation pump a l                                      1.7 Inadvertent opening of bypass resulting in increase in steam flow"
: 2.      Decrease in heat removal by the secondary system 2.1    Steam pressure regulator malfunction or failure that results in decreasing steam flow 2.2 Loss of external electric load 2.3 Turbine trip (stop valve closure) 2.4 Inadvertent closure of main steam isolation valves N
2.5 Ioss of condenser vacuus 2.6 Coincident loss of onsite and external (offsite) ac power to the station 2.7 Ioss of normal feedwater flow 2.8 Feedwater piping break 2.9 Feedwater system malfunctions that result in an increase in feedwater temperatures'
: 3.      Decrease in reactor coolant system flow rate 3.1 Single and multiple reactor coolant pump trips 3.2 Boiling-water        reactor  (BWR)  recirculation      loop controller malfunction that results in decreasing flow race 3.3 Reactor coolant pump shaft seizure 3.4 Reactor coolant pump shaft break
: 4.      Rasetivity and power distribution anomalies 4.1  Uncontrolled control rod assembly withdrawal from a suberitical or low-power start-up condition (assuming the most unfavorable reactivity conditions of the core and reactor coolant system),
including control rod or temporary control device removal error during refueling 4.2 Uncontrolled control rod assembly withdrawal at the particular power    level    (assuming    the  most      unfavorable  reactivity conditions of the core and reactor coolant system) that yields the most severe results (low power to full power) 4.3  Control    rod  maloperation      (system malfunction or operator error), including maloperation of part length control rods
 
e A.5  (continued) 4.4 Start-up of an inactive reactor coolant loop or recirculating loop at an incorrect temperature 4.5 A malfunction or failure of the flow controller in a BWR loop that results in an increased reactor coolant flow rate 4.6 Chemical and volume control system malfunction that results in a decrease in the boron concentration in the reactor coolant of a PWR 4.7 Inadvertent loading and operation of a fuel assembly in an improper position 4.8 Spectrue of rod ejection accidents in a PWR 4.9 Spectrum of rod drop accidents in a BWR
: 5. Increase in reactor coolant inventory 5.1  Inadvertent operation of emergency core cooling system during
;                                                power operation.
5.2 Chemical and volume control system malfunction (or operator error) that increases reactor coolant inventory 5.3 A number of BWR transients, including items 1.2 and 2.1-2.6
: 6. Decrease in reactor coolant inventory 6.1  Inadvertent opening of a pressuriser safety valve in either a                                %
t PWR or a BWR                                                                                  m 6.2 Break in instrument line or other lines from reactor coolant pressure boundary that penetrate containment 6.3 Steam generator tube failure 6.4 Spectrum of                  BWR steam system piping failures outside of containment 6.5 ! ass-of-coolant                        accidents resulting from the spectrue of postulated piping breaks within the reactor coolant pressure boundary, including steam line breaks inside 'of containment in a BWR 6.6 A number of BWR transients, including items 1.3, 2.7, and 2.8
: 7. Radioactive release from a subsystem or component 7.1 Radioactive gas waste system leak or failure
,                                          7.2 Radioactive liquid waste system leak or failure
!                                          7.3 Postulated radioactive releases due to liquid tank failures
!                                          7.4 Design basis fuel handling accidents in the containment and                                          1 l                                                spent fuel storage buildings                                                            ,
)                                          7.5 Spent fuel cask drop accidents i                                      8. Anticipated transients without scram 8.1  Inadvertent control rod withdrawal 8.2 Loss of feedwater 8.3 toss of ac power 8.4 loss of electrical load 8.5 Loss of condenser vacuus                                                                            j i                                          8.6 Turbine trip 8.7  Closure of main steam line isolation valves aThese initiating events were added for BWRs to be more specific                                      !
than DBE events 5.3 and 6.6.
 
A.6.          NOAC event categories for non-DBE shutdowns N 1.0 Equipment failure N 1.1                Failure on demand under operating conditions N 1.1.1 Design error N 1.1.2 Fabrication error N 1.1.3 Installation error N 1.1.4 End of design life / inherent failure / random failure N 1.2 Failure on demand under test condii; ions N 1.2.1 Design error N 1.2.2 Fabrication error N 1.2.3 Installation error N 1.2.4 End of design life / inherent                                                          failure / random i
failure                                                                  .
N 2.0 Instrumentation and control anomalies N        2.1        Hardware failure N        2.2        Power supply problem N        2.3        Setpoint drift N        2.4        Spurious signal N        2.5          Design inadequacy (system required to function outside design specifications                                                                                                    g N 3.0 Non-DBE reductions in coolant inventory (leaks)                                                                                                      D N 3.1 In primary system N 3.2 In secondary system and auxiliaries iI                                N 4.0 Fuel / cladding failurs                                                                          (densification, swelling,      failed fuel l                                              elements as indicated by elevated coolant activity)
N 5.0 Maintenance error N 5.1 Failure to repair component / equipment / system N 5.2 Calibration error l                                  N 6.0 Operator error
;                                              N 6.1                  Incorrect action (based on correct understanding on ,the i
part of the operator and proper procedures, the operator
;                                                                    turned the wrong switch or valve - incorrect action)
N 6.2 Action on misunderstanding (based on proper procedures
;                                                                    and improper understanding or misinterpretation on the
:                                                                    operator's part of what was to be done                                                              -
incorrect action)
N 6.3                  Inadvertent action (purpose and action not related, for j                                                                    example, bumping against a switch or instrument cabinet)
N 7.0 Procedural / administrative error (incorrect operating or testing procedures,                        incorrect analysis of an event                                                    -
failure  to consider certain conditions in analysis) t
  ,--  -m.,,_.-,,-,,.,_,,,-----g                      . , _ ,          , , - - - , . , - , - - , . - , . , , , . , , ,
 
      .      o Table A.6 (continued)
N 8.0 Regulatory restriction N 8.1 Notice of generic event                                                                                                                          ,
N 8.2 Notice of violation                                                                                                                              1 N 8.3 Backfic/ reanalysis
;                N 9.0 External events N 9.1 Human induced (sabotage, plane crashes into transformer)
N 9.2 Environment induced (tornado, severe weather, floods, earthquake)
N 10.0 Environmental operating constraint as set forth in Technical Specifications s
m l
) i V.-_..-------.,_,--,.,.-----        - - . _ _ . - - . . - - . , _ . - . - _ . , - ,_ , , - . - .      - - _ , , , , , , , - - , _ _ , , , _ . ~ - - - - , ~.
 
APPENDIX B REVIEW OF REPORTABLE EVENTS This appendix presents the Haddam Neck data on reportable events in narra tive and tabular format and lists informa tion sources.        It des-cribes how the information was encoded and how significance screening criteria were applied.
B.1  Scope 342 reportable events tha t occurred at the Haddam Neck plant from 1967 to 1984 were reviewed. The events include reportable occurrences (R0s), abnormal occurrences ( A0s ) ,
* and licensee even t reports (LERs) e filed by the utility resulting from technical specification viola-                ~
tions. In addition, some events that occurred prior to 1975 but which do not fit in the above classifications, are included since they are signilicant from a safety standpoint. The information contained in the reportable events was coded in the format discussed later in this sec-tion. Tables of coded reportable events, arranged by year, are pre-sented in Table B.1.
This studf reviewed information about operating events reported in LERs and LER predessors (e.g., AORs, unusual events reports, reportable occurrences (R0s)] . Da ta on these types of events were retrieved from the NOAC data files. Also, any documents that contained LER-type infor-mation (such as equipment failures or abnormal events) were included in
        *These report designations are to be distinguished from the events included in NUREG-0090, Reporta to Congress on AbnormL Occurrences.
 
the review to ensure that a total picture of the plants operating istory was  obtained. Various    types                          of      opera ting repor ts                and general correspondence were involved this way.
The table of reportable events (Table B.1) contains the following information for each event reviewed:
: 1. LER number or other means of identification of report type,
: 2. NSIC accession number (a unique identification number assigned to each document entered into the computer file),
: 3. date of the event,
;        4. date of the report or letter transmitting the event description,
: 5. status of the plant at the time of the occurrence (Table B.2),                                                                                      t
: 6. system involved with the reportable event (Table B.3),
: 7. type of equipment involved with the reportable event (Table B.4),
: 8. type of instrument involved with the reportable event (Table B.4),
: 9. status of the component (equipment) at the time of the occurrence (Table B.2),
;      10. abnormal condition associated with the reportable event (e.g., cor-rosion, vibration, leak) (Table B.5),
: 11. cause of the reportable event (Table B.2),
: 12. significance of the reportable event, and
: 13. comments and/or details on the event.
i B.2                  Data Sources 1
Thr N6aC files of LERs (including the Sequence Coding and Search System) were the primary source of information for the review of report-                                                                                    l I
able events. When additional informa tion on the event was needed, the                                                                                    ,
J m-- -- . . . - . - - _ _ . - . - , , , , . . . - , - - - ~------m..
 
original LER (or equivalent) was consulted by examining (1) those full-sized copies on file at NOAC (for the years 1976 -1984); (2) the micro-fiche file of docket material at NOAC; or (3) the appropriate operating report (semiannual, annual, or monthly).
Printouts ob tained from the computer files identified " docket material" other than reportable event reports.                          This included licensee correspondence with NRC (or the Atomic Energy Commission (AEC)] concern-ing particular events.                        Licensees are of ten requested to submit addi-I tional information or perform furthar analysis.                                        Before the LERs came into existence in the mid-1970s, it was not unusual for licensees to submit on their own or at the request of NRC or AEC more than one letter transmi tting information on a particular event.                                Thus, these printouts provided additional sources of information on reportable events.
Several special publications were reviewed for more detailed infor-ma tion on evenes of significance.                        These publications provided addi-tional details and evaluations or assessments of the events.
: 1. Reports to Congress on Abnonall Occurrences, NUREG-0090 series; I          2.      " Power Reactor Even t Series"                    (formerly  Current Even t Series) published bimonthly by NRC;
: 3.      " Opera ting Experiences," a section of each issue of the Nuclear Safety journal; and
: 4.      the publications of NRC's Of fice of Inspection and Ehforcemen t i
!                  (IE), such as operating experience bulletins, IE bulletins, IE cir-i culars, and IE informa tion notices.
l
                                                                                - - - - - - - - - - ,    --- - - - - , _  -----m
  - - - -  ,--.-m  ---,.m e  .y.  ..-,m- . - - - . - ,        ,,      - - - ,                      .
 
a
* B.3                Significance Screening
:                                            Two sets of criteria were used in determining the significance of reportable events.                                                                The first set of criteria listed in Table B.6 address events whose results include challenges to the safety protection l                          features of the plant.                                                                        These events are termed " safety significant".
The second set of criteria listed in Table B.7 address events that have the potential                                              to challenge the safety protection features of the plant.                            These events, which might require additional information or evaluation to determine their full implic tion, were termed "condi-tionally significant".
All reportable events were reviewed, applying the two sets of cri-                                                                                                  y 4-teria for significance rather liberally. A number of significant events and conditionally significant events were noted.                                                                                                                The events initially identified as significant or conditionally significant were analyzed and l
evaluated further based on (1) engineering judgment; (2) the systems, equipment, or components involved; or (3) whe ther the- nafety of the                                                                                                        ,
plant was compromised.                                                                      The conditionally significant events were sub-4 sequently " upgraded" to significant or " downgraded" to acr4significant as necessary.                                    The final evaluation for significance considered whether a DBE was initiated or whother a safety funetion was compromised such thae the sys tem as designed could not mi tiga te the progression of even ts.
Thus, the number of events finally categorized as significant was re-duced considerably by these steps in the review process.
I j                                            The reportable events not identified as either significant or con-1 dicionally significant were categorized as not significant (with an                                                                                                                'N' in the significance coluczn of the coding shee ts and in the tables).
.i
      -- - , . - - - - - , - , - - - - - , - - , . . . - - - . . , , , - . , , , - - - - - - . - - . , , - . , - - - - , - - . - - - - - - - - , - , - , , , - . . - , . . - ~ , , - . .
 
These events and the events rejected during the additional review step were further reviewed by compiling a tabular summary of the systems to detect trends and recurring problems. Table B.3 provides a listing of the systems.
B.4  Review of Reportable Events from 1967 through 1984 Figure B.1 illustrates the number of reportable events filed per year. The highest number of reportable events submitted by the licensee occurred during the years 1968, 1969, 1977, 1978 and 1984.      Most of the abnormal occurrences in the early years were reactor trips due to spuri-l ous signals and due to faults on the AC power vital bus.
e e
B.4.1  Yearly summaries
* The following sections present a yearly stamaries of the reportable events.
1967 Haddam Neck went critical in July 1967. The reportable events con-sisted solely of inadvertent reactor trips.      Six of sixteen trips were caused by maintenance errors while repairing or installing equipment on the plant's vital buses. Five other trips were attributed to spurious signals from various relays and power range monitors.
The only reactor trip classified as a significant event occurred on September 22. All ten steam dump valves opened during start-up due to an erronhous test signal and cancellation of trip override ( A0 67-07).
The reactor coolant temperature dropped 90*F (f rom 525'F to 435'F) in five minutes during this transient.      The incident . was terminated by closing the nonreturn valves in the main steam lines. See Se c t. B.5.1.2 for a detailed account of this event.
 
1968
              -        Twenty-three reportable events were recorded in 1968.                                                            The reactor tripped fourteen times during the year, with four of the trips occurring during a five-week period in November and December.                                                  Three reportable events were caused by problems with control rods.                                      Control rod problema are discussed in more detail in Sect.                                    B.6.2. Wo of four steam isola-tion valves failed to close during a test.                                      All four were then over-hauled and ratested successfully.
One reportable event was classified significant.                                                  On April 27, a switching error caused a loss of all of fsite power to the plant (A0 68-07). This was followed by the failut e of all three diesel generators to run.      This      s ta tion            blackout is          discussed            in greater detail                              in                              8 Sect. B.5.1.1.
1969 Twenty-three reportable events were reviewed for 1969.                                                          ho offsite power losses occurred, one on July 15 ( AO 69-09) and another on August 2 (Ao 69-10).          During the July event, one of the charging pianps failed to run. These two events represent 28% of the total number (7) of offsite power losses occurring over the history of the plant.                                                  These two events were classified as significant are discussed in Sect. B.5.1.1.
Five reportable events involved control rods.                                        On three occasions
)              con trol rods dropped into the core.                                    On the other two occasions they were inoperable.            Control rod problems are discussed in Sect. B.6.2.
The reactor was shut down five times due to inadequa te oil pressure in the turbine control sys tem ( A0's 69-03, 69-04, 69-15, 69-16, and 69-19). The low pressure was a ttributed to leaks and pump f ailures.                                                              The pump itself was replaced twice (AO's 69-15, 69-16).
1
 
Two large spills of radioactive liquid which occurred on May 3 and May 6 were classified as significant events. The first spill (A0 69-06) was caused by overpressure in the boron recovery tank due to improper valve alignment. The overpressure cracked the tank at the disked head sean, releasing about 200 gal of radioactive distillate (1.74 Ci tri-tium). The second spill occurred when a nipple broke and discharged 500 gal of radioactive boric acid (A0 69-07) .      In both instances the rup-tured vessels were repaired and the con tamina ted areas were cleaned up. Trace amounts of radioactive liquid and vapor were released to the atmosphere.      For  a  further  description  of  these    events,  see Sects. B.5.1.8 and B.5.1.9, respectively.      For other event of environ-        g 4-mental significance, see Sect. B.4.4.
Another event classified as significant, (Se ct. B.5.1.4), involved the f ailure of a feedwater regulating valve.      On June 10, a feedwater pump tripped on a low suction pressure, but the steam generator water level continued to rise.      Since the feeduster regulating valve is re-verse seating, the plug dropped open allowing full feedwater flow to the ste m generator (A0 69-08).
l      1970 l
i Eleven repor table even ts occurred in 1970.      Control rod problems con tinued this year with groups of rods dropping into the core on two
!      occasions (AO's 70-01, 70-03). Both events were caused by faulty relays r
which were replaced.
j          On October 12, a malfunction of one of ten steam dump valves caused l
!      an unanticipated cooldown of the reactor ( A0 70-09).      This incident was l      classified significant and is discussed fur ther in Sect. 3.5.1.2.
 
o  .
On August 19, a small fire was discovered and extinguished at the junction of a reactor coolant pump and the suction piping (AD 70-08).
This incident was also classified significant and is discussed further in Sect. B.5.1.6.
1971 Six reportable events occurred during 1971.        None of the events were classified as significant to plant safety.
On April 18, radioactive iodine was released when an operator pre-maturely broke the seals for the in-core thermocouples.        The operators had assumed the reactor coolant cleanup had been completed.            After breaking the seals, as in-core monitor indicated high particulate activ-icy. All personnel evacuated the containment. The reactor was resealed until April 22 when normal refueling operations resumed.      Four personnel involved received 10 90% of the maximum permissible dose for I-131.      For other events of environmental significance, see Sect. B.4.4.
1972                                                  __
Eight reportable events occurred in 1972. None of the events were significant to safety. Leaking containment isolation valves resulted three reportable events. A fourth reportable event occurred on May 19, when one of the purification ion-exchange vessels was tested to evaluate the effectiveness of unplugging operations ( A0 72-02).      The vessel was tested, then depressurized. The depressurization process evolved gases which were unexpectedly released into the a tmos phere.        All activities were below the maximum permissible concentration for the nuclides re-leased.
 
