05000259/LER-1980-063-03, /03L-0:on 800820,during Normal operation,CAM-1-RH- 90-251 for Turbine Bldg Roof Vent Removed from Svc for Period Exceeding 1-h Due to Failure of Schwitzer Series 325 Model 145473 Vacuum Pump.Pump Replaced

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/03L-0:on 800820,during Normal operation,CAM-1-RH- 90-251 for Turbine Bldg Roof Vent Removed from Svc for Period Exceeding 1-h Due to Failure of Schwitzer Series 325 Model 145473 Vacuum Pump.Pump Replaced
ML19338D742
Person / Time
Site: Browns Ferry 
Issue date: 09/16/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19338D733 List:
References
LER-80-063-03L-01, LER-80-63-3L-1, NUDOCS 8009230714
Download: ML19338D742 (2)


LER-1980-063, /03L-0:on 800820,during Normal operation,CAM-1-RH- 90-251 for Turbine Bldg Roof Vent Removed from Svc for Period Exceeding 1-h Due to Failure of Schwitzer Series 325 Model 145473 Vacuum Pump.Pump Replaced
Event date:
Report date:
2591980063R03 - NRC Website

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- 1/10/79 LER SUPPLEMENTAL INFORMATION DFRO-50.- 259. - /. 8063 -

Technical Specification Involved 4.8.B.l.a

.!!eported Under Technical Specification 6.7.2.b(2)

Date of Occurrence 8/20/80 Tihte of Occurrence 0853 1

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~ Identification and Description'of Occurrence:

While performing SI 4.8.B.4.2, CAM l-RM-90-251 for the turbine building vent was removed from' service-for a period exceeding one hour.

r Conditions Prior to Occurrence:

U-l at 96% We.

U-2 at 93% We U-3 at 100%'MWe Action. inoperable equipment.specified in the Technical Specification Surveillance Req due to Describe.

Chemical Laboratory notified to take samples.

Apparent Cause of Occurrence:

Vacuum pump failure.

Analysis of Occurrence:

There was no danger to the health or safety of the public, no damage to the plant equipment, and no resulting significant chain of events.

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Corrective Action':

The vacuum pump was' replaced. Personnel were cautioned to be more attentive to

.the time limit that the equipment can 1,a out of. service.

Failure D' ta:

a 259/ 74'3%- 259/795, 259/796,. 259/7924, 259/8032 and 260/782.0.

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