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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046C0661993-07-30030 July 1993 LER 92-009-01:on 920910,deficiencies Discovered During Dynamic Testing of Motor Operated Valves in Response to Generic Ltr 89-10.MOVs W/Deficiencies Modified or Repaired. W/930730 Ltr ML20046B6011993-07-26026 July 1993 LER 93-004-00:on 930428,plant Entered Mode 2 W/Afw Pump Turbine Main Steam Line Crossover Check Valve MS735 in Open Position.Caused by Inappropriate Use of Engineering Judgement.Valve MS735 closed.W/930726 Ltr ML20045D2451993-06-17017 June 1993 LER 93-003-00:on 930520,plant Experienced Trip from Approx & Continuity Between Fuse & Fuseholder Lost,Resulting in Loss of Selected RCS Average Temp Input to Ics.Faulty Fuse Cap & Fuse replaced.W/930617 Ltr ML20044B1681990-07-10010 July 1990 LER 90-002-01:on 900126,reactor Coolant Pump Current Monitor Inputs to Sfrcs ACH1 & Reactor Pressure Sys Channel 1 Experienced Reactor Trip.Probably Caused by Inadequate Test Switches & Isolation plug.W/900710 Ltr ML20043H3201990-06-18018 June 1990 LER 90-010-00:on 900518,station Experienced Inadvertent Safety Features Actuation Signal Level 1-4 Actuation W/Injection of 1,000 Gallons of Borated Water.Caused by Loss of 120-volt Ac Bus Y3.W/900618 Ltr ML20043B5711990-05-25025 May 1990 LER 90-008-00:on 900425,safety Features Actuation Sys Level 1 Actuation Occurred,Resulting in Trip of Containment Radiation Monitors.Caused by High Radiation Fields While Lifting Core Support Assembly.Mod initiated.W/900525 Ltr ML20043B8051990-05-25025 May 1990 LER 90-009-00:on 900426,source-check of Station Vent Radiation Monitors Not Performed Per Tech Spec 3.3.3.10. Caused by Use of Outmoded Light Emitting Dioide as Check Source.Source Check Procedures revised.W/900525 Ltr ML20042F2811990-05-0303 May 1990 LER 90-007-00:on 900403,inadvertent,inconsequential Safety Features Actuation Signal Occured While Defueled.Caused by Incidental Contact W/Monitor in Containment.Temporary Barriers Built Around monitors.W/900503 Ltr ML20042F2791990-05-0303 May 1990 LER 90-006-00:on 900403,station Experienced Safety Features Actuation Sys Levels 1 Through 5 Actuation.Caused by Contact W/Breaker Switch HAAE2 in High Voltage Switchgear Room 2. Meetings Held W/Craft personnel.W/900503 Ltr ML20042E4891990-04-16016 April 1990 LER 90-005-00:on 900314,determined That Some Class 1E Circuits That Pass Through Containment Electrical Penetrations Do Not Have Adequate Backup Fault Protection. Caused by Inadequate Design control.W/900416 Ltr ML20012D0341990-03-19019 March 1990 LER 90-004-00:on 900217,fuel Assembly Moved in Spent Fuel Pool While Emergency Ventilation Inoperable.Caused by Personnel Error.Personnel Involved Counseled & Subj LER Part of Required reading.W/900319 Ltr ML20012C7151990-03-14014 March 1990 LER 90-003-00:on 900212,station Entered Mode 6,refueling,w/o Operable Audible Source Range Indication.Caused by Personnel Error.Individual counseled.W/900314 Ltr ML20012B4851990-03-0606 March 1990 LER 83-039/03X-2:on 830726,discovered That Handwheel for Inner Door of Personnel Airlock in Shut Position & Partially Opened.Caused by Excessive Use of Door During Outages.Door Repaired & Returned to Operable status.W/900306 Ltr ML20011F3831990-02-26026 February 1990 LER 90-002-00:on 900126,reactor Tripped from 73% Power. Caused by Spurious Reactor Coolant Pump Monitor Signal Indicating Only One Pump Running in Each Loop.Pump Seal to Be Replaced During Sixth Refueling outage.W/900226 Ltr