On February 27, a partial loss of onsite power caused a reduction in feedwater flow followed by a reactor trip. The onsite power loss was caused by test personnel.                                                                        Following the loss of onsite power, some dif-
;              ficulty was experienced while separating the main generator from the 1
i              grid.                    Automatic sepcration failed due to two faulty breakers and the generator had to be isolated manually.                                                                              Routine maintenance was per-formed and the plan t continued operation.                                                                            On June 10, main tenance i
worker caused a scram by inadvertencly grounding trip inserumentation.
1
;              on September 21, power from a transformer to a semi-vital bus was lost, causing a reactor trip.                                                                      Following the trip, the lef t side turbine stop valve failed due to steam cutting.
P-i                                                                                                                                                                                &
1973 Haddam Neck recceded fourteen reportable events in 1973.                                                                  For the third consecutive year, none of the events were classified significant to plant safety.                                                      Problems with the pressurizer level alarm occurred i
i-            early in the year (AO's 73-01, 73-02).                                                                            Replacement of bad photodiodes corrected the problems.                                                                    'No failures of steam generator support struc-cures were reported ( AO's 73-08, 73-12).                                                                          These failures were attributed to installation errors.                                                                  The supports were subsequently replaced.
I Unplanned releases of radioactive material continued to occur ( AO's 73-06, 73-07).                                            The first airborne release of radioactive gas occurred due to a leaky diaphragm valve at the ion-exchange outlet.                                                                                In the second release, a procedural error during maintenance on the purifica-tion system caused the release of 20 gal of coolant.                                                                              None of the re-leases exceeded limits.                                                                      A total of 0.238 of Noble gases were released in the events.
 
o          .                                                                                                                                                        .
4 1974 Eleven reportable events occurred during 1974.                                              Severe winter a
weather caused problems at the plant. The only event classified as sig-i                      nificant occurred on January 19, when all of fsite power was lost to the plant due to incorrect protective relaying during an ice storm (A0 l
74-03). This loss of service power (see Sect. B.5.1.1 was followed by
!                      the failure of a diesel generator service water pump to start.                                          The pump
}                      was started manually.                            A faulty relay in the pump motor control circuit caused the pump to fail to start automatically.                                      On January 18 the re-actor tripped due to . frozen instrument sensing lines ( A0 74-02) .                                                    Sub-f zero temperatures, strong winds, and f ailures of two heaters caused the g
2 lines to freeze.                  Backup heaters were installed to prevent recurrence.
An unplanned release of radioactivity occurred when the hydrogen l                      supply regulator to the volume control tank was leaking through the dia-1 l                      phraga (A0 74-07). The valve was replaced, no limits were exceeded.
On October 11 one of four main steam isolation valves failed to close due to dried out valve packing (A0 74-10).                                            Following adjustment
:                      of the packing gland, a successful valve movement test was made.
l
{                      1975 i
!                            Six reportable events were recorded in 1975.                                          None of the events i
!                      were classified as significant to plant safety.                                        On October 30, broken i
hold-down bolts were found on a steam generator support structure (A0
!                      75-02). This was the third failure of steam generator hold down bolts reported at the plant, two others occurring in 1973 (Ao 73-08 and Ao l                      73-12). The remaining reportable events involved nonessential equipment l                      failures and resulted in no consequences.
i,                                                                                                                                                                            >
i I
I
  -_m.._.    . , _ _ _          _    . _ , _ _ . . . . _ . . . . . _ .                        _ . _ . . _ _ . _ _              , _ _ . . , _ _ _ _ . _ _ _ . _ _ _ .
 
1976 Two of the twen ty-two reportable events which occurred at Haddam Neck in 1976 were classified significant.                      Offsite power was lost during refueling on June 24 due to poor design of protective relaying (LER 76-14).          During the outage, RHR flow was lost three separate times (see Sect. B.5.1.1).                                        -
On July 5, with the reactor at 1% power, both auxiliary feedwater pumpe became vapor bound (LER 76-16).                      Both pumps failed due to back leakage through the check valve feed line.                        The ptsaps were vented and 1    returned to service.                    The faulty check valve was cleaned and repaired.
This incident involved a total loss of the auxiliary feedwater system                                    e --
and is discuased in greater depth in Sect. B.5.1.3.
8 1977 The second largest number of reportable events (33) were recorded
:    in 1977.            Six failures involved the charging pump sys tem.                The first three failures occurred in April 1977, with charging pump 1A.                            During operation, pump 1A was removed from service fc                            low discharge pres-sure.          Invescigation revealed 2 cracks on the shaf t due to installation l    errors.            When the pump was repaired and replaced, the seal housing leaked.          Af ter replacing the seal housing, the bearings failed due to 1" proper housing ins talla tion.                    The axial alignment was adjus ted and problems ceased.            The operability of the charging ptsspa is importan t i
since the pumpe serve as the high pressure injection pumps during a loss I
of coolant accident.                      Since these ptsaps perform a safety function, a more detailed analysis of their failures is examined in Sect. B.6.3.
 
One event classified as significant occurred in 1977.                            On August 21, multiple failures of reactor coolant pump (RCP) seal occurred (LER 77-19). The No. I seal failed due to chipping on its face.                            The cause of this failure was not found.      Leakage from this seal caused the No. 2 and No. 3 seals to fail. The loop was shutdown.                Three other coolant loops were available throughout the incident.            This event is discussed further in Seec. B.5.1.6.
1979 Of the 37 reportable events occurring in 1978, 2 were classified significant to plant safety.      On August 25, an IM radio caused a rod C
drop alarm, following by failure of the load runback signal to initiate                                  D (LER 78-18). Investigation revealed a closed pressure switch isolation valve that prevented a signal from reaching the turbine load limit con-trol oil system. This disabled the turbine load cutback feature.                              The valve was'in a closed position due to an incorrect procedure.                            The valve was opened and the system functioned normally.            The procedures were re-vised. This event is discussed further in Sect. B.5.1.10.
On December 29, an air supply valve unistched, closing isolation trip valves on all four steam generator blowdown lines (LER 78-22).                              The operator reset and blocked open the air supply valve to restore blow-down. This action provided a potential atmosphere release path in the event of a steam generator tube rupture.            Due to the safety implications of this event, it is discussed further in Sect. B.5.1.5.
1979 Nineteen LERs were submit ted by the utili ty in 1979.                              Only one event was classified significant to safety.            On August 13, a pressuri::er
 
,              ~                  '.  .
y ._                  ,
s                -
s
                  ~s 1 ,
PORV , inadvertently opened due to failure of a bistable in a pressurizer-
!''              pressure controller (LER 79-10).                                                The reactor blowdown stopped when an operator closed the isolation valve.                                                    This event is discussed further in Sect. B.5.1.7.
1980 Twen ty-f our licensee event reports were recorded in 1980, none of which were classified significant.                                                      On February 4, a pressurizer pres-sure relief valve opened for about 2 min (LER 80-04) .'                                                            The valve was
!                manually isolated and then closed.                                                    Pressure in the reactor dropped dur-ing the transient but was restored within minutes af ter valve isola-tion.              The valve actuation was believed to be caused by spurious sig-nals, though no source was found.                                                      Leaking continued at the junction of the steam generator blowdown and service water lines (LER 80-07).
1981
          -                  Twen ty-two reportable events occurred during 1981.                                                  Three of the events were of environmental concern.                                                              On August 16 and again on September 17, the amoun t of radioactivi ty released via the stack ex-ceeded limits.                        The last environmental event, which was classified sig-l nificant, occurred on April 22.                                                Contaminated tube bundles were released
;                from the site prior to a health physics review.                                                          (See Sect. B.5.1.11 for further details).
i A procedural deficiency caused both auxiliary feedwa ter system
!                ( AFWS) pumps to be inoperable (LER 81M)8). On June 16, the 'B' pump was removed from service for repair.                                                  The    'A'      pump was tested and declared operable.                  During a valve lineup check, On operator discovered that the i
                'A'        pump recirculation valve had been closed rather than the                                                        'B'        pump
 
valve. A review of the surveillance procedures showed that the ' A' and            '
          'B'  pump recirculation valve numbers were reversed. The error was not discovered earlier since both recircula tion pa ths are normally opened for operability tests. The procedure was revised.
1982 Ten reportable events occurred during 1982.      None of the events were classified significant. Four of the events involve failures of mechanical equipment during a test.      Two failures of mechanical equip-ment during a test. Two failures involved main steam isolation valves (MSIVs). The valves were repaired and ratested successfully. The other d
two failures involved dampers on the containment air recirculation              D fan. A control linkage was found disconnected in one event and a link-age failure mechanically in another. Af ter repairs were completed, the damper system operated satisfactorily during the ratest.
1983 Twenty-six reportable events were recorded during 1983. Three of the events were significant.
Two of the significant events involved a loss of containment con-crol air which resulted in the loss of control of the pressurizer spray valves and the Power Opera ted Relief Valves (PORV). The first event was due to improper maintenance and the second event was caused by mechan-ical failure of the air filter canister.      Both events occurred during the same month.
The third significant event occurred on March 15, 1983 during low power physics tests (LPPT)    following a refueling outage.          Due to
        , abnormalities during the test, it was discovered that four control rods
 
were unlatched from their control rod drive shaf t assemblies.      The unit was brought to a cold-shutdown condition and the reactor head was re-moved to facilitate repairs.
1984 Of the 31 reportable events that occurred during 1984, three were classified significant.
Two of the significant events involved a total loss of offsite power. Both events were caused by human error.      The first loss of off-site power occurred on August 1.      While performing a check-out proce-dure, an operator selected the wrong circuit breaker.      All of fsite power tn was lost for ten minutes. The second loss of offsite power occurred on        I August 24 when a large pump was started during a refueling outage. The service station transformer isolated during the attempted start because a transformer wire had been pulled from its terminal lug.      The wire pull occurred earlier the same day when maintenance activities were performed in close proximity.
The third significant event of 1984 involved the failure of the re-fueling pool seal during a refueling outage.          Approxima tely 200,000 gallons of borated reactor coolant water drained from the reactor cavity to the containment floor in 20 minutes.      The original all metal seal had been replaced wi th a seal which included flexible rubber boots.          The l
seal failure is attributed to inadequate design.        The design error re-sulted in the NRC levying an $80,000 fine.
 
                                ~  ~
k3010 Y Coding Sheet for 50portabl9 Ev03tc et Hadd33 Neck-1967
                                                                                                                                                        ~
muabar        AccessiO2 E700t        RCport    Plset                              comp:nett Abstract        S ig nifica sco N uIbe r Da ta        Dito      StatC3 Syrt3D E;Cipsest I ctr: ment States    cetdition Ctase  cctegory      Cc mest A06701        030200  07/25/1967 08/08/1967    8    RB          &&      P        8        BF        G      E        Ma in te na nce worker in adve rt en tl y trips overwaltage relay in cootrol rod power supply (reactor shutdows)
A06702        030200  07/28/1967 08/l8/1967    B    IA                  H        B        BF        D      5        Spike in the S                                                in term ed ia te ra nge Su t 1                                                                                                                              circuit and au tomatic cutout of BF-3s (reactor sh etdo va)
AO6703        030201  08/07/1967 09/18/1967    3    IA                  T          &        DJ        E      N        Beactor trip BF                          when operator bumps botton A06705        030201  08/16/1967 09/18/1967    8    IA          00      T          B        EB        D      5        Reactor trlp on CD                                      BF                          setpolat drif t of MSIT lou
                                                                  ,                                                          pressure switch A06704        030201  08/17/1967 09/18/1967    8    EB          G                  B        BD        D      E        Reactor trips on BF                          in a d ve rt en t groemdiaq of vital bus A06706        030202  09/20/1967 10/25/1967    B    IA                  T          B        BF        D      5        Beactor trip on in ad ve rten t clearing of pe rmissive switch A06707        030202  09/22/1967 10/25/1967    8    NE          00                B        AY        G      S3        In ad ve rt e n t BF                          opening of alt 10 steam dump valves causes reactor trip 406108        030203    10/05/1967 11/17/1967    B    EB          G                  B        ED        D      C7        Beactor trip due
                                                                    &&                          BF                          to loss of vital bus powe r su pp ly A06709        030203    10/10/1967 11/17/1967    8    IA                  P          B        BF        B      B        Bapid load reject signal f rom relay trips reactor during load reduction A06710        030203    10/33/1967 11/17/1967    8    EL)          G                  B        ED        D      C7        seactor trip d.e AA                          SF                          to loss of vital
[h'Q-                                            bus powe r supply
 
                                                                                                                                                      =
                                                                                                                                                                                                  \
Table B2 Coding Sheet for Reportable Events at Haddas Beck-1967 - (Continued)
                                                                                                                                                                                                                ~
Nu::bef~~~~lccession Event                                                                                  Report    Fiant                              Component Absoraal        SkalficaEI Number                                                                      Date              Date      Status System Egulpment Instrement Status    Condition Cause  Category Comment A05718        030203                                                                        10/15/1967 11/17/1967        8    In                  8        B        BF      D        E    Beactor trips If                      dee to high Sus signal AO5712        030203                                                                          10/16/1967 11/17/1967      B      EB              G            A        ED      G        C7    Beactor trips BF                      dee to inadverten t grounding of vital bus dering salatemance A06713        030203                                                                        10/25/1967 11/17/1967        B    'Tg                A1 H        B        EB      D        E    Beactor trip on 3                    BF                      blown fase la power supply A05714        030204                                                                        11/05/1967 12/19/1967        B    EB                G            A        ED      G        C7    Beactor trip d ue BF                      to inadvertent grounding of vital bus daring mainte na nce 406715        030204                                                                        11/18/1967 12/19/1967        8    EB                G            A        ED      G        C7    Beactor trip due BF                      to laadvertent grounding of vital bus while changing beibs 106716        030204                                                                          11/24/1967 12/19/1967      B      EB              G            B        ED      3        C7    Beactor telps BF                      des to maintena nce error while checking lasta11ation of ne w wi ta l bus 9
e (55                                                          .
 
