LER-1981-040, /03L-0:on 810625,during Testing,Grinnell Snubber SS7 Was Found Low on Fluid.Caused by Leak at Threaded Connection Between Fluid Reservoir & Snubber.Grinnell Model F-16200,Size 2.5,Type HSSA-10 Snubber (Sn 10734) Rebuilt |
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| 2591981040R03 - NRC Website |
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j e 121 l During refueling ourage, while performing functional testing and corrective adjust-i g
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o # 3 } l ments to Grinnell hydraulic shock arrestors (MMI-59B), Grinnell snubb'er No. SS7
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o141 I was found low on fluid when visually inspected per SI 4.6.H.
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 d reservoir and the snubber.
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Browns Ferry Nucleut-Plant 6/04/81 i, '
t LER SUPPLEMENTAL INFORMATIOli h
Table 3.6.H.
s B F RO 259 / 81040 Technical Specification involved
l 1200 Unit 1
Date of Occurrence 6/25/S1
_ Time of Occurrence l
Identification and Des,cription of Occurrence:
H While performing le(I-59, snubber No. SS7 was found inoperable.
I 1
ll Conditions Prior to Occurrence:
tl-Unit 1 in refueling outage.
Unit 2 at 100%.
l Unit 3 at 97%.
Action specified in.the' Technical Specification Surveillance Requirements met due to inoperable equipment.
Describe.
None i
t Apparent Cause of Occurrence:
A ' leak at the threaded connection between the fluid reservcir and the snubber, probably caused by improper thread sealant.
Analysis of Occurrence:
There was no danger to the health or safety of the public, no release of and no resulting significant activity, no damage to the plant or equipment, chain of events.
Corrective Action
Snubber will be rebuilt and a suitable titread connection sealant used.
Inspection intervals for snubbers will be changed per SI 4.6.H because this snubber was found inoperable.
Failure Data:
None Retention:
Per d - Lifetime; Responsibility - Document Control Supervisor titevision :
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| 05000260/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000260/LER-1981-001-01, /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | /01T-0:on 810102,scram Discharge Vol Level Switch 2-LS-85-45A Found Inoperable & -C & -D Found Offscale.Caused by One Robert Shaw Switch Model SL-305-EI-X Sticking & Setpoint Drift.Stuck Switches Float Chamber Back Flushed | | | 05000259/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000296/LER-1981-001-03, /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | /03L-0:on 810106,both Smoke Detectors in Reactor Bldg Fixed Spray Zone Were Inoperable.Caused by Loose Screw in Terminal Block.Screw Replaced | | | 05000259/LER-1981-001-03, /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | /03L-0:on 810105,core Spray Sparger to Reactor Pressure Vessel D/P Switch 1-PDIS-75-28 Found Set Above Tech Spec Limit.Caused by Barton Model 288 Setpoint Drift.Switch Replaced W/New Switch on 810115 | | | 05000260/LER-1981-002-03, /03L-0:on 810102,scram Discharge Instrument Vol Rod Block Level Switch 2-LS-85-45E Found Set at 27 Gallons. 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