ML20006E6861990-02-20020 February 1990 LER 90-001-00:on 900118,reactor Protection Sys Channel 2 Bypassed Temporarily During Performance of DB-MI-03207. Caused by Inadequate Procedure Re Inoperable Channel Removal.Procedure SP1105.02 revised.W/900220 Ltr ML20011E2251990-01-30030 January 1990 LER 86-032-01:on 860802,inadvertent Start of High Pressure Injection Pump 1-2 Occurred.Caused by Open Relay Coil. Failed Relay Replaced & Procedure Change Initiated. W/900130 Ltr ML20005G1091990-01-0909 January 1990 LER 89-015-01:on 891026,concluded That Transmitter Was Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status on 890924.Caused by leak-by in Instrument Manifold.Transmitter Recalibr successfully.W/900109 Ltr ML20042D4011990-01-0202 January 1990 LER 89-010-01:on 890612,control Room Ventilation Sys Declared Inoperable Due to Compressor High Pressure Trips. Caused by Tripping of Refrigerant Pressure Switch on High Pressure.Switch Reset & Sys retested.W/900102 Ltr ML19354D7361989-12-22022 December 1989 LER 89-018-00:on 891123,hydrogen Dilution Blower 1-1 Casing Drain Line Broke Off at Casing,Declaring Blower Inoperable. Caused by Drain Line Being Accidentally Stepped On.Drain Removed & Pipe Plug installed.W/891222 Ltr ML19332F8951989-12-13013 December 1989 LER 89-017-00:on 891113,containment Spray Pump 1-1 Inadvertently Started During Monthly Functional Test in Safety Features Actuation Sys (Sfas) Channel 1.Caused by Failed Relay in Sfas Channel 3.Relay replaced.W/891213 Ltr ML19332E7521989-12-0404 December 1989 LER 89-016-00:on 890917,unplanned Release of Radioactive Resin to Onsite Settling Basin Occurred.Caused by Personnel Error.Standing Order 89-051 Generated on 890920 to Direct Use of Working Copy of procedures.W/891204 Ltr ML19332D3111989-11-27027 November 1989 LER 89-015-00:on 890924,RCS Flow Transmitter Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status.Caused by leak-by in Instrument Manifold Seen as Zero Shift.Transmitter recalibr.W/891127 Ltr ML19324C2081989-11-10010 November 1989 LER 89-014-00:on 891011,plastic Sheeting Blocked Off Fire Detectors in Auxiliary Feedwater Pump 1-1 Room & High Voltage Switchgear Room B,Making Fire Detectors Inoperable. Caused by Personnel Oversight.Event reviewed.W/891110 Ltr ML19325D4671989-10-16016 October 1989 LER 89-004-01:on 890411,determined That Circulating Water Line Break Would Result in Loss of Svc Water as Result of Concerns Raised on 890206.Cause Unknown.Standing Order 89-026 in Place to Plug Floor drains.W/891016 Ltr ML19325C8531989-10-13013 October 1989 LER 89-013-00:on 890913,hourly Fire Watch Patrol Exceeded Allowed Interval,Violating Tech Spec 3.7.10,Action a.2. Caused by Personnel Error.Individual Counseled & Event Info Distributed to Fire Watch personnel.W/891013 Ltr ML20024E2591983-08-0101 August 1983 LER 83-033/03L-0:on 830620,fire Detection Zone Reactor Coolant Pump 1-2,containment Level 603 Ft Alarmed & Could Not Be Reset.Caused by Faulty Detector String.Zone Will Be Restored During Next Refueling outage.W/830801 Ltr ML20024B8351983-07-0101 July 1983 LER 83-028/03L-0:on 830603 & 17,fuel Handling Area Radiation Monitors RE8446 & 7 Found Deenergized.Caused by Blown Radiation Monitoring Cabinet Fuse.Fuse replaced.W/830701 Ltr ML20024B0471983-06-21021 June 1983 LER 83-026/03L-0:on 830524,one Half Channel Trip in Steam & Feedwater Rupture Control Sys (Sfrcs) Channel 2 Received. Caused by Component Failure.Input Buffer replaced.W/830621 Ltr ML20024A3621983-06-0909 June 1983 LER 83-024/03L-0:on 830511,while Starting Up from 