Table E2    Codisj Shset far Rsicctchls Evasto at Medics Neck-1918 - (Contiomed)                              ,
                                                                                        "                ~
Nuthor          Ac ce ssion Event      Ptpart    Picat                                    Casp4Gert A basr=ol        Sij3ificancs Numter  Date      Date      S tatus System Equipmen t Instrument Sta t us        Condition Cause  Category  Comment          ,,
406802            041938    31/15/1960 02/09/1968  D      HB        00                      C          BB      D      C dl    two steam isolation valves fail to close 406001            041833  01/15/1960 02/09/1968    B      IA        &&                      &          BG      G        N      Baintonance on BF                      power supply clears permissive, causing reactor to trip A06803            041e42  02/07/1960 03/12/1968    B    CF          FF                      B          /9]F    D        N      Escessive DD                                                            leakage of BMS pump seal 106804            041842  02/14/1968 03/12/1968    8      EC        &&                      &          BG      G        N      Loss of control
                                                                                                            ,BF                        power to RCP gover bus causes reactor trip 406005            041842  02/20/1960 03/12/1968    2      I&'                  jh          B                    D        N      Failure of rod BB                                                                      position coil stack causes rod bottom alara 106806            041641  31/28/1968 34/11/1968    B      IA                    8          B          BF      D        N      Inadvertent air into low vacuos turbine trip actua tor causes reactor trip A06607            030590  04/27/1968 05/14/1968    8      En        F          P          B          AT      G        S3      maintenance crew
{}ff              57      inadverten t1r tripped site feeder breakers.
All three DGs loaded then tripped off.
Total station
                                                                  .                                                                    blackout A06803            041846  05/04/1968 06/12/1968    8      In                    F          C          BF      G        N      Beactor trip during test of power range trap set points A06dO9            036295  06/09/1968 07/12/1968  'B      RB        J                      B          BF      G        W      Beactor trip gg                        when worker deenergized rod gripper while changing lobe
,                                                                                                                                      oli A06810            036295    06/10/1960 07/12/1968  8      I&                    E          B            EF      D        N      salfunction of BF'                      flow transmitter lg f                                          caused reactor en trin
 
Tcble  82. Cadiz.J Shact fer angertebis Eisnts at esdico unck-1968 - (certimad)
No bar    Accession Ersat      32          Picat                      -        CCfpStoSt Abn3rCAL          SiJIific5aco Number  Date      Dakott e      States Systes Egelpeent Instrument Sta tus      Condition Cause    Category  Comment 406811  041840  07/16/1J68 08/13/1968    B    PC        DD                    B        AU      D          N      Tolosse con trol JJ                                                        tank gases leak back into primary water guaps A06812    041839  08/02/1968 09/12/1968    5    NE        NN                    C        AC        D        N      peactor trir 00                              BF                        ductag test of j                                                                                                                            turblae stop l                                                                                                                            valve 406813  041039  08/09/1968 09/12/1968    3    NA        NE                    ($        AO-      E        C7    Beactor trip 00                              BF                        during reprogranaing of turbine control valvos due to i                                                                                                                            installation error 106014  041839  08/22/1968 09/12/1968    9    RR        90                    B        BF        D        N      Loss of control air closes feedwater rejulatin3 valve and trips reactor A06015    030206  10/13/1968 11/19/1968    E    25        J                    B        BC        D        N      Control rod 016282                                                                                                        slips in 42 steps A06817    030208  11/18/1968 12/20/1968    E    NA        M5        T          C        AG        D        N      Beactor tripped SF                        when metal fillags caused binding in turbine control switch A06316  030208  11/18/1968 12/20/1968    8    IA                              8        BF        D        C7    Beactor trip -
no apparent cause e
106810  030907  12/07/1968 01/14/1968    5    EB        G                      B        AC        D        C7    Vital bus (1/4) l 11                                                          fails due to had transformer in inve r ter A06820  030907  12/09/1968 01/14/1968    E    CB        DD        P          C        AL      G          N      Coil leads for time dolay relays on RCP        -
tound disconnected
* A06819  010907  12/09/1968 01/14/1969    E    IA                              B        BF                  C7    Beactor trip -    -
no known cause (see A06816)    ,
 
Table 82    coding Sheet for Bogottable Events at Raddam Neck-1968 - (Continued)
Musber  Accession Event      Report    Plant                                r;osponent Abnormal        Si jaltica nce N umber  Date      Date      Status Systen Rguipment Instrument S ta tes      Condition Cause Category    Conawat A06821    030907  12/17/1968 01/14/1969  E      IA                              E        BF                C7      Reactor trig -
no apparent-causo 106022    030907  12/18/1968 01/14/1969  B      RB        J          f          C                  D        N        Rod control salfunction during critical approach due to relay failure A06023    030907  12/25/1968 01/14/1969  5      IA                              B        BT                C7      seactor trip -
no apg>aren t cause 9
 
                                                                - 9c5ns 68
  - - - - - - - -              -      --- --------~
ct'oSlej S& cot. (for Ragartebiz Ev!nts at Hiddr Neck-1969-(Continued) su 55r--- A5ces3In:T Event --~~ iRFirt                  Plant                                    cotec= sat Abanraaf        SIsIIIIcenes Musber            Date        Dato      S tatus Syst0D Egtip2ma t Instrese3t . S ta t us      Conditica Cn==e Catogsry    Cac00st
                            = - - - - - - - - - - - -                  __
Ao6901        019269            01/06/1969 02/11/1969  D        EB          LL                  D          BF      D      C7      Inverter f or vital bus fails, causing reactor trip A06903          039269            01/08/1969 02/11/1969    B      HA          MM                    B          AD      G        N      Beactor trips NN                                BF                      due to oil leak of terbine i
control systes.
Line broken by maintenamac      .
A06902          339269            01/08/1969 92/11/1969  8        IA                                B          BF      D      C7      Beactor trips Ef                        due to spurious i
noise, source unknown A 069 04                          03/25/1969 04/18/1969  B        HE          QQ                    B          AL      D      C7      Reactor    manually BF                      tripped    on failure    of 1/2 turbine    stop valves A06905          034862            04/12/1969 05/16/1969  8        RB          J                    B          OA                N      Rod drive inoperable (no apparent cause) 314863            05/01/1969 05/16/1969  B        Ed          N          C          C          OE        H      k      Diesel genera tor fails to run during test due to procedural error 039001            05/01/1969 06/01/1969            ND          JJ                    B          OD        A      C3      Storage drum moved dear the fence (700 aces /hr activity at fence)
A06906          039231            05/03/1969 06/19/1969  B        PC          BB      /h          B          AH        H      S8      Boron recovery OH                        tank ruptures due to improper valve lineup Ao6907          039231            05/06/1969 06/19/1969  B      MA          Z                    B          Av        D      58      500 gal rad OH                        liquid spilled AD                        on boron recovery area -
broken pipe              ,.
Ao6900          0 39 229          06/10/1969 07/25/1969  B        HH          00                    B          AD        D      S7      High level in
                                                                                    //g                                            gp                        steam gen 83 due to broken              ,
f eed v ate r I                                            regulating flow cc atrol valve -    -
 
m-        LG RK f m ems Uce ksacrtab13 Eveatc at H:ddg3 Ncck-1969-(Continued)
                                                              - ~ ~ ~
SuillEr~~~~Icc335 Ion ~57Ent        Sepon      Picat                                  Cacpanant abastcef Number  D5to      04te        St&tuS Syct03 Eqtiprea t I ctrument S ta t es SI S TIcanco Conditian Cctso  Categsry    Ccceent
____________________                  _ _ = - -              -.    -
                                                                                                                        .
* c A06909          336147  07/15/1969 07/15/1969    8        PC          C                  B          BG      H          57    Loss of offsite EA          N                            OK              JEF      power,1 DG ER          DD                                                      fails to cua, I charging pump fails to run 106910          0 39046  08/02/1969 09/11/1969    B        EA f        P          B          BG      F        S7      Complete loss of g j:                        offsite power due to lightning strike on telephone relay 1069'?          0 19046  08/18/1969 09/11/1969      B        RB          J      P          B          AS      L        M      Control rods BF                        inadvertently drop into core due to relay fallare -
reactor shutdown' A06912          019046  08/20/1969 09/11/1969    B        ID                G          B          EG      D        E      Delta-T indicator f ails in loop 4 - unit replaced A06912          039046  08/29/1969 01/11/1969    B        ID                G          B          EG      D        N      Del ta-T indicator fails in loop 3 - unit replaced 106913          0 39067  08/31/1969 09/11/1969    8        RB          I                C          AG 019046                                                  J D          E      Stuck control rod, no cause reported, rod functioned normally after cooldown 106914          0 39345  09/07/1969 10/13/1969    B        RB          I                C          AG      D          E      Two control rods J
steck (no cause reported)
A06915          030807    11/11/1969 12/22/1969    8        NA          DD                B          BK I&                                        BF D        N      Failure of pump B                in turbine oil AY                        system. Beactor, BE                        shutdown by +ubME.
control system when ope ra tor inadvertently opened a relief valve 106916          038807    11/12/1969 12/22/1969    B      H&          {y)                1          4G      D        N      Failure of pump in turbine governor -
[$O                                        impeller slee we
 
Tal. lo 11 2                                            codinj stest far Warsrttblo Evaa*.s at Ilidd:c Nr.ck-1969-(continued) liu~siiUr"~~~IEEEEsI3n~ E ve nt      ~~~ Report                                                                          Plant                                  Component Abnoraaf          SI] Ell'lcance N um ber Data          Date                                                                          Status System Eguipseat Instrument S ta tus        Condition Cause  Category      Comment AOb917              330087  11/18/1969 12/22/1969                                                                          B      EB                    P        b            ED        G        N        Protective BF                          relayinJ trips plant - caused by noisture in relay box A06919              038887  11/28/1969 12/22/1969                                                                          B      HE          MN                  C            BK        D        N        Left hand 00                                                            turbine stop valve tails closed dus to low pressure in valve hydraulics A06910              038887  11/28/1969 12/22/1969                                                                          B      SB          J          P D            AS        D        M        Two rods dropped due to taulty relay. Also loss of rod control due to faulty capacator A06920              030007
* 11/29/1969 12/22/1969                                                                          B      SB          J                    8            BC        D        N        Control rod out of position (no cause reported)
                                                                                                                                                                                                                                  -k e
t I
e Ibl                                                              -
 
Tabla 82      c: ding sh2ct fer aspet:blo Evan*.a at Ridd;Q Ncck-1970- (Coninued)
                                ~~                                                                                                                      ..
Sim5er      Accession Event          leport      Plaat
                                                                ~~~        ~
Domponent Abnotaal  ~~
SigallIcance number    Dat e          Date      Status Systen Egelyneat Instrument S ta tus        Condition Cause  category    Comment A07001      044800    03/21/1970 04/21/1970        B      BB        J          T          B        AS      D.      N      Five rols slip into core -
faulty microswi tch A07002      344800    03/22/1970 04/21/1970                ta                    E JB                                        B        EG      D        N      Reactor trips on BB                                          BF                        erroneous signal (no cause reported)
A07003        044 864  04/02/1970 05/27/1970          B      SS        J          P          B        15      D      C7      Rod subgroup drops in -
caused by faulty contacts on relay.
AO7004        044864  04/14/1970 05/27/1970        B        IA                    L          B        BF      D      N        Automatic reactor trip during power range test.    (N o i                                                                                                                                      cause reported)
A07005      044864    04/20/1970 05/27/1970        B      CB        1 SC
                                                                                                  /J        As      D      N        Air leak f rom containment through RCP seal water retura system (no cause reported) 107006      347866    06/21/1970 07/27/1970        B      CB        CC                    B        AU      B        N      Steam leak from FF                                                          pressurizer due to gasket failure - gasket not rated for application 107007      058514    08/17/1970 09/15/1970        B        AC        G                      B        BF      [I        N      Reactor trip due to lightning strikes on telephone lines A07008      358514    08/19/1970 09/15/1970        B        CB        DD B        S4 BY D      S7      Small fire near '
RCP 84 - leaking oil from pump was ignited by hot piping A07009      357469    10/12/1970 11/24/1970        B        IA        QQ                    5        BF      D      57 NB                  /3                                              Reactor trip on BB              S 6L    erroneous loss EG                        of flow signal -
steam dump valve
                                                                                        /f 1L-                                      failed to close
                                                                                                                                      - nnesesn..e n.. e
 
T: bis d2                  Cading Sk30t frr R0[trtablo Ev3bts at HLdd 3 Meck-1970- (Continued)
                                                                                                                                                              ~~~~~        ~
Narber        ~5$ cession Event                                                      Repor[      Plant                                              Component Absoraal        Significance uusber          Date                                                Date        S tatus System Eguipment Instrument S ta tus                  Coedition Cause  Category  Coenent A07010          057469              10/24/19 70 11/24/1970                                                  D            ID                    I        C        ER      D        M      Setpoint drif t CB                                                                in pressurizer level aoattors 107011          057469              10/27/1970 11/24/1970                                                  B              ID                    I        C        BF      G        E      Balatemance crew C8                                                                trips reactor during work on presserizer levet sensor 1
l 1
e O
e t&T                                                        -
 
                                                                                                                                                                                    ~.
Tabla d2      Ccdi:3 Shoot far R31crteb13, Ersats at Hrddio 5cck-1971 - (Continued)                              ,
                                                                                                ~    ~
Eumber~            Ecossion Event                                Report      Plant                                  Component Absoraal        Sihificance
                                                                                                                                                                                ~~
susber                            Date      Date        Status System Equipment Instrument S ta tus        Condition Cause    Category Comment 363110                          04/18/1971 05/10/1971      C      CA          FF                  5          OD        M          C3  Radioactive OJ                        lodiae released OG                        due to operator error with penetration seals 068401                          08/01/1971 08/20/1971      B      PC        3                    B                    E          N  Raptured 40                        expansion jciat due to poor velds. Wald la L8 heater-draias piping 066476                          08/21/1971 09/21/1971      8      CR        5                    8          AU      D            N  Leaking tubes la feedwater heaters 067210                          09/07/1971 10/19/1971        B      EB        G                    C          8F      D            N  Homentary groemd ED                        on vital has causes reactor trip 340653                          12/02/1971 01/24/1972      B      CE        00                  C                  D            u  Solenoid valve A1                        failure causes feedvater control valve to close 107101                                                12/02/1971 01/24/1972      B      I1                  P          C          AG      D            N  Reactor trip relays blad due to grit 4
 
i Tabl6 82        Cadi:g Sh:<t he sagerteb12 Evtsto et andd:s a:ck-1972 - (corti:ued)
Werber Accession Event      Report      Plant                                  Component Abnormal                          Significance Humber  Date        Date        Status System Egelpaest Instrupeat S ta tes      Coedition              Caese      Category    Comment 407201  069324    01/18/1972 01/28/1972      B      SC        00                            15 B                                    D        5      Containment leak 80                                          dae to cracked          "
yoke on exhaust bypass isolation valuw 055283  02/27/1972 03/23/1972        B      EB        G                  C          BF                          G        N      Test personnel R3                                                                                    cause partial loss of orsite          ;
Fower, reactor trip 107202            05/19/1972 06/23/1972        B      PC        E                  C        OG                          H        C3    Unplanned airborne release DJ                                          from desimeralizer due to Operator error 072845    06/10/1972 07/01/1972      3      11                  L        1        BF                          G        E      Reactor scrans DJ                                          vhen maintenance        i saa grounds            -
instrument 076391    09/21/1972 10/20/1972      B      EB        LL                  B        BF                          G        s      Beactor trip on BG                                          loss of power to        ,
semi-vital bus f rom transformer        !
076191    09/21/1972 10/20/1972      5      EE        00                  8                                    D        E      After reactor BB                                          trip, left side        k terbine stop            .
valve fails, due        .
to steam cattlag        i A07203  075600    10/05/1972 10/13/1972      B      SD        00                  C                                      D        C7    1/3 containment          '
00                            Ba                                          isolation valves        -
fail to close,          -
due to leaking solenoid A07204  077213    12/19/1972 12/28/1972      e      SC        00                  8                                      D        5      Contaissent            4 AT                                          Purge ethaust            ,
bypass isolation        ;
watve fails              ,
open due to          -
crack in yoke (see 107201)      +
                                                                                  $b
 
