05000366/LER-1980-147-03, /03L-0:on 801029,drywell Hydrogen Dioxide Analyzers 2-P33-P001A & B Found Inoperative.Cause Unknown. Vendor & Util Investigating Failure

From kanterella
(Redirected from ML19345B494)
Jump to navigation Jump to search
/03L-0:on 801029,drywell Hydrogen Dioxide Analyzers 2-P33-P001A & B Found Inoperative.Cause Unknown. Vendor & Util Investigating Failure
ML19345B494
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 11/20/1980
From: Nix R
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19345B490 List:
References
LER-80-147-03L, LER-80-147-3L, NUDOCS 8012010393
Download: ML19345B494 (2)


LER-1980-147, /03L-0:on 801029,drywell Hydrogen Dioxide Analyzers 2-P33-P001A & B Found Inoperative.Cause Unknown. Vendor & Util Investigating Failure
Event date:
Report date:
3661980147R03 - NRC Website

text

.A 30G U.S.PlVC #fe mThnY COMMISSIO*J

/

LICENSEE EVENT REPORT CONTROL O LOCK: l l

l l

l l lh (PLEASE PRINT On TYPE ALL REQUIRED INFORMATION) 1 6

lG l Al El I I H j 2 l@l 01 0101 0101 01010 l Ol 0101@26l4lllllllll@!

I l@

LICENSEE CODE 14 15 (ICENSE NUMBEH 25 UCENSE TYPE JO bi CAT 18 DN' 01 510101013 I 616 l@l 1101 219 I R I 01@l1 111210 l 8 l 0 l@

itJ S' "J l L l@l 8

LO G8 DOCKET NUVUER f3 63 EVENT DATE 74 7h REPORT DATE 80 EVENT DESCRIPTION AND PRODABLE CONSEQUENCES h (Drywell H 0g Analyzers) I E lWhile operating at 2397 MWt, 2P33-P001A and B, 7

g gwere found to be inoperative.

Tech Specs section 3.3.6.4 r'equires both l iTilIchannels t; be operative during power operation.

The plant was placed I

I iTslf n a 30 day LC0.

The health and safety of the public was not affected. l i

I g lThis is a repetitive event as last reported on Reportable Occurrence I

i iTO 150-366/1980-130.

I

>nii

'l 80 as DE CO E SU C E COMPONENT CODE SU8 CODE SU E

E I S I E l@ W@ [_X_j @ l X I XI X l X I X l X I@ [Z_l@ l Z l @

SEQUENTIAL OCCURRENCE REPORT REVISION LE R EVENT YEAR REPORT NO.

CODE TYPE N O,

@,ajg/RO I 81 01 L-]

111 417i M

lo I 31 It I l-l 10 I 21 22 23 24 26 27 28 29 30 31 32 "iU

  1. '2CW Ot L

$WTWO HOURS @ ^SU h" k$

T FO 5

R" M

ER K

l LD.J@

l._ZJ@

l_zl@

L01010 lo l I v l@

l N l@

l A l@

lD 10 l 9161@

33 34 3h 36 3

40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Qi] IThe cause o f the f ailure is unknown at the time of this report.

The I

l s ii i Iplant has shutdown for refueling and a vendor representative has been l

I m ischeduled to assist plant personnel in the checkout and repair.

A I

lg l followup report will be written following the return of the instruments I i

I i

,9ii o service.

I j

t 8 g 80 M

sA S

% POWER OTHER STATUS is O RY DISCOVERY DESCRIPTION g

i Is l y@ l 0 l 918 l@l NA l

[B_j@l Operator inspection l

A TIVITY CO TENT RELE AsE OF REL E ASE AMOUP.T OF ACTIVITY LOCATION OF RELEASE ilel @

[Z_J@l NA l

l NA l

3 9 to 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE

DESCRIPTION

l 7l 10 10 l Ol@l Z l@l NA l

,ERSO~~it.~;ULS I-OESCniPnO~@

NUMun lR Ll Ol 0101@l NA l

l

%S,OrOaO/jAGE O FACluTY g I

l t> l l Zlgl NA l

!j

.0

.0 TrEl in_j@L'SCn,nO~@

go 12 o 103M

.ssui"""

"ac "S' l

NA l

ll;;;;;illl;l:;

8 9 10 G8 69 SO E R

T. N i x 912-367-7781 8

-*^

'LER'#':

50-366/1980-147

~

Licensee:.-Georgia Power Company

-([)'

FacilityLName:

Edwin I. Hatch Docket #:- 50-366 i

Narrative

Report-for LER 366/1980-147 1

l On October 29, 1980.while operating'at 98% power, 2P33-P001A and B Analyzers) were found to be giving erroneous indica -

-(Drywell H202 7

)

j.

tions.

Tech-Specs section 3.3.6.4 requires both instruments to be operative during power operation.

The plant was placed in a 30 day-

~

l Limiting Condition of Operation.

The health and safety 4of the-public was not affected.

This is a repetitive event as last reported on reportable occurrence 50-366/1980-130.

At-the time of this report: the' cause of the event had r,ot been -deter-mined.

.The plant has~ shutdown for refueling and a factory represent-d oative has been scheduled:on site to assist with the investigation an

. repair.

The analyzers are not required to be. operable during cold shutdown.

y Unit.I does not; utilize:this type analyzer.

Further generic review will be conducted upon the completion of the maintenance and a follow-(]) up report-submitted.

T l

4 l

1 i

4

)

f g

r b

J

  • ~I'?*-

m-

~.9