830510 Reactor Trip,Quadrant Power Tilt in Quadrant Yz Exceeded Tech Spec steady-state Limit.Caused by Inherent Design of B&W NSSS & Negative Moderator Temp coefficient.W/830609 Ltr ML20024A5341983-06-0808 June 1983 LER 83-023/03L-0:on 830510,120-volt Ac Essential Bus Y4 Lost,Resulting in Deenergizing Reactor Protection & Safety Features Actuation Sys Channel 4.Caused by Blown Fuse in Inverter YV4.Power Restored to bus.W/830608 Ltr ML20024A5481983-06-0707 June 1983 Revised LER 83-002/03X-2:on 830115,18,0409,10 & 0510,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Slight Fission Product Leakage Through Fuel Cladding.Level of I-131 monitored.W/830607 Ltr ML20023D9051983-05-26026 May 1983 LER 83-027/03L-0:on 830428,valve RC240B Would Not Close W/O Repeated Signals from Control Room.Caused by Valve Operator Torquing Out Due to Dirty & Improperly Lubricated Stem.Stem Cleaned & Torque Switch reset.W/830526 Ltr ML20023C3241983-05-0505 May 1983 LER 83-016/03L-0:on 830407,determined That Amplifier of Startup Level Transmitter LT-SP9A3 for Steam Generator 1-2 Failed.Caused by Component Failure within Amplifier. Amplifier Replaced ML20023C3021983-05-0505 May 1983 Revised LER 83-002/03X-1:on 830115,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit of 1.0 Uci/Gm.Caused by Leakage of Fission Products Through Fuel cladding.I-131 Monitored Until Level Dropped ML20028E9581983-01-19019 January 1983 LER 82-068/03L-0:on 821220,core Imbalance Vs Core Power Limit Computer Alarm C963 Inoperable.Caused by Mistake in Alarm Subroutine.Alarm Statement Corrected So Limits & Value for Imbalance Scaled Same ML20028D2291983-01-0707 January 1983 Revised LER 81-045/03X-1:on 810730,after Unit Trip,Three Action Statements Entered.Auxiliary Feedwater Pump 1-2 Did Not Operate Properly.Shield Bldg Integrity Lost When Panel Blown Out.Main Steam Safety Valve Lifted at Low Setpoint ML20028C1231983-01-0303 January 1983 LER 82-064/03L-0:on 821129,decay Heat Cooler Component Cooling Water Outlet Valve on CCW Train 1 Would Not Open. Caused by Mfg Error.Flanged Bearing Missing from Actuator Mounting Plate.Flanged Bearing Installed on 821215 ML20028C3111982-12-30030 December 1982 Revised LER 81-031/03X-6:on 810512,following Reactor Trip, RCS Sample Level Peaked Above Microcurie Limit.Other Iodine Spikes Occurred 810730,0902,1016 & 23 & 1228.Caused by Slight Leakage of Fission Products Through Fuel Cladding ML20028C1971982-12-30030 December 1982 Revised LER 82-045/03X-1:on 820904 & 1203,auxiliary Feedwater Pump 1-1 Suction Valve FW786 Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown.Valve FW786 Reopened Upon Discovery ML20028C2591982-12-30030 December 1982 LER 82-065/03L-0:on 821201,discovered That Control Room Not Placed in Recirculation Mode within 1 H of Ventilation Sys Chlorine Detector Being Taken Out of Svc.On 821203,chlorine Detector Failed.Caused by Personnel Error ML20028B0291982-11-19019 November 1982 LER 82-054/03L-0:on 821021,Door 107 to Radiation Equipment Found Partially Open & Blocked by Hose When Personnel Attempted to Perform Routine Flush on RE-1878.Caused by Personnel Error.Personnel Counseled ML20028B2281982-11-16016 November 1982 LER 82-053/03L-0:on 821018,half Trip Alarm on Steam & Feedwater Rupture Control Sys Channel 2 Received Due to Failure of Steam Generator Level Instrument Cabinet Channel 2,24-volt Dc Power Supply.Caused by Component Failure ML20027E7891982-11-0404 November 1982 Revised LER 82-052/03X-1:on 820928,reactor Quadrant Power Tilt in Wx Quadrant Exceeded Tech Specs.Caused