Table B2 Coting Shsot fer Ralert:bla E7en'.s at Middts Ncck-1973 - (Continued)
* Eurbor        AcceErios Esset      R;ptrt    Pic2t                                  Carp 2naat Aba'stmal      Sig ificanco N um ber  Dat o      Dtto      S tatus System Eguipment Instrument Sta tus      Condition Caqso  Category    Comment          .-
Ao7301          078302  01/11/1973 01/22/1973    8    IA        CC          I          C          AA      D        N        1/3 pressurizer CB  .
g                                                  level alars fails due to failure of light source A07302          079103  02/22/1973 03/02/1973    5    IA        CC          A          C          4A      D        N        1/3 pressurizer CS                                                                    pressure sensor fails due to bad photodiode A07303          080132  03/26/1973 04/04/1973    3    38        N          C          C          AL      D      N        DG' load fluctuates during test due to loose governor Ao7305          081508    06/01/1973 06/22/1973  D      SD        00                      C          AT      D        N        Containment AT                        1 solation val ve leaks, is replaced A07304          081514    06/02/1973 06/04/1973  5                00                      8        AT      D        C7      1/3 reactor PC                                          At                        letdown valves
{same as 407203) f ails to close due to boric acid around valve packing Ao7306          082978    06/21/1973 06/22/1973  8    PC        00                    C          OG      D        C3      Uaplanned A dd                      airborne release due to leak in purif sca tion system valve.
valve had faulty diaphrage.
Valve replaced AO7107          081867    06/21/1973 07/03/1973  D              00                      jQ        BI      &      C3      Unplanned        .
PC                                          ON                        release of rad 11guld when letdova systen placed in servico due to procedural error A07308          084215    09/01/1973 09/28/1973  8    NB                                C          AD      E      C7      Steam gene ra tor EK                                04 0                                                            seismic support hold down bolts fail A07109          084871    10/04/1973 10/18/1973  B    SC                  C            C          BC      C        C2      Ta mers f or EE 54                                                                    service wa ter
                                                                                ,                                            pumps and cont.
air f ans f ail
                                                                                  / s,e0 during DG test
 
s Table 82                                  codinj Sheet for tegottable "Even*.s at Haddas Neck-1973 - (coattaued)
Numbut                        l' cession Event            Repor t                      Plant N um ber      Date Component Aboormal        Significa nce Dato                        Status Systen Eguipseat Instruneat S ta tus Coadition Cause  Category    Comme nt A07310                        084874          10/07/1973 10/19/1973                                8      EB          11            T      C          88      8        C4      Power supply fails to e
transfer dae to desiga error A07311                        085506        11/01/1973 12/13/1973                                  3      Sr          00                    a          18      D        C3      Valve on aus?
JJ                                ON                        thermosipnoa 3eaks radioactive water (bad diaphraga) into local stora newer a07312                        387101        11/26/1973 12/07/1973                                  3      NB                                C        /hh      E        C7      Steam gene rator EK                                01 a                                                            holddova bolt failure 087305        12/01/1973 12/21/1973                                  a                                                    OD      &        C3      overeuposure of two sea (gae rterly readings of 3.0 3 and 3.66 rea)
A07313                        088104        12/28/1973 01/07/1974                                  5      dO          00                      C          88      D        u        1/4 RSIV fails to operate, gland packing too tight O
e (67
 
Tablo 82    Cading Sheet f r Rsytetab13 Ev30tc at N:4420 N;ck-1974 - (Cortinued)                          *
                                ~~'                        ~~
35Eb5r'~~~ A3 cession Evott        R2 port    Plcat sunber    Date      Date Carpscott abattnal Status System Egelpment Instressat States                      SiglifIcanca Coaditica Casse    Category  Comment          *
* 807401        088083  01/01/1974 01/28/1974    3      IC                  y          C                  D        E      Fa11ere of a BB core cooling lattiation timer to load DGs A074 02        088084  01/18/1974 01/28/1974    5      I4        T          E          B        BF      D        C7    seactor trip dee as      I                to frosen lastrument sensing lines (mait heaters not operational) 407403        088451  01/19/1974 01/21/1974      5    E&        5        P          S        BD as                                                  D        57    Total loss of 54 I        g3      of f si te po wer dering ice store
                                                                                                                              - Se peeps on a DG did not start automatically -
loss of line dee to incorrect relay 1ag A07404        089348  04/01/19'74 05/12/1974    D      PC        e                    C        &C Sif      00 D        s      Degradation of air charcoal filters (filters replaced) 407405        089744  04/04/1974 04/04/1974    D                00                  C          BB      e        3 PC                                                                  Failure of reactor letdows stop valve to close completely (packing too tigtil 107406        390648  04/04/1974 04/10/1974    D      SA        PP                  C        AT        D        s      &acessive leak 40                        rate in contatement penetration check valve (grit on valve stem) 107407        091668  04/26/1974 04/29/1974    5      FC        00                    B        OG      D        C3    caplassed radioactive release from aux building exhaast faa dee to leak la diaphrage in hydrogen supply regalator A 074 08      093699  05/06/1974 05/06/1974    5      35                            C        ~BT      B        C4    DC excitation LL transfoceer fails (improper grounding scheme)
I6f
 
Table 52 i
coding sheet for negottable 5: eats at saddam sock-1974. (Coottaued) t seabor            Accession Event sunber                                                    Date brort      Plant Cosponent Ahmeraal
                                                                                                                                                                                                                                ~
Significance
                                                                                                                                                                                                                                                                ~
Date        States system Egelpaent Instrument s ta tes              condition Casse        category    Conseat 107409              092190                                                    05/24/1974 06/03/1974                              8      It                    L                C                  55      D                8 Setpoint drif t la accioac overpower trip lastrementation AO7410              393792                                                  06/14/1974 06/24/1974                                5    d@          00                          C                AC        D                5 asIt fails to BB                          close dee to dry valve pacting A07411              09437Y                                                  06/20/1974 06/28/1974                                5      CS        CC        E                C                35        9                N Setpoint drif t IA                  T                                                              la pressere switch
* I
                                                                                                                                                                                                    /G                                                                .
 
Table 52      Codtag Sheet for begottable' sweats a t saddam sock-1975 - (Gatimad) insbei"~~~45cessica sweat            soport      Flaat u ue ber Date        Date component Ah'n ormal States System agalpaeat Instransat Statae Sigallicence Coadition Canse  Category    Commen t 407501          101154  03/26/1975 04/01/1975      s      Cs                                          ~
00                    s        aI SF e        s      acs VAL VdI #AtKIN6 glaae fails, reactor skatdown a07502          103051  05/21/1975 05/27/1975 1:          se        II        &
l Es j}          Se      /9        C7      Steam generator a                                                          hotadosa bolts fail 104202    05/26/1975 06/30/1975    C      Cs        EE                    &        AL      3        s        Seismic CC                              BC 0                                                          restraints (3/a) on press:stser
;                                                                                                                                act properly icatalled 104049    07/02/1975 07/02/1975    C      CE        EE                  C          As      e        e      Feedwater hanger II a                                                          pipe attachments brokea 407501          106 348  Os/08/1975 09/05/1975    s      es                  &          C          01      e        a      missolved osygen IS                        across plant cooling water ascoeds limit A07504          108249    11/1s/1975 11/25/8975    s                y
                                                            $s'                            a        OJ        e        s      Service water to O
costalaseat faa cooters laterrupted dae to operator error 1
                                                                                      /78
 
TIbis 82 Cading SbCt fir R3]ortab17 Events at HIddse ucck-1976-(Continued) suiSEr'~~~i3c3Ei[3a Event                      Report                                    Plaal Component abnormal Status Systen Egulpaent Instrument Sta tus Condi tion cause SI]allica            nce Number  Date      Date Category      Comment lea 7604                    110359  01/01/1976 02/05/1976                                          Rr          F                      B          or              D    C7        High fish impingemen t rate on latake screens LER7603                      110941  01/08/1976 02/02/1976                                    D      I&                    L          C            EN            D    N        Setpoint drif t la overpower channel lea 7602                    110933  01/22/1976 02/03/1976                                  O    d s0          00      T          C            An              I    u        RSIT 00                                se B8 malfunctions due to frozen air opera tor lek 1601                      110940  01/22/1976 02/02/1976                                  8      NS                  E            B            OE            I      B        Sensing lines on It                                            Bu            G              Luo steam flow Br                            sensors froze L Ek7605                      111649 01/24/1976 02/20/1976                                    B      PC          *DD                  E                            D    M        Charging pump FF                                AT outboard seal leaks due to 0-ring failure LER7606                      111602  02/03/1976 02/23/1976                                    B      EE          5                  C              OK            G    N        Energency diesel BF                            tr1 PS 'h*"
calibration tool is left in unit L ER1607                      111603  02/19/1976 02/25/1976                                  8      11                  L          C              EN            D    W        Selpoint drift in overpower instr u ne at ation L EH7608                      113549  03/30/1976 04/29/1976                                  8      58      ghg                    B              OD              E    C3      Unplanned OG                            release of radioactive gas (11.59 Cil - two rupture disks in vaste gas ducar taan 4%:/ cbse do damage during insta lla tion L EH1609                        113548  04/03/1976 05/03/1976                                  B      In                  E          5 n                        EG I    N        Steam line break low flow alare received due to chanie in weather affectie)
L ER7610 instrumentation 114170  04/25/1976 05/24/1976                                  D      EC          C        C          D              EC            D    N      Dattery charger                    '
goes into overcharJe due                  -
to faulty contact on timer              .
 
Table 82 coding Sleet for negottable Events at Haddam Neck-1976-(4betimed)
                                                                                          ~~
535EEi'~~~i3cessio$'3 vent                  Report    Plant                                Composant Absormel          Significance u ual.er  Date            Dato      Status Systen Equipment Instrument Status      Condition    Cause  Category  Commen t LER7617          116272    07/2G/1976 03/03/1976        8            NB          B E        B        BK          E        N        Steam line flow G                  AT                            indicator fails due to leak in i
sensing line -
leak caused by cross threaded titting i              LER761b          117665    08/19/1976 09/03/1976        3            SF                      B                    S        C4      Error discovered is a.ssumption la vendor ECCS analysis ETs760s          118793    10/01/1976 10/13/1976                      NF          F            5        0F          D        C7      Nigh fish ispingenea t rate on intake scree ns Lea 7619        I l9 51's  10/01/1976 10/22/1976        3            PC        D            8        AB          D        N      Concentrated DD                    AT                            boric acid pump fails due to bearing failure L ES7701        121030    12/14/1976 01/14/1977        3            NI          E 110100 3        15          D        C3      Small leak ta
                                                                                      #A                                RF                          11guid waste NA                                05                          line adjacent to area reported la lea 7613 O
9 D3                                                              '
 
Tabla 82 Cc: ding Stoct tr tsgretab12 E?osts at Midd;o ucck-1974-(&mtimed)
NuEber'~~~i3cozzios EYeat                                            Report    Plant                                  Component Absoraal dueber              Date                        Date Status Systen Egelpaent Instrument Sta tus Sidalfica nce                                - c condition Cause  CateJory      Commen t Lga7611 05/10/1976 06/14/1976                      B    S M-C        00                    C            at      D        s        Lov discharje pressure on ama feed pum p (s fer6A[ driven) due to laadvertest opening of steam supply valve L ER7613            115876              06/15/1976 07/12/1976                    C    BI            1                    8          As        D      C3        Small leak la 51                                            05                          vall of safety lajection      .
cubicle due to deterioration ot steam generator blowdown piping L ER7612            115450              06/17/1976 06/24/1976                    C    CF          S                      B          SG        E      N        Power lost to BB          DD                                                            BNR pe op-o pe ra tor overloaded bus for pamp Len1614            115875              06/24/1976 07/09/1976                    C    Et                  F              B          BF        B      57        Total loss of CF                                            SG                          of f si te ge wer due to poor design la protective relaying-kNS flow lost 3 times Len1615            1 16 274            06/29/1976 07/27/1976                    C    55            00                    8          AD      D        E        Waste gas decay OG                          tank rupture disk fails due to pressere surge - 2nd time 1151.10              07/01/1976 07/15/1976                    C                                        A          OD        A      C3        Possible overamposure of maintenance worker (quarterly readings: 2.19 ren dosialter, 3.11 ren tron badge)
LER7610            11621)              07/05/1976 07/27/1976                    P    SH-C          DB                    A          DK        D      S2 PP Two aux feed AT                          pumps fail to DJ                          reach pressure -
both pumps vapor bound due to fault y check l }P 1L-
 
t a blo 82    Codia) sheet for Regortable Events at Itaddas Neck-1977-(Coettmund)
                                                                            ~~~
id55$r'~~~i3ce55IoE~ Event              Roport      Plant                                component abnormal          Significa nce numbur      Date        Date        status Systen squipment Instrument S ta tus      condition cause  Category    consent ETs770a        325397      05/25/1977 06/07/1977      8      NF          P                    B        0F      D        C7        Nigh. fish impingenea t rate on intake acreens L Ek1109        125591      05/31/1977 06/30/1977      B      FD          L        T          B        &&      D        N      Overhead crane control malfunctions due to wear of swatch mechaatse L EB1711        127017      06/23/1977 07/06/1977      8      ID          G        L          5        AC      D        N        NacLear Er                        instrument detector current erratic due to deterioration of detector and cables lea 7710        126490      06/27/1977 07/06/1977      8      I&                    P          5          EG      D        N        8eactor coolant pg                                            EE                        low flow relay fails due to open circuit la relay cott ET:;7705        126006      06/29/1977 07/07/1977 9    NF          F                    8          0F      D        C7      sigh fish impingemen t rate on intake scree ns LEH7712        le3528      07/05/1977 08/01/1977      5      I&                    I          C          EN      D        N        Setpoint drif t in pressurizer level channel LEH7713        143527      07/19/1977 08/09/1977      8    IE ED LL        U          S          EF      5      cy        Perturbations in BL                        loop temperature lastrumentation caused by failure of static inverter la h8.gk temp envitomment LEH1714        1435:6      07/20/1977 08/09/1977      8    IA          II        B      d            &&      D      /V        Steam generator I                    EG                        marrow ranje
* level trannoit be r fails due to amplifier
['[jI                                      failure
* Tablo M2    Coding Sheet for Regottable ivoats at haddas sock-1977-(cutimad)                              " "
                                                                            ~
W uatear        AccessioA~ Eve nt      Japort    Plant                              component Abgereal          Sijaificance 4 ua ber Date        Date Status Systes Equipment Imatrument S ta tus  Coadition Cause      Category    Comme nt ETS1701          122205  01/12/1977 02/09/1977    8    NF        P                    8        0F      D          C7        Nigh fish impingement rate on intake screens ko7702            123001  02/24/1977 03/10/1977    8    N&        JJ                    C        AB      E          5        Leak in recycle 0                              & LJ                          test tank due to corrosion (1000 gal radioactive water spilled) rT57702          123054  03/09/1977 03/31/1977    5    NF        F                    S        OF      4 C7        sigh fish impingement rate on intake screens lek 7705          124333  04/04/1977 05/03/1977    3    PC        89                    3        &Y      E          N        Decrease of BE                          charglag pump discharge pressure due to cracks la shaf t 80770s            148001  04/13/1977 04/14/1977    3    PC        1 110101 B        Adl    D          N        Leak in boric 15                            acid peep
                                                                                                                                          . smetion piping due to chloride stress corrosion LEH770t          125033  04/26/1977 05/12/1977    3    PC        DD                  8          &T      D          E        Small weep fouse tr                                                            in charging pump seal (la) houstag due to porosity la satorial L P.R7 707        125034  04/28/1977 05/12/1977    5    PC        DD                  5          SL      G          N        Bearing fails in D                              BC                          charging pump la doe to misalign me nt after saintenance ETS7703          125015  04/29/1977 05/12/1977    3    NP        P                    B          0F      D          C7      Nigh' fish 1spingement rate on intake screens L ER1706          125535  05/23/1977 06/22/1977    5    SC        D                    8          &&      D          N        Bearing fails on E                              AP                          contaissent air circulation fan j7                                          due to moraal
                                                                                                            ,                              wear
 
