05000259/LER-1981-041-03, /03L-0:on 810722,while Performing Turbine Bldg Vent Monitoring Sys Tests,Operate/Test Switch on Continuous Air Monitor 1-RM-90-249 Would Not Operate.Caused by Equipment Malfunction.Vents & Fans Isolated & Tagged

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/03L-0:on 810722,while Performing Turbine Bldg Vent Monitoring Sys Tests,Operate/Test Switch on Continuous Air Monitor 1-RM-90-249 Would Not Operate.Caused by Equipment Malfunction.Vents & Fans Isolated & Tagged
ML20010B065
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 08/07/1981
From: Holder G
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20010B060 List:
References
LER-81-041-03L-01, LER-81-41-3L-1, NUDOCS 8108130276
Download: ML20010B065 (2)


LER-1981-041, /03L-0:on 810722,while Performing Turbine Bldg Vent Monitoring Sys Tests,Operate/Test Switch on Continuous Air Monitor 1-RM-90-249 Would Not Operate.Caused by Equipment Malfunction.Vents & Fans Isolated & Tagged
Event date:
Report date:
2591981041R03 - NRC Website

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d l o l > J l During ref ueling outage, while performing turbine building vent monitoring systems g

switch on continuous air monitor (1-RM-90-249),

(SI 4.8.B.4-2) the operate / test lnj3l l tests for the turbine building roof exhaust would not operate, rendering the monitor [o la j l There was no danger to the health or safety of the g

j inoperable per T.S. 3.8.B.8.

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. B F 15. 2 f arowns Ferry Nnclear Plaitt G/04/81 1.F.1: StTPI !.101F.NT AI. INil >RM ATION ItiiltO-f20 _ 259] _81041, Technical Specil'ication in co!ved 3.,8.B.8' _ _ _.

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8 Iteported Under Tecluiical Specificati< n,6.7.2.b(2)

  • nate due NRC:

I) ate sif Occurrence. 7/22/81 Time of Occurrence 0400 Unit 1

Identification and Description r,f Occurrence:

Operate /tsht s#itth"ori thW~cbstiinuous ai'r monitor (1-RM-90-249) for the

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turbine building roof exhaust would not operate, rendering the monitor inoperable.

Canditions Prior to Occurrence Unit I refueling outage.

Unit 2 at 100%.

Unit 3 at 97%.

Action specified in the Technical Specification Surveillance Requirements met.

d:ie to, inoperable e3tuipment. Describe.

None Appar ent Cause of Occurrence:

Equipment malfunction. The operate / test switch was placed in test'during 4

SI performance and could not be returned to operate.

Analv:.is of ()c"urrence There was no danger to the health or safety of the public, no release of activity, no damage to the plant or equipment. and no resulting significant chain of events.

- Corrective Action:

The vents and fans were isolated and tagged. The continuous air monitor was repaired and returned to service at 1530.on 7/22/81. This is considered a' random event and no recurrence control is required.

.F.ai__ lure Da_t.a:

None Iterention :

Pr 1 - - I.ifetime; llesponsibility - Document Control Supervisor d'/

tiles ision :.

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