by Xenon Oscillation Producing Large Negative Imbalance.Control Rod Group 7 Borated Out to Reduce Negative Imbalance ML20027C9551982-10-19019 October 1982 LER 82-049/03L-0:on 820920 & 22,Channels 2 & 3 on Containment post-accident Radiation Monitor Re 4597BA Were Reading High.Caused by Problem in Microprocessor Software. New Set of Software Installed & Faulty Actuator Replaced ML20027C5381982-10-0404 October 1982 LER 82-045/03L-0:on 820904,auxiliary Feedwater Pump 1-1, Suction Valve FW786 Observed Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown. Valve Reopened ML20027A9471982-09-0707 September 1982 LER 82-036/03L-0:on 820808,hole Discovered in Fire Barrier Wall Above Door 309.Caused by Snubber EBD125R43 Penetrating Wall Through Pipe Shell.Hole Left by Workers After Work on Snubbers.Fire Watch Established & Hole Filled ML20052G6651982-05-0707 May 1982 LER 82-020/03L-0:on 820409,while in Mode 6,station Experienced Loss of 120-volt Ac Distribution Panel Y2.Caused by Blown YV2 Inverter Fuse When Short to Ground Occurred During Maint on Control Room Emergency Ventilation Sys ML20052E6231982-04-30030 April 1982 LER 82-019/01T-0:on 820426,some Steam Generator Tubes Adjacent to Auxiliary Feedwater Header Showed Potential Interaction W/Header Support Sys.Header Found Insecurely Fastened & Damaged.Cause & Corrections Being Investigated ML20052E8761982-04-29029 April 1982 LER 82-016/03X-1:on 820312,door 108 Found W/Both Door Closure Mechanisms Broken.Caused by Improper Operation of Door Closure Mechanisms by Personnel.Mechanisms Temporarily Repaired & New Parts Ordered ML20052C4151982-04-23023 April 1982 LER 82-018/03L-0:on 820326,electrician Cut High Voltage Cable on Source Range Detector NI-2,while Working in Containment Penetration Box P1L1L1.Caused by Problem in Coordination of Work Performed.Cut Cable Reconnected 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046C0661993-07-30030 July 1993 LER 92-009-01:on 920910,deficiencies Discovered During Dynamic Testing of Motor Operated Valves in Response to Generic Ltr 89-10.MOVs W/Deficiencies Modified or Repaired. W/930730 Ltr ML20046B6011993-07-26026 July 1993 LER 93-004-00:on 930428,plant Entered Mode 2 W/Afw Pump Turbine Main Steam Line Crossover Check Valve MS735 in Open Position.Caused by Inappropriate Use of Engineering Judgement.Valve MS735 closed.W/930726 Ltr ML20045D2451993-06-17017 June 1993 LER 93-003-00:on 930520,plant Experienced Trip from Approx & Continuity Between Fuse & Fuseholder Lost,Resulting in Loss of Selected RCS Average Temp Input to Ics.Faulty Fuse Cap & Fuse replaced.W/930617 Ltr ML20044B1681990-07-10010 July 1990 LER 90-002-01:on 900126,reactor Coolant Pump Current Monitor Inputs to Sfrcs ACH1 & Reactor Pressure Sys Channel 1 Experienced Reactor Trip.Probably Caused by Inadequate Test Switches & Isolation plug.W/900710 Ltr ML20043H3201990-06-18018 June 1990 LER 90-010-00:on 900518,station Experienced Inadvertent Safety Features Actuation Signal Level 1-4 Actuation W/Injection of 1,000 Gallons of Borated Water.Caused by Loss of 120-volt Ac Bus Y3.W/900618 Ltr ML20043B5711990-05-25025 May 1990 LER 90-008-00:on 900425,safety Features Actuation Sys Level 1 Actuation Occurred,Resulting in Trip of Containment Radiation Monitors.Caused by High Radiation Fields While Lifting Core Support Assembly.Mod initiated.W/900525 Ltr ML20043B8051990-05-25025 May 1990 LER 90-009-00:on 900426,source-check of Station Vent Radiation Monitors Not Performed Per Tech Spec 3.3.3.10. Caused by Use of Outmoded Light Emitting