05000259/LER-1980-036-03, /03L-0:on 800422,during Steady State Conditions, 1B Recirculation Motor Generator Set Tripped During Transfer from Alternate to Normal Power Source.Cause Unknown.Transfer Later Accomplished W/No Problems

From kanterella
(Redirected from ML19323F770)
Jump to navigation Jump to search
/03L-0:on 800422,during Steady State Conditions, 1B Recirculation Motor Generator Set Tripped During Transfer from Alternate to Normal Power Source.Cause Unknown.Transfer Later Accomplished W/No Problems
ML19323F770
Person / Time
Site: Browns Ferry 
Issue date: 05/21/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19323F767 List:
References
LER-80-036-03L-01, LER-80-36-3L-1, NUDOCS 8005290451
Download: ML19323F770 (2)


LER-1980-036, /03L-0:on 800422,during Steady State Conditions, 1B Recirculation Motor Generator Set Tripped During Transfer from Alternate to Normal Power Source.Cause Unknown.Transfer Later Accomplished W/No Problems
Event date:
Report date:
2591980036R03 - NRC Website

text

fy",$,]"*' '""

t' s nucLkt R nLoutAweiv conausssion LICENSEE EV

.crOtt1 coNTRot eLOct.: l l

l l

l l

l (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATIONI

. l0 l1l l Al Ll B l R l Fl 1 l@l 0 l 0 l - l 0 l 0 l 0 l 0 l 0 l-l0 l0 l@l4 l1l1l1l1l@l l

l@

r a 9 uCENSEE CODE to IS LICENSE NUMUE*t 25 h

LICENSE TvPE Jo St C A T Sa con r 10I'I

$2nN l L hl 0 l 5 l 0 l 0 l 0 l 2 l 5 l 9 @l 0 l 4 [ 2 l2 l 8 l0 @l 0 l 5 l 21 1l 8 l 0 l@

i 8

Go 61 DOCKET NLNSER 68 69 EVENT DATE 74 75 AEPORT OATE 83 EVENT DESCRIPTION AND PROSABLE cCNSEQUENCES h I o 121 l During steady state conditions 1B recirculation MG set tripped during a transfer i

lol31 l from alternate to normal power source. Normal supply breaker did not close.

lo(41l Reference T.S.3.6.F.1.

This caused a power reduction for approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

l 1 lolsl l There was no danger to health or safety of public. No previous occurrences.

l 10161I i

10171 1 j

lo ta l I l

F 4 9 SYS1EM

CAUSE

CAUSE r rf.'P s a ty (

CODE COOF Sil Co.*vcNENT 200E SLitCODE SUIRC ODE I c ; B i g gg g'ICODEg lz l z'j zi zj zl zl g l z ; g g g lo101 F

d 9

to it il TJ 14 19

0 StoL'EN Te AL oCCUNHENCE HE rCftT REvtstoN i f R Ro E'/ENT YE A R RE'ORI No CODE TvPE No

@.7,',g;'l, la l0 l l-l l 01 al 6l l-l l 0l 3 l IL l g

10l

_v u

a v

o ao v

SLIB MAN FA T 58 E f t T

EP ACT O PLANT M T4 Ho'J R $

17 D F ne vt, St PPLI lXl@lzl@

lBl@

lzl@

l 0l 0] 0l 2l

{g l Nlg l zlg lz l9 l9 l9 I u

24 as 26 v

w ei o

u 44 4,

cAUSE DESCAIPTION AND CORRECTIVE ACTIONS W l Cause of failure to transfer is unknown. The normal supply breaker was inspected I

lilii ! and no trouble found.

S.I. 4.6.A.6&7 was run prior to restarting 1B MG set.

I ii i2; l On a subsequent startup the MG set transferred normally with no problems.

No 1

l 13l l recurrence control required.

l I s l41 1 I

F 8

'J M.'

ST is NPOWER OTHER5*ATUS i

f v D.SCoV EH*r DESCRIPTION y ] @ l0l2l2lgl N\\

l l A lgl operator observ.

l M li'/tTV COP TENT ATLE MED O' DEL E Ast AMOLINT o, AcilVITY LOC Af TON OF RE LE ASE I d i j L zJ @ l zJ @ l NA l

l NA j

i 9 9 10 11 44 43 e*

P(na.ryNyg( y xPr;syra[$

[, l, ; l 6[""0'l 0l@l Tlg['""dE" O' i

PE,. SON.E L imu',fiEs r3EsCnip ritsNh

n -.r e.

l3 j;ll0l0]0l@l NA j

i e I il 12 Pr.

L fr.*, or oM O AUAGE TO F ACILt 7 r '

fvet t iE SCite r TION I ztgl NA l

i o i.,

w.

t"AV E CHtPTION 12IofLIE8I NA l

lllllllllllll l

8 0'.052 9 0 Vf/

  • a 5'

l

..,e,..........

.. -, c

Tennessee Valley Authority Form DF-17 Browns Ferry Nuclear Plant BF 15.2 1/10/79 LER SUPPLEMENTAL INFORMATION BFRO 259 / 8036 Technical Specification Involved 3.6.F.1

~

Reported Under Technical Specification

6. 7. 2.b (2)

Date of Occurrence 4/22/80 Time of Occurrence 0602 Unit 1 Identification and Descrip_ tion'of Occurrence:

Recirculation MG set 1B tripped during a transfer from alternate to normal power source.

Conditions Prior to Occurrence:

Unit 1 @ 22%

Unit 2 @ 95%

~

Unit 3 @ 98%

Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment. Describe.

NA Apparent Cause of Occurrence:

The cause of failure to transfer is unknown.

Analysis of Occurrence:

There was no damage to plant equipment. There was no activity release, no personnel exposure or injury and no danger to the health or safety of the public.

s

Corrective Action

The normal supply breaker was inspected and no problem found.

S.I.4.6.A.6&7 i

was run prior to restarting the 1B MG set.

On a subsequent startup the MG set supply breakers transferred normally with no problems.

Fuilure Data:

NA

  • Reten tion :

Period - Lifetime; Responsibility - Administrative Supervisor

  • Revision:

[

O