LER-1981-035, Left Bank Starters Would Not Develop Min Rotational Speed During Testing.Caused by Normal Wear,Dirt & Grit in Air Start Sys.Air Start Motor Replaced |
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| 2591981035R03 - NRC Website |
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u. S. NUCLE AR REGULATORY COMMISSION NRC FORM 366 UPDATE REPORT - PREVIOUS REPORT DATE 7/15/ ;l (7 77)
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H tw 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 F VE N T DESCRIPTION AND PnOBA3LE CONSEQUENCES h l With unit 1 in refueling outage and units 2 and 3 in steady state, during diesel l
,, 2 g g l generator redundant start test (EMI-3), left bank starters would not develop l
[nl4l l minimum rotational speed. Diesel generator B was removed from service to r7 pair l
l air start motors. (T.S. 3.9.B.2)
Diesel generator B is common to units 1 and 2.
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FITil i There was no danger to the health or safety of the public. Redundant systems were
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t ioin I i 74021W, 75008W, 81020; 296/81023.
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44 41 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l i l o ] l Normal wear, dirt, and grit in the air otart system. The Ingersoll-Rand model l
i i l D89Ril46 air start motor, size 150 EMP, pressure class 200 psi, pneumatic activation, f j was replaced. Recurrence control: clean and inspect air start motors and actuation l i,
J [il3ll valves semiannually and rebuild all air start motors (new vanes, worn parts, l
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liep rted ilnder Technical Sp"cificatirin 6.7.2.b(2)
ADate elue tH:C:
N/A Date of Occurrence,6/20/81 Time of Occurrence _, 103,0 Unit 1 and_2__,,__,
Identification and liescript. ion,,9f Oc,currence i
Diesel generator B.was removed.from service to repair lef t bank air start motors.
Centrlitions Prior to Occurrence:
Unit 1 in refueling outage.
l Unit 2 at 76%.
Unit 3 at 77%.
5 Action t.pe ific.I in :h+ Technical Specification Surs edlaner itequirements mes 3
'o inoperabh; eiptipraent,._ Ihperibe. _, _
'. ae Het surveillance requirements of T.S. 4.9.B.2.
i Apparent Cause of Occut'rence-Normal wear, dirt, and grit in the air start motor.
l Analysis c.i (>ccurrenre There was no danger to the health or safety of one public, no release of i-activity, no damage to the plant or equipment,'and no resulting significant chain of events, i
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i Corrr clive Ac.t._io. _n :
Replaced the air start motor. Recurrence control: clean and inspect air start motors-and activation valves semiannually and rebuild all air start motors (new vanes, worn parts, etcetera) annually.
Failure I)ata:
BFRO-50-259/74004W, 74012W, 74013W 75008W, 81020; 296/81023.
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| 05000260/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000260/LER-1981-001-01, /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | | | 05000259/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001-03, /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | | | 05000259/LER-1981-001-03, /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | | | 05000260/LER-1981-002-03, /03L-0:on 810102,scram Discharge Instrument Vol Rod Block Level Switch 2-LS-85-45E Found Set at 27 Gallons. 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