Dioide as Check Source.Source Check Procedures revised.W/900525 Ltr ML20042F2811990-05-0303 May 1990 LER 90-007-00:on 900403,inadvertent,inconsequential Safety Features Actuation Signal Occured While Defueled.Caused by Incidental Contact W/Monitor in Containment.Temporary Barriers Built Around monitors.W/900503 Ltr ML20042F2791990-05-0303 May 1990 LER 90-006-00:on 900403,station Experienced Safety Features Actuation Sys Levels 1 Through 5 Actuation.Caused by Contact W/Breaker Switch HAAE2 in High Voltage Switchgear Room 2. Meetings Held W/Craft personnel.W/900503 Ltr ML20042E4891990-04-16016 April 1990 LER 90-005-00:on 900314,determined That Some Class 1E Circuits That Pass Through Containment Electrical Penetrations Do Not Have Adequate Backup Fault Protection. Caused by Inadequate Design control.W/900416 Ltr ML20012D0341990-03-19019 March 1990 LER 90-004-00:on 900217,fuel Assembly Moved in Spent Fuel Pool While Emergency Ventilation Inoperable.Caused by Personnel Error.Personnel Involved Counseled & Subj LER Part of Required reading.W/900319 Ltr ML20012C7151990-03-14014 March 1990 LER 90-003-00:on 900212,station Entered Mode 6,refueling,w/o Operable Audible Source Range Indication.Caused by Personnel Error.Individual counseled.W/900314 Ltr ML20012B4851990-03-0606 March 1990 LER 83-039/03X-2:on 830726,discovered That Handwheel for Inner Door of Personnel Airlock in Shut Position & Partially Opened.Caused by Excessive Use of Door During Outages.Door Repaired & Returned to Operable status.W/900306 Ltr ML20011F3831990-02-26026 February 1990 LER 90-002-00:on 900126,reactor Tripped from 73% Power. Caused by Spurious Reactor Coolant Pump Monitor Signal Indicating Only One Pump Running in Each Loop.Pump Seal to Be Replaced During Sixth Refueling outage.W/900226 Ltr ML20006E6861990-02-20020 February 1990 LER 90-001-00:on 900118,reactor Protection Sys Channel 2 Bypassed Temporarily During Performance of DB-MI-03207. Caused by Inadequate Procedure Re Inoperable Channel Removal.Procedure SP1105.02 revised.W/900220 Ltr ML20011E2251990-01-30030 January 1990 LER 86-032-01:on 860802,inadvertent Start of High Pressure Injection Pump 1-2 Occurred.Caused by Open Relay Coil. Failed Relay Replaced & Procedure Change Initiated. W/900130 Ltr ML20005G1091990-01-0909 January 1990 LER 89-015-01:on 891026,concluded That Transmitter Was Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status on 890924.Caused by leak-by in Instrument Manifold.Transmitter Recalibr successfully.W/900109 Ltr ML20042D4011990-01-0202 January 1990 LER 89-010-01:on 890612,control Room Ventilation Sys Declared Inoperable Due to Compressor High Pressure Trips. Caused by Tripping of Refrigerant Pressure Switch on High Pressure.Switch Reset & Sys retested.W/900102 Ltr ML19354D7361989-12-22022 December 1989 LER 89-018-00:on 891123,hydrogen Dilution Blower 1-1 Casing Drain Line Broke Off at Casing,Declaring Blower Inoperable. Caused by Drain Line Being Accidentally Stepped On.Drain Removed & Pipe Plug installed.W/891222 Ltr ML19332F8951989-12-13013 December 1989 LER 89-017-00:on 891113,containment Spray Pump 1-1 Inadvertently Started During Monthly Functional Test in Safety Features Actuation Sys (Sfas) Channel 1.Caused by Failed Relay in Sfas Channel 3.Relay replaced.W/891213 Ltr ML19332E7521989-12-0404 December 1989 LER 89-016-00:on 890917,unplanned Release of Radioactive Resin to Onsite Settling Basin Occurred.Caused by Personnel Error.Standing Order 89-051 Generated on 890920 to Direct Use of Working Copy of procedures.W/891204 