Table B2 Cadtag She:t far sagnetsbis E7ents et Cadd2n 3:ck-1977 -(continued)
                                                              ~~
Nulbur~~~~5cces5 ion Evect          Deprrt      Fisst                                Carpseett Abarreal
                                                                                                              ~
Sijsifica ncs M us be:r Date      Data        Status Systen Eguipseat Instrument S ta t us  Conditloa Cause  Category    Consent lea 772)      141420    10/03/1977 10/14/1977    3    as        Og                  g                  D        N        Seactor power lin                                      81                          level mones taril y escoeded due to slow response of turbine control valve ETS7707        130910    10/19/1977 11/15/1977    8    NF        F                    B        0F      D        C7      Righ fish leptagement rate on latake screens EFS7706        113614    10/28/1977 01/13/1978    3    BA                                                D        C3      Trities activity 0F                        in river water OD                        sample was high L EH7728      113613    10/31/1977 01/20/1978    C    FC        3          5        8        10      E        5        Boric acid leaks IA                  T                                              onto pressurizer pressure switch due to veld failure L Ek7727      149386    11/03/1977 12/06/1977    C    23        I                    C        AO      C        C7      Bod cluster control spider assembly vahe separates from bub due to faulty brare jola t .
ETS7708        130919    11/04/1977 11/17/1977    8    NL        DD                  a        05      G        C3      A river effluent BA        F                                                        somitor sample pump was not operating while 21 tanks were drained LER7725        144201    11/14/1977 08/25/1978    8    .c5        GG                            OA C                  D        s        right saubbers 3                            AW                          for feedvater piping failed tests due to fuel oil ta saubber LER7726        144127    12/01/1977 12/05/1977    D    IA        00                  B        AN      G        N        Wiring errors in c)        G                              SF                        RSIV valve circuitry, could have prevented a reactor trip.
Caused by salatemance error                              .
17 7                                                                          -i
 
T2 bis 82 Coding Shact for R2gart:513 Brsato at Hrdd:a Nick-1977-(Cutiewed)                              '
suiEir~~~~Ic6eli[EE Ev33t                                                      PJpart      Pictt            ~~
sustier Dato        Date                                            C3tPunert absurnaf-~' ~ '~~Illallicasca Status Systen Equipment lastrumeqt Sta tus Condition cause Categogy Comment            .
:                                                                              lea 7716                                                  143416  07/30/1977 08/29/1977      8      FC            DD l
C        A ll    C          5        Pinhole leak in 00                                                charging pump l
bypass salve due to faatty casting          ,
L ER7715                                                    143544  08/01/1977 08/18/1977      B      SR-C          DD          C        BE      D          s        Aux f eed p um p PP                    AT                          pressure below BB                          limit caused by leaking stuck open check vales L Ek7717                                                    143417  08/11/1977 09/06/1977      B      NB            3            5        44      D          5      Steaa leak on SG 00                    15                          level settling pot vent pleg valve due to steam cutting L Ea7 718                                                    143525  08/20/1977 09/20/1977      3      IA                  R      C        AQ      D          E        Brs low flow SS                          trip matrix relay fails to operate due to grit lea 7719                                                      143418  08/21/1977 09/20/1977      5    CB              De          3        43      D          S3      BCP loop 1 seal FF                    AT                          fails [chippia on  seat face))
during operation, causing other 2 SCP seals to fail lea 7720                                                    143419  09/16/1977 09/26/1977      3    4h                00 '
C        4G      D          C7      RSIT fails to PF move during test due to binding of valve packing gland LER7721                                                      144204  09/18/1977 09/19/1977      3    NB              00            8      OD      D          C3      Deplanned OG                          releasp of 7 44 C1 Nd**Cf/V8-gas-d iaphr a ja ruptured in vaste decay tank LER7722                                                      143524  09/21/1977 10/14/1977      a    11                    L      C      :H      D          N        Setpoint drift la nuclear overpower trip chaemel t14
 
Tabla 82 Codi:3 Sh2ct fic 82gsctibia Evasts at R:ddio 53ck-1978 - (continued) l I
ustbst        Acceesion Eeur.t      se        Plcnt                              CM s cat Ahaarnal        31 alficance                      b unaber    Date      Dahrt    States System Eguipment Instreneht St tus      Condition Cause hategory Comme n t              '
lea 7806        138369  05/08/1973 05/19/1978    8        EE    8                  8        EA      B      C4      Potentini exists for diesel          y generators to be overloaded under    ;
certain LOCA        [
conditions          (
(utong design      i assum ption s)
* p L ER7 80s        138939  05/09/1978 06/01/1978    8        FC      E                  B        RF      D        u      Leak found La          -
AT                      charging pomp rectre. bypass      '
valve due to erosion [Puey 8)    t LER7812          141030  05/31/1978 06/21/1978    B        PC    I                    C        10      E      C7      Leak found la 00                            As                        charjing pump pressure gauge      !
isolation valve      '
l due to veld failure [ Pump B)      f LER7009          140558  06/05/1978 06/12/1978    8 CS    CC                  &        AT        D      E      Leak tound la        f SS                                                      pressurizer          6 spray isolation valve ETS7806          140556    06/06/1978 06/19/1978    3        NF    DD                  8        0F        M      C7      Bate of change a:r                      of discharge tenge rat ur e      '
exceeds limit LER7010          1 39504  06/13/1978 06/21/1978    5        SR    0                  C        of        E      N      Electrical G                                                      penetration FF                                                      fails LOCA test      j due to landeguately sealed cable end tot LER7813          139025    05/17/1978 07/05/1978    8  gg          G                  A        AC        D      N      Hole found in E                            ED                        cable sheath for      '
CAR fan motor due to electrical arc LEH7811          141029    06/18/1978 06/21/1978    D        SN    GG                  C        CA        E      5      Hydraulic g3      I                                                      saubber uncoupled from    '
feeduater Piping    g
                                                                                                                                                -f 11*l
 
                                                                                                                                                                          ~
Tabis 82    Coditg Shact for Begsrtablo E7sato at crddan GCck-1978- (Contiamed)
                                                                                              ~
* uuaber    Accession Event        Report      Plant                                  Component Abnormal Number    Date        Date                                                                            31Jaitica nce Status System Egelpeemt Instrummat Sta tus        Condition Cease'    Category    Comment r
LER1801    1349f 0    01/26/1978 02/10/1978    3      ZE        S                      C          01        8      C4,      Terminal clocks f ail to . pa ss gealification tests    +
ETS7801    835892    01/29/1978 02/16/1978            EF        F                      5
                                                              ,                                                    0F        D      C7      Nigh fisk                ;
impingemen t rate on intake screens ETS1802    136380    02/23/1978 03/09/1978            SF        F                      3          0F        D      C7      Nigh fish impingemen t rate on intake scree ns LER1803      137248    03/97/1978 03/31/1978    a      NI        I                    g.                              C7 B                Leak in steam 34                                            A0                cf        generator 54                                            BC                          blowdoun line due to a sold failure caused by tuteraction of hot steam and cold service water LER7802      137340    03/22/1978 04/04/1978      3      se        e                    C          '
s      C4        tiectrical 08                          degradation on terataal block due to interface with aluaalaus bos ETS7804    137853    03/29/1978 04/26/1978              E,F        F                    B          0F        D        C7      Nigh fish impingemen t rate on intake
                                                  ,                                                                                            ecree ns LER7805    137854    04/03/1978 05/03/1978      8      S F-C      FF                    A          ST        D        N        Cracks found in DD                                                            wear rings and tapeller rings of NPSI pumps L ER1804    138255    04/28/1978 05/12/1978      8      FB          EK                    d        DJ          B        C4      Pressere buildup in anautar poison cavity of sient fuel racks.      Design deficiency LER7dO7    118797    05/0s/1978 05/26/1978      8      PC                              a          ur        D        u        Leak found in 60                              AT                            charging Pump          j recirc. valve due to erosion O[                                            (Pump B)          .
 
T2 bis 82. Codi:g shoot far asgrrt bis Evrats et Midden W(ck-1978- (Cestimmed)
                                                                                                                                                                                    ' ' ~ '
uusher                        Acesssics Evett      R: port    Finat                                  campement Abstrcli        Sigiificance Number  Date      Date        States Systen Egelpsent Instrument' S ta tus    Conditica  Cause  Category  Connea t ETS7809                        141286  09/29/1978 10/13/1978          NF          F                    5        0F        3        C7    Nigh fish lapingemen t rate on intake scree ns lek 7820                        141853  10/04/1978 10/17/1978    B    Cs        CC                    S        &&        D          E    treasuriser PC                    T                    41                          levet and Lressure crease due to fattere of charging flow cont ro11er suitch ETS7817                        151479  10/16/1978 04/02/1979    3    EF          F                              C 0f  -
D        C7    Rate of change AD                        of discharge DD                          .                              tempe rat ure exceeds limit ETS7011                          141812  10/31/1978 11/16/1978          RF        F                      B        0F        D        C7    Nigh fish impingement rate os intake screens              .
ETS7812                        142220  11/02/1978 11/30/1978    D    EF                                          BF        D        C7    Reactor trip up                          caused rate of change of discharge temperature to escoed 11mit ETS7813                          142646  11/12/1978 12/13/1978          NF        F                              OC        8 S                              5      Fish impiajenent or                          saapie accid entally discarded L ER181e g                        146631  12/01/1978 01/12/1979    3    NF        F                      B        OF        D        C7      Nigh fish impingement rate on intate screens RTS7H15 E                        146630  12/15/1978 01/15/1979    8    NF                                        OF        D        C7      Rate of change of discharge tem pe rat ore escoeds limit -
five times LER7821                          144618  12/27/1978 01/27/1979    5    BB        J                      C        OC        N        u      gineekiy rod motion test not completed on et
!                                                                                                                                                                                                              h
 
Tab 13 82    CodL:g Sh::t fre R2gertsb12 strats at N dd;o 5:c&-1978 - (Contimad) e
                                                              ~~
i Number    Accession Event            Report      Plant                                Component abnormal
                                                                                                              ~
Sijullica nce j            ' N um ber    Dat e      Date        Status Systes Equipment Instrument Sta tus      Condition Caeso    Category    Comment
{
l lea 7814    139810      06/18/1978 07/05/1978      8    31          E                    C
(                                                                                                        AT      G        N      Containmen t electrical
!                                                                                                                                  penetration j
'                                                                                                                                  leaks as a result of malatenasco lea 7816E  146629      07/01/1978 01/15/1979    a      ur          e                  a        or      D        C7      sigh fish layingemen t rate on intake screens
( L ER7815    139901      07/11/1978 07/28/1978    5      I&                    E          B        A&      D          N      Drain valve on 00                            A6                          8t**" 11"'
sensor leaks due to moraal usarout L ER7816    139902      07/24/1978 08/04/1978    8      SF-C        DD                  A          av      D        C7      Cracks found on NPSI pump la shaf t sleeve ETS7808    140769      08/01/1978 09/20/1978    D      EF-                                        0F      D        C7      Bate of change of discharge tem pe rat ure exceeds limit LEB7017      139957      08/04/1978 08/10/1978    3      CB                  U,          3                  D        N      Decrease la 00                                                        pressurizer 85                        pressere d me to EG                        failure of press urize r spray valve controller LER7818      140161      08/2f/1978 09/08/1978    8                  00      A          B          OE      N        58      FM radio caused IC                  R                    DJ      G                dropped rod alata, followed by failure of load rumback signal to ialtiate.
Failure caused by procedural error ETS7813      141456      09/01/1978 10/27/1978    8      BA                              B          ON      D        C3      Trittua level la river sample exceeded limit lea 7819    141760      09/09/9978 10/06/1978    8      IA          S        E          8          AA      D        N      High stoam flow 4.1      G                    BC                        indicator failed due to failure of power supply I60                                        f...
 
V Table $2    Cadi:3 shoct far Battetchio ETents at RIddas ucck-1979 - (coattamni)
Number        Accession E ve nt      Be et      Plant                            *                          '                        ~~
Number    Date        9ake Component &baotaal Status Systen Egelpment Instrument S ta t us                      51Juificance Condition Cause  Category    Coese n t fly 7901        154C72    03/16/1979 03/16/1979    C                                                OC        &      C3        Escessive socke r CD                          doses over          [
quarter due to leadequate          I recordia)            I procedures          '
E757904        152295    05/17/1979 05/25/1979          pg                                  8      0#        G      C7        Hypochlorite was 00                              0F                          inadvertently released to the ri ver lek 7907        150701    07/07/1979 07/23/1979    3      NA        RE                    C        AN        E E
N        fipe support in      ;
service water system f atis to meet seismic criterion LEn7908        152005    08/03/1979 08/14/1979    E    CP          EE                    C        AL        E      E        RRR pipinj 1                                                                                k seismic suppott missin7 due to        5 installation
                                                                                      ,                                          error LER7910          152183    08/13/1979 09/07/1979    8      C8        CC                                                                                !
a          B        At 00                              EG D      S7      Pressurater PCRT      [
inadvertently opas due to light source failure Lea 7909        151999    08/31/1979 09/12/1979    3      EE        D                        0 3
AE        C      CY      Potential probles with DG torbocharJer thrust oearin g lubrication (nanufacturer's error) lea 7911        152237    10/04/1979 10/10/1979    D      M&        EE                      C        AL        E      N    ~ 35 seismic S F-C      5 restraints            !
PC                                                                    alssing due to        j installation          !
error (3 systems      i' involved)
ETs790S        153396    10/16/1979 10/26/1979    a 94          00                      a      or        H      C7      Mypochlorite was      {
U                inadvertently released to the river EEu?90b        154816    12/16/1979 12/26/1979  a      as        00        I          a        06        o      C3      A icvel control P                    BJ                C4      valve relay        ,
failed resulting in 15.8 C1            _'
g gf3                                    relea sed in 10 min via the atack        _
 
Ta ble B2 - coding sheet for kegottable Events at Naddas Neck-1978 - (Continued)
                                                                    '      ~
5NE~uf~~~'I5 cession Event        Report            Plant
                                                                                      ~
Component absoraal
                                                                                                                      ~
s ual.er Date        Date                                                                                      $1 Jaificance Status syntes Eguipment Instrument S ta tus      Coedition Canse        Category Comment L Ek1622    146617  12/29/1978 01/22/1979            8    3D'        00                    B        OK            N          36    Air supply NI          MN                            BG            &          58 S
valves to At                        E3    isolation valves blocked open, loss of blowdova capability and loss of containmen t high pressere isolation ETS7603      1372a9  04/06/1974 04/10/1978                  un        JJ                    B                        5          C7    Discharge canal 0F                    .          PM level te                              escoeded limit 05 e
e 9
* lit i
 
I
                                                                                                                                                      )
Table 82 Codiaj Sheet for Begortable Events at gaddam sock-1979 - (Coattaued) 1 N u mbe!E    4ccession Event      Besort      Plant                              Component Atmoraal                                  ~
fiumber  Date      Date        Status 3 2stem Egelyment Instrument S ta t us                  Si.Jaillcance Condition Cause  Category      Comment                I L eatt 002    154453  12/24/1979 01/18/1980      5  EE        G                    &                  'E      E LL                                                          Beutral leads Ok                            from DG to            r N
transformer cut by construction      i s
I t
(
9 e
f 175                                                              -
A
 
