05000259/LER-1981-017-03, /03L-0:on 810423,Athens 161Kv Line & D Cooling Tower Switch Gear Tripped.Diesel Generators Failed to Immediately Demonstrate Operability Per Tech Spec 4.9.B.1. Caused by Personnel Error.Operators Will Review Incident

From kanterella
(Redirected from ML20004B150)
Jump to navigation Jump to search
/03L-0:on 810423,Athens 161Kv Line & D Cooling Tower Switch Gear Tripped.Diesel Generators Failed to Immediately Demonstrate Operability Per Tech Spec 4.9.B.1. Caused by Personnel Error.Operators Will Review Incident
ML20004B150
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 05/22/1981
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20004B147 List:
References
LER-81-017-03L-01, LER-81-17-3L-1, NUDOCS 8105270300
Download: ML20004B150 (2)


LER-1981-017, /03L-0:on 810423,Athens 161Kv Line & D Cooling Tower Switch Gear Tripped.Diesel Generators Failed to Immediately Demonstrate Operability Per Tech Spec 4.9.B.1. Caused by Personnel Error.Operators Will Review Incident
Event date:
Report date:
2591981017R03 - NRC Website

text

!

?

U.S. NUCLEAR REGULATORY COMMISSION N R"~'3M 366.

I 17 (V LICENSEE EVENT REPORT e@

cONiRot sLOCx: l 1

l l

I l

l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) i l A l L l B l R l F l 1 l@l 0 l 0 l - I O l 0 l 0 l 0 l 0 l-l 0 l 0 l@l 4 l 1 l 1 l 1 l 1 l@l I

l@

o i I

H

LICENSEE CODE le 15 LICENSE NUMSER 25 26 LICENSE TYPE J0 SF CAT $6 CON'T lol l 3[*,c % )0l5l01010]2l5l9 @l0l4l2l3l8l1l@l 0]5l2l2l8l1 g i

8 60 61 DOCKET NUMBER 68 69 EVENT DATE 14 7S REPORT DATE 80 EVENT DESCRIPT!ON AND PROBABLE CONSEQUENCES h l On two separate occasions (4/23/81 and 4/24/81) during normal operation, the Athens I

lo [2]

l 161 KV line and "D" cooling tower switchgear tripped. Units 1 and 2 diesel l

io ;3i

[ generators were not demonstrated operable immediately as required. (T.S. 4.9.B.1) l [o l4 )

[ o l s i l There was no danger to the health or safety of the public. There were no redundant l

Iu is l l systema, There were no previous similar events.

I I

lolill l

l o t a l L_

if0 SYSTEU

CAUSE

CAUSE COMP.

VALVE COJE CODE SUSCODE COMPONENT CODE SUSCODE SUSCODE lo191 i Zl Zl@ l Al@ l A l@ lZ lZ lZ lZ lZ lZ l@ ]@ @ @

1 d

9 to 11 12 13 18 19 20 SEQUENTI A L OCCURRENCE REPORT REVISION

_ EVENT YE AR R EPORT No.

CODE TYPE No O,"(j[,g/ROl8 l1 l l_l l0 l1 l 7 l y

l 0l 3l lLl l_]

Q R

Rr

_ 21 22 23 24 26 27 N

N 34 31 32 TA EN A TO ON PLANT ME MoVR$

$8 iT FOR 8.

SUPPLIE MAN FACT RER lHj@lGl@

lZI@

Lz_JO I of 01 01 ol W@

IN l@

l Z l@

lZl9]9]9l@

JJ J4 35 26 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

T.S.4.9.B.l.

l l i i o I l Personnel failed to recognize and comply with the requirements of Iiii] l Recurrence control: Operators will review this incident during retraining. Form i

I i 1 1 I BF-14 (Licensee Reportable Event Determination) will be revised to include a

[

I liIii l signoff that applicable SI's are performed.

I ii la I l 80 e

51A u

% POWER OTHER STATUS 015 V RY DISCOVERY DESCRIPTION NA l

lBl@l Operator observed l

li I'-l LJij @ l 0 ! 0 l 0 l @ l

'2

'8

' ?nvity ce2rsor AucuNroF ACTiviiv h 4

toCArloN OF RELEASE mtE A..Eu OF acu A.5 NA l

l NA l

It 161 d @ W@l PsnsoEetr,Pm2Aes d '

cEseniPTiON @

no.wsw rvPe l

liltj I0l0lQJ@lZl@l NA n w onNi,'in c.',ic anco,P noN@

.u.....,

l lt I l l Ol Ol Ol@l NA 30 s +,

at 12 t ira os or DMtAfA TO F ACIL'TY lvPC 12E'iCDIP T I(IN l

[,1IIzl@l NA w

i.,

,.in t leip T ION l

lllllllII!l!Il j.' l +. l l

NA 64 69 au ;

i 4

in O

PHONE 810 5 27 0'f h" PDEDARER N A?

o l

t b

Tennessee Valley Authority Form BF-17 Browns Ferry Nuclear Plent BF 15.2 3/24/81 LER SUPPLEMENTAL INFORMATION BFRO 259 /a1017 _ Technical Specification Involved 4 9.B.1 Reported I'nder Technical Specification 6.7.2.b (2)

Date of Occurrence 4/23/81

, Time of Occurrence 152r Unit 1&2

!dentification and Description of Occurrence,:

Personnel failed to run SI's when Athens 161 KV line tripped.

Conditions Prior to Gecurrence:

Unit I refueling outage.

Unit 2 at 98%.

Unit 3 at 95%

Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment. Describe.

~

Required testing was not performed.

Apparent Cause of Occurrence:

Personnel failed to recognize the requirements of T.S. 4.9.B.l.

Analysis of Occurrence:

There was no danger to the health or safety of the public, no release of activity, no damage to plant or equipment, and no resulting significant chain of events.

I i

l t

Corrective Action

1 Reinstructed personnel threugh retraining. Form BF 14 will be revised to include a signoff that applicable SI's are performed.

i

~

Failure Data:

None

~

  • Reten tion : Period - Lifetime; Responsibility - Document Control Supervisor
  • Revision :