Ltr ML19332D3111989-11-27027 November 1989 LER 89-015-00:on 890924,RCS Flow Transmitter Out of Tolerance When Reactor Protection Sys Channel 2 Returned to Operable Status.Caused by leak-by in Instrument Manifold Seen as Zero Shift.Transmitter recalibr.W/891127 Ltr ML19324C2081989-11-10010 November 1989 LER 89-014-00:on 891011,plastic Sheeting Blocked Off Fire Detectors in Auxiliary Feedwater Pump 1-1 Room & High Voltage Switchgear Room B,Making Fire Detectors Inoperable. Caused by Personnel Oversight.Event reviewed.W/891110 Ltr ML19325D4671989-10-16016 October 1989 LER 89-004-01:on 890411,determined That Circulating Water Line Break Would Result in Loss of Svc Water as Result of Concerns Raised on 890206.Cause Unknown.Standing Order 89-026 in Place to Plug Floor drains.W/891016 Ltr ML19325C8531989-10-13013 October 1989 LER 89-013-00:on 890913,hourly Fire Watch Patrol Exceeded Allowed Interval,Violating Tech Spec 3.7.10,Action a.2. Caused by Personnel Error.Individual Counseled & Event Info Distributed to Fire Watch personnel.W/891013 Ltr ML20024E2591983-08-0101 August 1983 LER 83-033/03L-0:on 830620,fire Detection Zone Reactor Coolant Pump 1-2,containment Level 603 Ft Alarmed & Could Not Be Reset.Caused by Faulty Detector String.Zone Will Be Restored During Next Refueling outage.W/830801 Ltr ML20024B8351983-07-0101 July 1983 LER 83-028/03L-0:on 830603 & 17,fuel Handling Area Radiation Monitors RE8446 & 7 Found Deenergized.Caused by Blown Radiation Monitoring Cabinet Fuse.Fuse replaced.W/830701 Ltr ML20024B0471983-06-21021 June 1983 LER 83-026/03L-0:on 830524,one Half Channel Trip in Steam & Feedwater Rupture Control Sys (Sfrcs) Channel 2 Received. Caused by Component Failure.Input Buffer replaced.W/830621 Ltr ML20024A3621983-06-0909 June 1983 LER 83-024/03L-0:on 830511,while Starting Up from 830510 Reactor Trip,Quadrant Power Tilt in Quadrant Yz Exceeded Tech Spec steady-state Limit.Caused by Inherent Design of B&W NSSS & Negative Moderator Temp coefficient.W/830609 Ltr ML20024A5341983-06-0808 June 1983 LER 83-023/03L-0:on 830510,120-volt Ac Essential Bus Y4 Lost,Resulting in Deenergizing Reactor Protection & Safety Features Actuation Sys Channel 4.Caused by Blown Fuse in Inverter YV4.Power Restored to bus.W/830608 Ltr ML20024A5481983-06-0707 June 1983 Revised LER 83-002/03X-2:on 830115,18,0409,10 & 0510,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Slight Fission Product Leakage Through Fuel Cladding.Level of I-131 monitored.W/830607 Ltr ML20023D9051983-05-26026 May 1983 LER 83-027/03L-0:on 830428,valve RC240B Would Not Close W/O Repeated Signals from Control Room.Caused by Valve Operator Torquing Out Due to Dirty & Improperly Lubricated Stem.Stem Cleaned & Torque Switch reset.W/830526 Ltr ML20023C3241983-05-0505 May 1983 LER 83-016/03L-0:on 830407,determined That Amplifier of Startup Level Transmitter LT-SP9A3 for Steam Generator 1-2 Failed.Caused by Component Failure within Amplifier. Amplifier Replaced ML20023C3021983-05-0505 May 1983 Revised LER 83-002/03X-1:on 830115,RCS Dose Equivalent I-131 Exceeded Tech Spec Limit of 1.0 Uci/Gm.Caused by Leakage of Fission Products Through Fuel cladding.I-131 Monitored Until Level Dropped ML20028E9581983-01-19019 January 1983 LER 82-068/03L-0:on 821220,core Imbalance Vs Core Power Limit Computer Alarm C963 Inoperable.Caused by Mistake in Alarm Subroutine.Alarm Statement Corrected So Limits & Value for Imbalance Scaled Same ML20028D2291983-01-0707 January 1983 Revised LER 81-045/03X-1:on 810730,after Unit Trip,Three Action Statements