0CAN088507, Responds to Violations Noted in Insp Rept 50-368/85-17. Corrective Actions:Incident Reviewed W/Operations Personnel to Emphasize Importance of Category E Valve Administrative Controls & Documentation

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Responds to Violations Noted in Insp Rept 50-368/85-17. Corrective Actions:Incident Reviewed W/Operations Personnel to Emphasize Importance of Category E Valve Administrative Controls & Documentation
ML20132B201
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 08/25/1985
From: Enos J
ARKANSAS POWER & LIGHT CO.
To: Denise R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML20132B161 List:
References
0CAN088507, CAN88507, NUDOCS 8509260124
Download: ML20132B201 (3)


Text

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ARKANSAS POWER & LIGHT COMPANY POST OFFICE BOX 551 UTTLE ROCK. ARKANSAS 72203 (501) 371-4000 August 25, 1985

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l OCAN088507 lQ)G ? Q g jlz

.il Mr. Richard P. Denise, Director J

__ ___ _ _ _ M Division of Reactor Safety and Projects U. S. Nuclear Regulatory Commission Region IV 611 Ryan Plaza Drive, Suite 1000 Arlington, TX 76011

SUBJECT:

Arkansas Nuclear One - Units 1 & 2 Docket Nos. 50-313 and 50-368 License Nos. DPR-51 and NPF-6 Response to Inspection Reports 50-313/85-16 & 50-368/85-17 Gentlemen:

The subject inspection reports have been reviewed.

A response to the Notice of Violation is attached.

Very truly yours, t

/

. Ted Enos Manager, Licensing JTE: RJS: ds Attachment cc:

Mr. James M. Taylor Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission Washington, DC 20555 Mr. Norman M. Haller, Director Office of Management & Program Analysis U. S. Nuclear Regulatory Commission Washington, DC 20555 g9260124 850918 G

ADOCK 05000368 PDR gmrbr MEMBEA MtOct.E SOUTH UTIUTIES SYSTEM L

.o NOTICE OF VIOLATION During an NRC inspection conducted during the period June 1-30, 1985, a violation of NRC requirements was identified.

The violation involved the failure to follow the requirements of a valve lineup procedure.

In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1985), the violation is listed below:

Unit 2 Technical Specification 6.8.1 requires that, " Written procedures shall be established, implemented and maintained covering... a.

The applicable procedures recommended in Appendix "A" of Regulatory Guide 1.33, Revision 2, February 1978."

Plant Operating Procedure 2102.01, " Plant Pre-heatup and Pre-critical Checklist," has been established in accordance with this Technical Specification.

Section 3.5 of Attachment E to Procedure 2102.01 requires any valve not in the required position be listed on the Category E valve log sheet (Form 1015.01C).

Contrary to the above, Category E valve 285-32 was found to be out of its required position on June 3,1985, yet no entry was made on Form 1015.01C.

This is a Severity Level V violation (Supplement I.E) (368/8517-01).

Response

On May 12, 1985, in preparation for plant heatup after the ANO-2 fourth refueling outage, alignment verification of Category "E" valves was performed as required by Plant Pre-Heatup and Pre-Critical Checklists procedure.

During the performance of this alignment verification, all valves that were not positioned to their required Category "E" position were identified and were listed on the Category "E" Valve Log Sheet in the control room.

While performing final checks and realignment of these valves during plant heatup, an error was made concerning the required locked position for valve 285-32.

An entry was made on the Category "E" Valve Log Sheet specifying that valve 285-32 should be " LOCKED OPEN".

The required Category "E" position for this valve is " LOCKED CLOSED".

This error resulted in the valve being verified in the incorrect position.

Also, as a result of the entry for the valve being incorrectly completed on the Category "E" Valve Log Sheet, no record existed to indicate that 285-32 was not in the correct Category "E" position.

The NRC resident noted this discrepancy on June 3, 1985.

As stated in the body of the report, the Unit 2 operator immediately entered 28S-32 on the valve exception Ifsted as required by procedure.

I

An~ independent review of this. incident was conducted.

As a result, the

-following actions will be taken to prevent recurrence:

1.

Review of the incident with Operations personnel with. emphasis on the-importance of Category "E" valve administrative controls and

. documentation.

2.

Performance of a ' detailed review of procedures relating to Category "E" valve alignments and administrative controls and revision of these

. procedures to provide clear, unambiguous instructions concerning their i-use.

3.

Detailed operator training on the use of procedures relating to Category "E" valves.

Full compliance was achieved when an entry was made.on the Category "E" Valve Log Sheet for 285-32 on June 3, 1985.

Actions to prevent recurrence are planned'to be completed by October 11, 1985.

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