Table 82    Ceditg Shict fer negartabla s;ents at Ridd:a ucck-1979 - (Certimed)
BimEir      IcciliIii~legat-      Deport    Plail                                              -
c.omponent IEa5taal            sigullica nce uusber    Date      Date      Status Systes Egalpment Instressat S ta t es          condition Cause  Category Consent ETS7902      150653  01/27/1979 02/12/1979 D          Mr                                            or        D        C7        Bate of chaaje et discharge tem pe rat ure exceeds limit 17S7901    150638  01/31/1979 02/02/1979          NF          F                    B            0F        D        C7        Nigh tLab impiajemen t rate on intake scree ns LER7906      149251  01/18/1979 04/24/1979    5    SM-C        DD                    C                      D        M 00                                                              L1A flow rate of SL                          aus feed pump BB                          due to NS                          overheating, steam bea tia j supply valve had f ailed open lea 7902    147341  01/28/1979 02/26/1979    D      I4        4          E          D            AD        D        u        Loss of reactor EG                          coolant flow G
ladicatin-J unit fails due to brokea signal lead LER1905      148745  02/08/1979 04/04/1979    D      PC        PP                    C                      D AT 3        tacessive loot fill check valve leakage due to degradation og seating surf aces lea 1901      150336  02/14/1979 07/24/1979    C      R8        8 147340  02/14/1979 02/28/1979                                            C            19        D        M        Crack s found in f uel cladding.
All elements examined, rest ok LE87903      148568  02/5 /1979 31/11/1979    C      kB        DD 151370  02/15/1979 27/1t/1979 C            46        D        N        Diesel fire peer I                                  se                          fails to start Ab                          (1/2) due to burned out coil in starter motor ETS7903      150992    02/19/1979 03/19/1979    C      PC        JJ                    B            OD        D      C3        Radioactivity is refueling water storage tant reached 26.1 Ci.
Limit is 10 Ci LEB1904      148744    C3/10/1979 04/05/1979  C      CB          1                    B            L Y,      D      D        Leak in primary drain cooler line due to
* cracked pipe fittings
 
e Table 82    Cading Shxt fcr psgertibla a:0210 at Hidda N:ck-1980-(Coettaued)
_Nurbar            Acce rsio2 Event              R2 port    Plant
                                                                                              ~~
CarpineEt Abatrchl                                    ~
Number    Date              Date                                                                        51 J aificance S tatus Systes Egelpeent Instrement S ta tus    Condition Cause    Category      Coesent L Ea8002 c          158157    05/04/1980 05/12/1980                  s1        y                    &        OG        &          C3      Badioactive OE                            release limits N&                            escoeded when an ion exchanjer was removed from service and replaced L ERS 009          158569    05/16/1980 05/30/1980          D      51        FP                    C                  D          8        Containment leak AT                            rates exceeded 33                                                                      due to uneven check valve seating LER8004 E            158253    05/19/1980 05/28/1980                R4                              5                  &          C3      Trittua activit y ON                            escecded release OK                            limit due to larJe amounts of processtag water for uponia]
l                                                                                                                                                refuellag outage L EB0005 C          158623    05/28/1980 06/06/1980                            00                    s        11        a          C3 AB        E
                                                                                                                                                  & vaste gas l                                                                                                                                        C4      systen valve OG                            opened releastag senon to the environment L EkN 010          160253    06/21/1980 07/04/1980            D    SF-C      EK                    C        AL.
3 E          D        Seksmic pipe supports on HPSI lines missing -
act installed LER8000E            158255    06/22/1980 07/01/1980            C              JJ                    B            .      &          C3        activity in a OE                            raw water SF                                        0D                            storage taak exceeded limits LE88012            160219    07/17/1980 08/11/1980          D      C8        FF                    C        15        a DD Ca      BCP seal supply bypass valve bushing broken due to high torque setting LcRCOstel 170020              07/17/1980 03/12/1981          D      CJ        00                    3        AM        H          C4      & throttlinJ valve was designed for i                                                                                                                                                moderato throttling but not low              "
throttliaJ for
* which it was (g y                                                          .
                                                                                                                                                                    -    i
 
Tab 13 B2                    Cading sheet far asgtetabla E7sato at ntdano u:ck-1980-(Cantimad)                              -
useber        accessiso E7Cet                                      32 Port    Ple:t                                                b5dpsDc;t Abatraal        Sig-ificanca
                                                                                                                                                                                                                        ~~
sunber                          Date        Date        S tatus Systen Eguipment Instsenent S ta tus Condition cause    Category    Commen t          --
LEna001                  154454                        01/03/1980 01/15/1980                B                ER              C                                                                      i C                  B        u      DG load sequence O                            OA timers for .
se rvice water pumps and containment fans        '
fail test L ER800 3              154452                          01/29/1980 02/07/1980              8                  EE    N                    &        R&      B        C4      Poten tial DG overload    duria)
LOOP, LOC &, with SIAS found to exist L ER8004              154451                            02/04/1980 02/12/1980              8                  CB    CC        8        a          At      D 00 C7      Pressurizer POPV EG                        ogen 2 aim. -
proba b? y spurious zijnal from press ure controller LER8005                155569                          02/07/1980 02/29/1980              3                  FC  g.7                  8          10      D          3      Boron vaste 17"                        storage tank
;                                                                                                                                                                                                                thermosig6on heator leaks due to weld cracks LER8001E              155375                            02/23/1980 03/03/1980                                      DD PC                          8        0F      M        C7      Chlorine discharged into river enceaded limit L ER8006              155989                            02/26/1980 03/25/1980            8                    B&    G          B        B        AE      E        u      nata station rad G                  sonitor falls due to beat plug-la module LER8007              155986                            02/27/19f0 03/25/1980            5                    31    E                    B        Au      D        C7      Liquid rad waste EI                                  At                          line leaks due WL                                  oj)                        to corrosion of suppo rts L Ena 006            155984                            03/06/1980 01/20/1980          5                    SC    E                  C          AD      D        u      containment 6            ,                                            atmosphere recirculat ion f an bypa ss damper fails open due to troken linkage L ER800 i d          158782                              04/28/1980 05/12/1980                                                          d, go                              11      D        C3      an unplanned na                                  OG                        radioactive release occurred when a dogassifier g                                        puputre    disk anse cracked
 
Table B2 coding Sheet for Re;ortable' Events at uadda: b eck-1980-(cuttemmi)                                      *
                                                                                              ~
uuaber        tecession F.went                Sopor t                Plant                              component Abnormal        SigaL}}cance susbur          Date          Date                  Status Systen equipment Instrument S ta tus  condition cause category    Comme n t LERdO11        160286        08/01/1980 3d/13/1980                    B    SA        FF                  c        oc        n        a      containment batch leak rate not tested on time L ER8014      160042        09/26/1980 10/24/1980                    8    45        80                  c        on        D        a      Diesel fire pung W.                            SE                        discharge pressure below tech specs (Low eagine speed)
L ER8007 C      161681        09/26/1980 10/08/1980                          PC        00                  B        OG      H      .C3      As operator OJ                        opened the wrong valve causing 1.3 ci to be released via the stack LER8013          162400        09/26/1980 09/29/1980                    5    FC        00                  t        OG      M        c3      Techniciaa makes DJ                        sampling error, 1.3 ci I
radioactive gas relea sed LERH0lb          160512        10/20/1980 10/24/1980                    3    51        FF                  S        AT      D        5      Aerated draia 1                                                        line leaks la Liguid Gas System due to failed gasket oQ reboiler pump L Endo 16        161762          11/18/1980 12/03/1980                  8    R5        J                    B        AC
                                                                                                                                      &S D        5      2 con trol rods drop-ia due to burned out contac to rs      .
LER600s r          16 4= 3 8      12/17/1980 01/11/19s1                        mr        F                  r.        Or      a        c7      aigh ispingement rate of fish on the intake screens lWV
 
Tabis 82 ccding shact frr sagttt:b13 E7s tc at Midd:o N:ck-1981 - (carimma) 1 Eum5ec    Accession ~1 ent                                    aeporE    riant                          -
component Abaormal        sijallica nce~            ~~    ~
Number                  Date                        Date      Status System Ege1 Paest Instruseet s ta t es  Condition cause  category    conse n t LEE 0101  164334                  C2/05/1981 01/02/1981                    2    SC        00                    C        AQ      D          s        A contalement I                                BB                          air I                                                            tecirculation dealer f ailed to close LESd102    165395                  03/22/1981 04/13/1981                    3    SF-C      DD                    C        OJ      N          N        A safety OE                          lajection puay DC                          test was not completed FroPe rlF Les3013    165900                04/03/1981 04/21/1981                    9    CS        S                    3          AL      5          C4      fressurizer reliet and AT                          blocking valves opened due to a loose electrical comaectton LEB8104    166067                  04/07/1981 05/18/1981                    3    55-C      F                    3        BC      e          a        An APUS valve 00                                                          breaker was OJ                          found to be opea LES$1005  166187                  C4/22/1981 05/22/1981                        RB        5                              OE                  S8 A                  Con ta m [A 4 ft4[
bundles were released tros site prior to health physses reviee LER0106    174698                  06/03/1981 06/25/1981                    B    S R-C    qgg                    a        AC      D          5      Aus feedwater BR                          pump started due
                                                                                                        ,                                                            to a control valve failure L E B8107  166846                  06/04/1981 06/25/1981                    B    EE                    F          C                  D          N      A diesel EH                          Jesorator load seguenciaJ timer f ailed due to timer drift LERQ103    167720                  06/16/1981 07/10/1981                    5    S M-C      00                  4          OE      A        C2      toth AFWS pumps At                          inoperable due
                                                                                                                                            ,                        to a procedural deficiency LP.38110  167842                  07/04/1981 07/29/1981                    E    PC        DD                  N          AP      D          W      Charjia, pump AW                          vibration caused
* FF-                                                        its oti line to crack and leak      -
 
                            ~ ~ ~ ~ ~
if3CLWLJ      @KE)g shoot far 333tet:b13 3 coto et ; a4423 N:ck-1981 - (Coettaued) ancher ~~~$~csasica c        E7cdi~~~~~'Beytet            F155%
                                                                                  ~
Ncobst    Dito          D.Ito        Stetco SyEten Eguipment Instres2atC*rPs555t      thastaal Statta Condition          sigaificinco                    ~
CecGo    Ca tegtr y    Conawat
_ _ . e LEB0109    167854  07/23/1981 C8/03/1981            3 OE      &        N        1he lou population zone was incorrectly calcolated LBaa112    168526  07/28/1981 C8/20/1981            3    NB        II                    e          nu      D        a        an air ejector radia tion monitor indicated a primary to secondary steas generator tube leak LEB8111    168527  08/03/1981 08/17/1981            3    EE        N                    C          E&      D        5
                        ,                                                                                                          During a test, a SC                        diesel generators
* ouput exceeded the easinua LE98111                                                                                                                            allowable 168621    08/03/1981 88/31/1981          3    35        u                    C                  D        M        a diesel 2emerator could not be synchronized due to a lact et governor control LBa8100 E  168192  08/16/1981 08/25/1981            3    45        00                    5          OG      N        C3        Bobot gas 03 releaso rate escoeded limits due to oporator ettor LEB3114    168929  09/01/1981 89/14/1981          3      EB        O                    C          A LL    D        u 8                                                            the diesel 9enerator was inoperable due to a leaking coolia) sy ste n LER8115    170001  09/17/1981 10/16/1981            8    &&        E                    B          11      E        C3        Badioactivity 40                        released via OG 40                        cracked exhaust L End 11t. 169563                                                                                                                duct to stack 09/27/1981 11/23/1981            D    CF        00                    8 171561                                                                                      &L      D        N        4 valvo an the Av                        SNR systes leaked due to LER811a                                                                                                                          loose bolts 170137 172047    11/la /1981 11/2 C/198(        0    50        00                    C 11/14/1981 01/26/198 >                                                                    &        N        1he contalasest 40                        penetration leak rate exceeded the 11stt l99
 
i Table 52          Coding Sheet for Begortable Evoets at Naddam Neck-1981 - (Coartaued)
Number                    Accession Event                      3eport      Plant                                      ';ompcaest Ahmoraal                          S ignificence n ual.or        Date                pate        status Systen Eguipment Instrument Sta tus                      Condition    Cause              CateJory                                  Commer.t
_ _ _ . _ _ _ - - = -- _ _ _ _ -                        ___
L E Rel119                171704          11/19/1981 12/04/1981                B        PC          DB                        B            AP            D                                W                          Charjing pump D                                      &&                                                                        vibration was excessive due to a worn out i
bearing LEadl20                    171821          11/22/1981 12/17/1981                5        NB          00      q                8              BG            D                                N                          & staae flow IE                                                  Au                                                                        differential pressure transaatter leaked giviaJ falso flow readings Leahl21                    171825          12/04/1981 12/15/1981              B        NA          00                      5                            8                                5                          011 pressure for R5          J                                                                                                                  turbine valve us                                      at                                                                        control fluctuated causing power osic114tions y                                                                                                                                                                      -
14j                                                                                                                          .
 
i                                                                                                                                                .
Tabla B2 Coding She:t for sagtetchls Ersats et ande)s sick-1982 - (contimmed) a
    .sunber  accesalon Event      Sepe t    Plant                                Composest abnormal        Sigallicence                    ,
number  Date        Date      States Systes Eguipment Instressat S ta tes    Conditica cause    Category  Commen t lea 8201  172191  01/12/1982 02/04/1982    B    BC        C                    8          3G        s      C4      Dee to desija 5                                                        error both 0                                                          tattery chargers 1
are powered by e            one diesel
                                                                                                        .                    generator          -
L Ea8 202  172178  01/20/1992 83/03/1982  3      us      LL          C        a          BG        9      8      Failed inverter In                    I                                              causes f eedvater flow transmitter to f ail high LEBd203    173361  04/23/1982 05/14/1982  8    cp          FF                  C        AG        D      C7      RSIT fails to 00                                                        novo during test due to binding of valve packlag gland-staller to LEB7720 lea 8204  175151  06/06/1982 06/24/1982  D    g)          00              ^'C          15        G      C7      RSIV failed to cycle durinj test due to damage duriaJ previous maintenance LER8205    175147  06/03/1982 06/24/1982  3    SC        E                    C        AL        D      C7      Contalement air a
CA                        recirculation fan damper f ails test due to disconnected i                                                                                                                          control linkage LEB8206    179054  09/19/1982 11/02/1982  3    BC        C                    B        15        D      s      Battery bank 3C                        decla red O&                        leoprabie due J
to leakin; cell
)    Lek 8207  177690  09/27/1982 10/28/1982  5    RB        J        P          B        BE        D      E  . Poor relay It                        contact on a
!                                                                                                                          master cycler j
relay caused a l                                                                                                        '
control rod
'                                                                                                                          drive slave cycler
'                                                                                                                          f atture/ rod stop 414ra
!  LEB8208    177829  09/24/1982 11/02/1982  D    $4      pp                    &        OC        k      N      Containment
'                                                                                                                          personnel batch test not .
terformed Joe to ongoing fk2--                                      maintenance
 
Table 82    Coding Sheet for Regottable Events at Naddaa Beck-1982 '(Cantimad)
Number        accession Event        sepet      Plant suaber Conpcaest Absornal        31Jaiticance Date      Date        Status System Egelpeemt Instressat S ta tus    Condition Cause  Category    Commen t LE23209        179a67    10/15/1982 01/26/1983    E      PC        Q                    R        AU      D        N        Plehole beak la 4
3                              op                          pipe joint mest to charging peng throttle valve-saall
;                                                                                                                                                                    release of radioactive l                                                                                                                                                                    coolant to aus building l
LERd210        179421    11/13/1982 12/08/1982    3      SC        E                    &        AD      a        C7        na operating linkage for a bypass desper om a containment air I
recirculation faa failed nochanically durin g maintenance i
l i
3 I
e
                                                                                                                          /?5                                                              .
f
 
Tabls 82 Codtag shsct far 33girttblo avosto at Haddas teck-1983-(ometamed)                        .
uncher    Accattico Evert      Dep:rt    Flcat                                Czaproc;t Abairr41          StJilfIcseca l                  sunber  Date      Data        Status Systes Eguipseat Instressat S ta tus    Condition Cause    Category    Comment              . .
L ER8 301  130844  01/05/1983 01/26/1983    8    SC              E              B        AR        D          u      Service water W&              EN                      Au                            leak la coil of j
BS                          containment air i                                                                                                                                  recirc fan cooler due to corrosion and erosion- se rvice water was blanked off L Ek8 332  181080  01/11/1983 02/15/1983    3    BE              E              B        BE        D          E        mechanical pg.                                                                    failure of air compressor for diesel generator
                                                                                                                                    - alare received on asia control board L Ea8 33 3  190578  01/22/1983 06/25/1984    C    SE-C            DD            C 1
At        D          E        Aux feed pump RB              00                      AB                            fails flow capacity test doe to wore relief valve on steam supply to turbiae lea 8304    183455  01/26/1983 04/12/1983    C    51              FF            C        40        0          m      contalament aetrations rallleak    rate tests LER8305    182157  03/09/1983 04/11/1983    C    SC              B              C AD        J)  .      C7      Rechanical i
linkages on two containment air recirculat ion faa dangers found broken LEss 306    182158  03/07/1983 04/11/1983    C    CF              00            C        AD        D          5 j
BHR flow controi QQ                      Bt                            valve fails l                                                                                                                                  partially opea due to brokaa t                                                                                                                                  actuator ara l        t rP9 30 7  182159  03/22/1983 04/22/1983    C    SD                    a        C        RI        D        a        containment
;                                                            15                  T                  EN                            isola tion pressure instrumentation actuation setroint out of calibrat ion d ue to drift la secomtar calibrettui
                                                                                                                                  ,3 Aacc/
19't 1
 
Tabl2 B2    codtog Sheet far R31ertable Ev20ta at Naddas unck-1983-(Contiamed)                          -
55 5Zr-~~~I2c3 ZI5a'Ei43Y                  poport    FIs.t                                Campose:t Abagraal .              SIj7IIIsaac3 s ea ber        Dato      Dato      States Systen Eguipment Instrgment S ta tes            Condition Casou  Category  coemen t
___ -=
LER8308        183093          04/14/1983 05/20/1983  3      as            II                3              47,        e          a    primary to
;                                                                                55                                                          secondary steae i                                                                                                                                              pee ra tor tube leaks in muaber        ,
2 steaa                !
i generator i
{  L ER8 309      183299          05/05/1983 06/17/1983  5      PC            DD                C              AG        S          W    Opera tor was j                                                                                                                                              enable to rotate
'                                                                                                                                              the "A" charging peep by hand la
                                                                                                                            ,                order to perfore the routiae surveillance test due to solidified boric l                                                                                                                                            acid 1
l i
lea 8310      183300          05/07/1983 06/17/1983  3      SC 91 E
P B              Ag NC
                                                                                                                              )          5    Temporary loss of service water to contalement air recirc f ans dee to a clogged service water filter Lead 311      183301          05/04/1983 06/17/1983  3      S P-C        DD                C                BK        &          5    NPSI pump fails OK                        to reach the shutoff head of 1400 psi l                                                                                                                                            requireJ by the i
1 test procedure duo to l
marealistic regelrement
?
I LER8382        183558          05/17/1983 06/27/1983  5      EE          5      C          &                BE        D          5    Governor voltage setting drif ted j                                                                                                                                              when dieari
;                                                                                                                                            generator was shutdown f or aninteaaace at air-star t actors LER8313        183559          06/01/1983 07/05/1983  8      Et          u                  C                SI        e          u    Diesel generator failed to attata moraal idle speed withia j                                                                                                                                            time specified i
la mathly        -
surve111once test  ,
i 19s-                                                                  .
i
 
Tablo B2    Cadhg Sheet Er 22prtab13 Emats at Caddas Neck-1933-(Centlaued)                      ,
53ESW~~Ecadon 172E                Beperl    PEl~                              . Ca mpw. vat A ha s:r eal    SijillicracJ
                                                                                                                                    ~
uueber  Date        Date      Status Systes Eguipneat Instrqment Status        Condition Cause Category Coenest                .
L ER8 314    185176  07/30/1983 04/25/1983    3    54        S                    S            BG      I      s      one of the two ojr                      incoming station service supplies was disabled by
                                              ,                                                                          a theaderstors L ER8 315    186378  08/31/1983 10/25/1983    3    CB        CC        I          C            AG      e      a      Pressuriser high In                  F                      BA                      level trip relay stect ductag test - 2 out of 3 logic L Ea8 316    186328  09/01'/1983 10/25/1983    3    PC        G        5          B            AD      8      N      Charging Pump DD                                OA                      declared inoperable due to broken wires os motor bearing thermocouple LER8 318    187111  10/19/1983 11/21/1983    5    PC        DD                  8            As      D      E      the "a" charging C5        FF          .                                            pump was taken        .
out of ser vice due to leakage i                                                            on the out board peep seal L ER8 320    187491  11/01/1983 12/13/1983    3    CB        P                    5            AR      G      $2      containment P&        Fr                                as                      control air lost 00                                BG                      due to incorrect BE                      filte r o-ring -
caused loss of pressurizer spray salves and
                                                                          .                                              PORVs LER8311      187253  11/03/1983 12/01/1983    5    EE        3        C          C            EN      D      u      Set point drift S F-8    58                                                        in the energency diesel timer for the "B" LPSI Pe*P lea 8325    187=70  11/28/1983 12/13/1983    3    C5        P                    S            AA      D      S2      Loss of PA        FF                                AD                      containment 00                                AW                      control alt SG                      (broken air BK                      filter canister) caused loss of control of Pressuriser sprey valves and FORVs 146
 
Tab 13 82 CadL;g Shoct f ar Coggrtab13 EJsata et Nadd22 Nock-1983-(Qattamed)                                    d t
35C5Ic~~~~15c!E2EE3 EviEE                                                                                                                          I Eer3fE      FIta t
* R2aps,omt Ibaarmal        sta silIcanca                            '
sunber Dat e      Date        Status System Egelpaent Instreneet Sta tus    Condition Cause  C4tegory    Comaea t                  i b
i L ER8 322    188309 11/23/1983 01/16/1984    B    PC          3                    8        1R      S          C4      Loss of control JJ                            BG                          power to motor 00                                                      operated valve              1 00                                                        on WCT outlet              d LL                                                      due to f ailed j
transformer and            1 fuse 1
l lea 8323    187980 12/01/1983 01/05/1984    8    EE          5        C          C        BC      G          N      Derlag a test
!j                                                                                              EA                          the diesel                -
9enerator                .
I                                                                                                                          assened a load greater than the i
governor setting des to an out of          ,
adjus t neat              -
9overnor assembly                  E LEB832n      188664 12/30/1983 81/27/1984    3    un          3                            EB      B          C4    Service wa ter SS          E                                                        flow to
* a contaissent coolers is less con se r va ti ve            .
than assumed la current containment                j 1
pressure                  g analysis                    j L Ea8 325    188387 12/07/1983 01/27/1984    5    RB        J        T          C        SD      D          u      Fallere to                  8 withdraw rods during rod notion checks due to a t ailed actor starter switch                    ,
PMOI6120            03/15/1983 03/17/1983    C    RB                              C I                              AE      G        $7      Improper J                              BC                        latchia; between C1                        control rod drive shaf ts and          t rod control cluster assemblies during low power physics tests
!                                                                            19r7                                                            -
i 4
                                                                                                                                                  'l i
 
s
                          .                                                                                                                              g Table 52    Coding sheet for negortable Events at Naddae sock-1983 - (Continued)                          , e i
los Evea[
              ~
Number                            Be        Plant sue Accesf= r  Date      Dakaort e
Component &bsetaal Status Systee Eguipment Instransat Sta tus 31.alf5C    ace Coeditica  Cause    alegory      Comment Puo!8195                09/06/1363 09/06/1983    3      as        as                  a        sE        D          C3      3. 3 Ci of noble 00                  .          3J                            gases released OG                            to the stack t
vbes a cellet valve on the vaste gas surge tant 11fted doe to fallece of gas coeFressors 4
1 1
i                                                          e I
l 1                                                                                                                          -
I i
I 5
j IVf
 
T: bis 82          C@ ding Sheet far 23prtsb13 2700to at Nadda2 Cock-1983- (Coettaued) penber    Adcassion Event        Report            Flaat
* Component abnormal        Sijaifica nce sunber    Date      Date            Status Systen Eguipseat Instremost Sta t es    Condition Cause    Category    Conseat LEp8401    189204    03/21/1984 04/23/1984          8    At                              8        OA        D        C7 ff                                                          Several fire doors were foemd to be Laoperatie LEBd402    189507    03/23/1984 B4/26/1984          5    AB        F                    8        11        N        N        Loss of power to 51                                        BG                          the fire detection system for the screenwell building due to a manually opened breaker LEs8401    189508    04/04/1984 05/08/1984          3    at        ff                    a        01        D        C7      A fire door was inoperable f or
                                                                    ,                                                              two days lea 8404    190589    04/13/1984 06/25/1984          5    SA        FF                    3        01      D        C7      A penetration 18                                                                    tire barrier was found to be inoperable LER8405      190099    04/26/1984 05/30/1984          3    NB        5                    B        AD      5        C4      Errors were I                              OK                        discovered in the design basis evaluation of the steam line treak accident during three loop operatton LER8406    190536    06/11/198e 07/10/1984          3    at      ff                      B        04      0        C7      4 fire door was O                                                        dtscovered with an inoperable latchta}
nochanise lea 0407    190537    06/12/1984 07/10/1984          3    5/l        FF                  a        04      D        C7      Several laoperable fire karrier penetration seals were discovered during an inspection L End40d    190973    07/21/1984 08/23/1984          S    AB        FF                    8        04      D        C7      A fire door was disco ve red with an taoperable latchinj nochanisa                ~
lea 8409    191 329  08/01/1984 09/10/1984          9    En        F                    &        A1      N        S2      Totat losa of
* SG                S5      normal off site EA                        power due to          -
fj4I                                          laadvertent c.
                                                                                                                                    . . losing
                                                                                                                                        . . .. of.a *KW <
 
                      .                                                                                                                        C Tablo 82 Codia) Sheet for segortable Beasts at Naddas Neck-1984 - (Gunlamed)                            ,
                                                                                                                                            ~
EGa5=c    Icce ssI5E~E vill    1 sport    Plant                              component Absoraal        sijai? Ice nce States System Eguipment Eastrument S ta t us  Condition Cause    Category    Comment a ua ber  Date        Date
                                        ==.
L E Ed 410  191266  38/03/1984 09/13/1984    C    CB        00        5        B        &Y      D          W      During a ref neling shutdown the reactor coolant low pressere overpressure protection system relief valves operated Leadmit      191330  08/17/1984 39/21/1984    C      S1        FF                  C        45      9          5      the containment on                          penet rations f ailed t he intejratee leak rate test LEBd=12      191311  08/19/1984 09/24/1984    C      St        PF                  C        AU      D          8      Combined leak 00                            01                          rate from 4 valves escoeds limit for containment penet ration local leak rate test lea 0413    191618  38/21/1984 09/28/1984    C    FA        FF                  S        15      3          S7      Fa11ere of the JJ                                                        refueling pool seal due to improper destga LgEH414      191741  08/24/1984 09/28/1984    C    E1        F                    3        3B      &          $7      total loss of Et        g                            BG      G                  aormal off site LL                                                        power due to G                                                          maintena nce error on a dif f e ren tial relay current transf ormer -
output breaker for one diesel LEB841S    191112  08/20/1984 09/20/1984    C      NB        II                  C                S          W        Two steam am                                                        generators fall the first level of oddy current test LEB8416    191331  08/23/1984 09/28/1984    C    c)        00                  C        At      S          5      Dering a test an SS                          isolation valve in the aata y                                            steam drain line f ailed to close due to a beat
 
Nsaber  acc2ecTom toe:t            seyort    plant                                cocesacte abaarnai        sli3IIIcInca mecher        Dato      Dcto      S tatc0 SFCtes 59ei P    asat Inctr nont states  Condities ccese  Categsry  conne:t lea 4417  192019        10/04/1984 11/13/1984  C    ga      G                      &        &&      D        C7    Dejraded cabies AC                        la the reactor g rotection systes instrumentation that is nousted la the asia controi board Lssa418  192020        10/08/1984 11/14/1944  C    43      ff                      5        01      m        C7      4 fire door was found to be tropped opea LEEd419  195497        10/M/1984 01/30/1985    a    sc      00
* C        08      &        s      Containment 59                                                                    integrity tech spec is violated by operation of post accadest saapie systen -
tech spec witi te revised Lens 420  192275        10/13/1984 11/29/1984  8                                                OD      &        C3    cae worker receives high es pos are (guar terly
;                                                                                                                                          reading of 2.8 rea) -
angualified health physics technictaa j                                                                                                                                          assi)ned to area i
traut21  192201        11/03/1984'12/11/1984  3    11                    L          C        BF      M        C7    Seactor tripped during start-up physics tests due to operator etror
)              tend =22  192276        10/10/1984 12/06/1984  e    as      FF                      8        04      D        C7    Besident j                                                                    51                                                                  laspector j                                                                                                                                          discovered a fire barrier i
yenetration
!                                                                                                                                          without a face
!                                                                                                                                          tarrier seai LEade21  192790        10/31/1984 12/06/1984  C              F                                88      5        C7    gestin jhou se Ce    circuit breakers fati to close on demand 6 times j                                                                                                                                          in 5 mon th s d oe J                                                                                                                                          to dust on the relay a
 
7;ble B2    Codi2J Kheet ist 33gtrtabla Essatu et OcJda2 sock-1983. (custmed)                              C sesher    accession Evuat      Deport      Plant                                Component Ahmoraal        Si jaliica nce                    ,
s ea ber Date        Sete        States Systee Egelpaent Instremmat S ta t es  condition cause  Category    Coenent                #
LEade2e    192336  11/10/1984 12/1)/1984      3      In        00        E          S        SC        G        s        Cae portion of the reactor g rotec tion system was inoperable due to salvin) error during malatemance 192569  11/20/1984 81/04/1985      3      In        F        T          S        SF        N        C7      Opera tor lea 842S CS        99                            OJ                          inadvertently SC                                                                  tripped a reactor coolant peep - reactor tripped LEke426    192366  11/15/1984 12/24/1984      3    51        T          C        a        SF        D      C7      Circuit card
                                    -                                                          EC                          defect chaajed sain generator current -
opera tor maneatly tripped outpet breakers and initia ted manual reactor trip 14                  L          C        RR        D        5        Set point drif t LEE 8427  192411  11/15/19 64 12/26/1964    3 la overpower trip setpoints for 2 of a power range chamaels s      as        00                  C        At        D        C7      During a test, lea 8428  192367  11/16/1964 12/26/1984                                                      on                          11 of 16 mais steam safety valves lifted at a pressere lower
                                                            .                                                                than the e                    setpoint pressere lea 8429  195498  12/02/1984 D4/12/1985      3    IB                  L          3        sc        G        C6      Load reaback initiated (ESP) due to erroneosa
                                                                                                                              ' dropped rod-rod stop s alara caused by a power raa.je indicator that mas out of ad jus tment Ub 1
 
Table 52            Ccdisj Sheet for Ragortsbi3 Emots ct Caddae Neck-1984 - (Coetinued) usaber  accession Event      Report              Flaat                                  Component Abnors41        Sijaifica nce number  Date        Date              Status Systee Egsipeest Instrueest Sta t us      Coedition Cause  Category    Comeomt
                                                                                                                                                  ~
2136a14          08/01/1984 12/12/1944            C      34          FF                  s        O&      D        C7      1mo penetrations as                                                                    in the safety-relayted cable vault and the aus feed pump roos.were
                                                                                      ~
act scaled and no fire watch was established 2139414          10/30/1984 12/12/1984            c      SA          FF                  5        O&      B        C7        & toeporary fire AB                                                                  seal on a penetration was removed and no tire watch was established 4
Los                                                            *
 
      .  .,.~_
e    e t
Table 8.2.        Plant status, component status, and cause of reportable events Code  Plant status Component    Cause of reportable status            event A    Construction                    Maintenan a Administrative error and repair                                ,
B    Operation                      Operation    Design error Refueling l
C                                  Testing      Fabrication error                -
j                D    Shutdown                                    Inherent error 1
E                                                Installation error j                F                                                Lightning                    .
G                                                Maintenance error R                                                Operation error I                                                Weather s
i q
P e
l                                        [
4 I
e 0
 
l Table B.3. Systems involved with reportable events
(
Systes                .
Code Reactor                                                          RX 4            Reactor vessel internals                                      RA I
Reactivity control systems                                    RB Reactor core                                                  RC Reactor coolant and connected systems                            CX l
Reactor vessels and appurtenances                            CA Coolant recirculation systems and controls                    CB Nain steam systems and controls                              CC Main steam isolation systems and controls                    CD                      l Reactor corp isolation coo 11ag systems and controls          CE Residual heat removal systems and controls                    CF Reactor coolant cleanup systems and controls                  CG i          Feedwater systems and controls                                CE i'          Reactor coolant pressure boundary leakage detection systems  CI Other coolant subsystems and their controls                    CJ Engineered safety features                                        SX                      1
(          Reactor containment systems                                  SA
;          Containment heat removal systems and controls                SB Containment air purification and cleanup systems and controls SC            g Containment isolation systems and controls                    SD            g i(        Containment combustible control systems and controls          SE            d l          Imergency core cooling systems and controls                  SF
              . Core reflooding                                          SF-A Imer-pressure safety injection system and controls        SF-5 Righ-pressure safety injection system and controls        SF-C l      ,
Core spray system and controls          -
SF-D Control room habitability systems and controls                SG Other engineered safety feature systems and their controls    SH Containment purge system and controls                    SH-A Containment spray system and controls                    SH-B Auriliary feedwater system and controls                  SH-C Standby gas treatment systems and controls                SH-D Instrumentation and controls                                    IX Reactor trip systems                                          IA Engineered safety feature instrument systems                  IB Systems required for safe shutdown                            IC Safety-related display instrumentation                        ID Other instrument systems required for safety                  IE Other instrument systems not required for safety              IF L                    A
 
4                        ,
l Table 8.3 (continued)
( . ._ . .                                                                                                                                              --
.                                                                                        System
* Code i                                        Electric power systems                                                                                    EX Offsite power systems and controls                                                                    EA AC onsite power systems and controls                                                                  EB DC onsite power systems and controls                                                                  EC
:                                            Onsite power systems and controls (composite ac and de)                                                ED l                                            Emergency generator systems and controls                                                              EE Emergency lighting systems and controls                                                              EF Other electric power systees and controls                                                              EG i
Fuel storage handling systems                                                                            FX
,                                            New fuel storage facilities                                                                            FA
:                                            Spent-fuel storage facilities                                                                          FB Spent-fuel pool cooling and cleanup systees and controls                                              FC Fuel handling systems                                                                                  FD Auxiliary water systems                                                                                  WX Station service water systems and controls                                                            WA Cooling systems for reactor auxiliaried and controls                                                  WB Domineralized water askaup systems and controls                                                        WC                                  g Pocable and sanitary water systems and controls                                                        WD Ultimate heat sink facilities                                                                          WE                                  3 f                                    Condensate storage facilities                                                                          WF
      \                                    Other auxiliary water systems and controls                                                            WG Auxiliary process systems                                                                                FX
:                                            Compressed air systems and controls                                                                    FA Process sampling systems                                                                              PS 4
                      ,                      Chemical, volume control, and liquid poison
* systems and                                              PC i                                              controls Failed-fuel detection systems                                                                          PD Other auxiliary process systems and controls                                                          PE Other auxilisry systems                                                                                  AX
;                                            Air conditioning, heating, cooling, and ventilation systems                                            AA J                                              and controls a                                            Fire protection systems and controls                                                                  AB l                                            Commsunication systems                                                                                AC
!                                            Other auxiliary systems and controls                                                                  AD
)                                        Steam and power conversion systems                                                                        HX Turbine-generators and controls                                                                        HA Main staan supply systees and controls (other than CC)                                                HB Main condenser systees and controls                                                                    BC Turbine gland sealing systems and controls                                                            HD
 
l Table B.3 (continued)
(
System                                              .          Code Turbine bypass systems and controls                                                                            HE Circulating water systems and controls                                                                          HF Condensate cleanup systems and controls                                                                        HG Condensate and feedwater systems and controls (other than CH)                                                  HH Steam generator blowdown systems and controls                                                                  HI Other features of stesa and power conversion systems (not                                                      HJ included elsewhere)
Radioaccive waste management systems                                                                              MK
,                            Liquid radioactive waste management systems                                                                      MA i                          Gaseous radioactive waste management systems                                                            -
MB Process and effluent radiological monitoring systems                                                            MC Solid radioactive vaste management systems                                                                      MD i
Radiation protection systems                                                                                      BK Area monitoring systems                                                                                          BA Airborne radioactivity monitoring systems                                                                        BB Other                                                                                                            KK Not applicable                                                                                                  ZZ S
i 1
I i
l l
[
l                                                                                                                                                                                I I
1 l
1 i
t                                                                                                                                                                                1 l
I                                                                                                                                                                                I I. - , - . - _- - -,                      . _ . - -    . _ - ._ - - -        - . - . _ . . _ . _ _ . - - . - - - - -                _ ..    -.                  - - - - .
 
Table B.4.        Equipment and instruments involved in reportable events
                    - Code -                                                                Code Equipment A      Accumulator                                                  W  Internal combustion engine B      Air drier                                                    X  Motor C      Battery and charger                                          Y  Noszle D      Bearing                                                      Z  Pipe and pipe fitting E      Blower and dampero                                          AA  Power supply F        Breaker                                                    BB  Pressure vessel G      Cables and connectors                                        CC  Pressuriser H      Condenser                                                    DD  Pump I      Control rod                                                  EE  Recombiner J      Control rod drive                                            FF  Seal K      Cooling tower                                                GG  Shock absorber L      Crane                                                        HK  Solenoid M      Domineralizar                                                II  Steam generator N      Diesel generator                                            JJ  Storage container O      Fastener                                                    KK  Support structure P      Filter / screen                                              LL  Transformer
  . ..___ _            _.Q. _ . Flange                                                      MM  Tubing -          . - - _          _ _ _ . _ . . _ _
R      Fuel element                                                NN  Turbine S      Fuse                                                        00  Valve T      ' Generator                                                  PP  Valve, check                                      b
[                    U      Heat exchanger                                              QQ  Valve operator                                    $
V      Hester Instrumentation                                                                      _
A      Alarm                                                        L  Power range instrument
              -        5      Amplifier                                                    M* Pressure sensor C      Electronic function unit                                      N  Radiation monitor D      Failed fuel detection instrument                              0  Recorder E      Flow sensor                                                  P  Relay F      In-core instrument                                            Q  Seismic instrument
* G      Indicator                                                    R  Solid state device                                    t H      Intermediate range instrument                                S  Start-up range instrument I      Level sensor                                                  T  Switch J      Meteorological instrument                                    U  Temperature sensor K      Position instrument l
4
 
_-                _ .-          - _ __                                  --.~-._7--_    .
                                                                                              ,      w Table B.5. Abnormal conditions of reportable events
(
Mechanical              -
AA      Normal wear / aging /end of life: expected effect of normal usage AB      Excessive wear / clearance:        component (especially a moving com-ponent) experiences excessive wear or too much clearance or gap exists because of overuse, lack of lubrication AC      Deterioration / damage:      component is no longer at an acceptable level of quality (e.g., high temperature causes rubber seals to chemically break down or deteriorate, insulation breaks down) i              AD      Break / shear:    structural component physically breaks apart (not l                      when something " breaks down")
AE      Warp / bend / deformation:      shape of component is physically dis-torted
:              AF      Collapse:      tank or compartment has an external pressure exerted l                      that results in deformation AG      Seise/ bind /j as: component has inhibited, movement caused by crud, l                      foreign asterial, mechanical bonding, another component l              AH      Excessive mechanical loads:            mechanical load exceeds design l                      Mdu
!              AI      Mechanical fatigue: failure due to repeated stress AJ      Impact: the result of the force of one object striking another AK      Improper lubrication: insufficient or incorrect lubrication AL      Missing / loose: component is missing from its proper place or is loose or has undesired free movement i              AM      Wrong part: incorrect component installed in a piece of equip-              o-(
AN sent Wrong material:          incorrect anterial used during fabrication or      k i
installation A0      Weld-related failure:          failure caused by defective veld or
                  , located in the heat-affected zone AP      Vibration other than flow induced: vibration from any cause l                    other than fluid flow AQ      Crud buildup: buildup of foreign material such as dust, sticks, trash (not corrosion or boron precipitation)
AR      Corrosion / oxidation: unanticipated attack AS      Dropped:      component is dropped (includes control rod that is
                      " dropped" into core)
AT      lask . internal, within system: leak from one part of a system to another part of the same system AU      Leak, internal, between systems:          leak from one Epstem to a dif-farent system AV      Crack:      defect in a component does not result in a leak through I
the wall AW      Imak, external: defect in a component results in a leak from the system that is contained in an onsite building AX      I4ak to environment:        leak not resulting from a cracked or broken component AY      Was opened / transfers open:        component is/vas opened by error or spuriously opens
 
u
  .,      c.
Table B.5 (continued)
I_
AZ  Was closed / transferred closed:            component is/was - vrongly closed by error or spuriously closes BA  Fails to open:          component is in the closed state and fails to open on demand (e.g., the circuit breaker " fails to open" when an overcurrent occurs)
BB  Fails to closes            component is in the open state and fails to close on demand BC  Malposition or anladjustment:              component is out of desired posi-tion (e.g., normally open valve is closed) or adjusted improperly (not for instrument drift or out of calibration)
BD  Failure to start / turn on: component fails to start on demand BE  Stopped / failed to continue to run:              componant fails to continua running when it has previously started                                                          -
BF  Tripped:    component automatically trips on or off (desired or undesired) (e.g., the turbine tripped because of overspeed, the circuit breaker tripped because of overspeed, or the circuit breaker tripped because of overload)
BG  Deanergized/ power removed: component on systea loses its driving potential but not necessarily electrical power [e.g., (1) a fuse blows and there is no power to a sensor, and the sensor is de-energized; (2) a valve closes off the steam supply to a turbine, and the turbine has no driving power]
BE  Energized / power applied:            component or system gains its driving potential but not necessarily electrical power                (e.g., valve is
(              opened allowing steam to turn a turbine)
BI  Unacceptable response time:              component does not respond to a                    g demand within a desired time frame but does not otherwise fail                                ;I (e.g., a diesel generator fails to come to full speed within the time constraint)                                                                            -
BJ  High pressure: higher than normal or desired pressure exists ic a component or system (does not include instrument aisindica-tions)
BK  Iow pressure:      lower than normal or desired pressure exists in a component or system (does not include instrument aisindication)
B1. High temperature: component experiences a higher than normal or desired temperature BM  Iow temperature: component (or system) experiences a lower than normal or desired temperature BN  Freezing:    fluid medium (e.g., water) freezes in or on a com-ponent 50  Excessive thermal cycling:              frequent changes in temperature that could result in metal fatigue or cracking BP  Unacceptable heatup/cooldown rate:                    heatup or cooldown rate exceeds limits BQ  Thermal transient: system experiences an undesired or unstable thermal transient or thermal change BR  Excessive number of pressure cycles: system experiences an un-desired number of significant pressure changes (e.g., pressure pulses as from a positive displacement pump)
_.    . - , . .  . _ . . - . . . .  . .  -      ..      .  -      ..    ..-.....v-.-,.-...
 
se a          . . -      - ..                          - - - -          u        -          +    . .
                                                                                                          .u      ;
Table B.5 (continued)
(
BS  High level / volume: higher than normal or des' ired level or volume exists (actual or potential)' in a component, such as tank or sump, or area, such as auxiliary building (not for instrument misindication)
BT  Iow level / volume:                    lower than norac1 or desired level or volume exists in a component (not for instrument misindication)
BU  Abnormal concentration /pH: an abnormal (either high or low) con-centration of a chemical or reagent exists in a fluid system or an abnormal pH exists (does not include abnormal boron concentra-tion)                                          ,
BV  Abnormal boron concentration:                            process system control rod has an abnormal boron concentration from burnup, dilution, or overaddi-tion SW  Overspeed:        speed in excess of design limits BX  Cladding failure:                        cladding of a component fails (e.g., the cladding of a fuel pellet is breached, and radioactive fuel leaks occ)
BY  Burning / smoking:        component is on fire or smoking BZ  Engaged:        component engages or meshes (this is not to be used when a component binds or becomes stuck or jaianed)
CA  Disengaged / uncouple'd: component disengages, loses required fric-tion, or is no longer meshed (as in gears), for example, the clutch on the actor disengages from the shaft (this should not be used for dropped control rods)
(                                              Electric / instruments                                        u_
EA  Excessive electrical loads:                              electrical loads exceed design            -
rating                                                                                              E EB  Overvoltage/ undercurrent:                            component failure produces an over-voltage / undercurrent condition other than open circuits
      . EC  Undervoltage/overcurrent: component failure produces                            an under-voltage /overcurrent condition other than shorts ED  Short circuit / arcing / low impedance: electrical component shorts or arcs in the circuit or has a low impedance including shorts to ground EE  Open circuic/high impedance / bad electrical contact:                          electrical component has a structural break, or electrical contacts fail to contact sad fail to pass the desired current
;      EF  Erratic operation:                      component (especially electrical or instru-ment) behaves erratically or inconsistently (if an instrument produces a bad but constant, signal, use "EG", if an instrument produces an inconsistent signal use "EF")
EG  Erroneous /no signal: electrical component or instrument produces an erroneous signal or gives no signal at all (not for out-of-calibration error)
EH  Drifc:      a change in a setting caused by aging or change of physi-cal characteristics (does not include personnel errors or a physical shift of a component) l
: u.                    .  .
 
1      + 9-
* Table 5.5 (continued)
(                    EI      out of calibration:                component (particularly instruments) become out of adjustment or calibration (does not include drif t)
EJ      Electromagnetic interference:                      abnormal indication or action resulting from unanticipated electromagnetic field EK      Instrument snubbing: dampening of pulsating signals to an in-stcument Hydraulie HA    High flow:            higher than normal or desired flow exists in a com-ponent/ system (does not include instrument aisindication) (see code EG)
EB    Low flow:            lower than normal or desired flow exists in a com-ponent/ system (does not include instrument aisindication)
EC    No flow or impulse:                    fluid flowing through a pipe, filter, orifice, or trench or the fluid in an impulse line (e.g., instru-ment sensing line) is blocked completely or decreased due to some foreign material, crud, closed (either partially or completely) valve or damper, or insufficient flow area HD    Flow induced vibration HE    Cavitation HF    Erosion                                ,
HG      Vortex formation HE      Water hammer HI      Pressure pulse / surge HJ    Air / steam binding
(                  HK      Loss of pump section
* HL      Boron precipitation Other
[p
                    . 0A    Declared inoperable:                  component or system is declared inoperable
          ,                  as required by Technical Specification's but any be capable of partially or completely performing its desired duties when re-quested (a component / system that is completely failed should not use this code) 08    Flux anomaly:              flux characteristics of the reactor core are not l                            as required or desired (e.g., flux spika due to xenon burnout)
OC    Test not performed:              operator or test personnel fails to perform a required test within the required period OD    Radioactivity contamination:                    component, system, or area becomes more radioactive than desired or expected OE    Temporary modification:                an installation intended for short term use (usually this is for maintenance or modification of installed equipment)
I                    0F      Environmental anomaly OG      Airborne release OH      Waterborne release OI      Operator communication OJ      Operator incorrect action OK      Procedure or record error l                -.      ..        .  . - . . - - . . - -    - -
                                                                        -<    ---m  ,,~~-r-  -
t-  ~ ~~ ~ ~ r
 
                                                                                      . r Table 5.6. Significance Criteria for reportable events - Significant
                    ,                              Evenn description 51        Two or more failures occer in redundant systems during the same event S2        Ttso or more failures due to a common cause occur during the same event S3        Three or more failures occur during the same event S4        Component failures occur that would have easily escaped detection by testing or examination
                  $5        An event proceeds in a way significantly different from what would be expected 56          An event or operating condition occurs that is not enveloped by the plant design bases 57        An event occurs that could have been a greater threat to plant safety with (1) different plant conditions, (2) the advent of another credible occurrence, or (3) a different
,                            progression of occurrences 4
S8          Administrative, procedural, or operational errors are committed that resulted from a fundamental misunderstand-ing of plant performance or safety requirements S9          other (explain)
                                                                                          ~
                                                                                        +
 
i  T(
4, Table B.7. Significance criteria for reportable events -- Conditionally Signifi. cant Category of conditional                        Event description significance C1        A single failure occurs in a nonredundant system C2        Two apparently unrelated failures occur during the same event C3        A problem results in an offsite radiation release or ex-posure to personnel C4        A design or manufacturing deficiency is identified as the cause of a failure or potential failure C5        A problem results in a long outage or major equipment damage C6        An engineering safety feature actuation occurs during an event C7        A particular occurrence is recognized as having a sig-nificant recurrence rate C8        Other (explain) o-e}}

Latest revision as of 03:48, 8 December 2024

Draft Review of Operating Experience History Through 1984 of Haddam Neck for NRC Isap
ML20199L730
Person / Time
Site: Haddam Neck File:Connecticut Yankee Atomic Power Co icon.png
Issue date: 07/03/1986
From: Clemans V, Kimmins A
OAK RIDGE NATIONAL LABORATORY
To:
Office of Nuclear Reactor Regulation
Shared Package
ML20199L726 List:
References
CON-FIN-A-9469 ORNL-NOAC-231, ORNL-NOAC-231-DRFT, NUDOCS 8607090593
Download: ML20199L730 (228)


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