Entered.Auxiliary Feedwater Pump 1-2 Did Not Operate Properly.Shield Bldg Integrity Lost When Panel Blown Out.Main Steam Safety Valve Lifted at Low Setpoint ML20028C1231983-01-0303 January 1983 LER 82-064/03L-0:on 821129,decay Heat Cooler Component Cooling Water Outlet Valve on CCW Train 1 Would Not Open. Caused by Mfg Error.Flanged Bearing Missing from Actuator Mounting Plate.Flanged Bearing Installed on 821215 ML20028C3111982-12-30030 December 1982 Revised LER 81-031/03X-6:on 810512,following Reactor Trip, RCS Sample Level Peaked Above Microcurie Limit.Other Iodine Spikes Occurred 810730,0902,1016 & 23 & 1228.Caused by Slight Leakage of Fission Products Through Fuel Cladding ML20028C1971982-12-30030 December 1982 Revised LER 82-045/03X-1:on 820904 & 1203,auxiliary Feedwater Pump 1-1 Suction Valve FW786 Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown.Valve FW786 Reopened Upon Discovery ML20028C2591982-12-30030 December 1982 LER 82-065/03L-0:on 821201,discovered That Control Room Not Placed in Recirculation Mode within 1 H of Ventilation Sys Chlorine Detector Being Taken Out of Svc.On 821203,chlorine Detector Failed.Caused by Personnel Error ML20028B0291982-11-19019 November 1982 LER 82-054/03L-0:on 821021,Door 107 to Radiation Equipment Found Partially Open & Blocked by Hose When Personnel Attempted to Perform Routine Flush on RE-1878.Caused by Personnel Error.Personnel Counseled ML20028B2281982-11-16016 November 1982 LER 82-053/03L-0:on 821018,half Trip Alarm on Steam & Feedwater Rupture Control Sys Channel 2 Received Due to Failure of Steam Generator Level Instrument Cabinet Channel 2,24-volt Dc Power Supply.Caused by Component Failure ML20027E7891982-11-0404 November 1982 Revised LER 82-052/03X-1:on 820928,reactor Quadrant Power Tilt in Wx Quadrant Exceeded Tech Specs.Caused by Xenon Oscillation Producing Large Negative Imbalance.Control Rod Group 7 Borated Out to Reduce Negative Imbalance ML20027C9551982-10-19019 October 1982 LER 82-049/03L-0:on 820920 & 22,Channels 2 & 3 on Containment post-accident Radiation Monitor Re 4597BA Were Reading High.Caused by Problem in Microprocessor Software. New Set of Software Installed & Faulty Actuator Replaced ML20027C5381982-10-0404 October 1982 LER 82-045/03L-0:on 820904,auxiliary Feedwater Pump 1-1, Suction Valve FW786 Observed Closed for No Apparent Reason W/O Operator Touching Close Button.Cause Unknown. Valve Reopened ML20027A9471982-09-0707 September 1982 LER 82-036/03L-0:on 820808,hole Discovered in Fire Barrier Wall Above Door 309.Caused by Snubber EBD125R43 Penetrating Wall Through Pipe Shell.Hole Left by Workers After Work on Snubbers.Fire Watch Established & Hole Filled ML20052G6651982-05-0707 May 1982 LER 82-020/03L-0:on 820409,while in Mode 6,station Experienced Loss of 120-volt Ac Distribution Panel Y2.Caused by Blown YV2 Inverter Fuse When Short to Ground Occurred During Maint on Control Room Emergency Ventilation Sys ML20052E6231982-04-30030 April 1982 LER 82-019/01T-0:on 820426,some Steam Generator Tubes Adjacent to Auxiliary Feedwater Header Showed Potential Interaction W/Header Support Sys.Header Found Insecurely Fastened & Damaged.Cause & Corrections Being Investigated ML20052E8761982-04-29029 April 1982 LER 82-016/03X-1:on 820312,door 108 Found W/Both Door Closure Mechanisms Broken.Caused by Improper Operation of Door Closure Mechanisms by Personnel.Mechanisms Temporarily Repaired & New Parts Ordered ML20052C4151982-04-23023 April 1982 LER 82-018/03L-0:on 820326,electrician Cut High Voltage Cable on Source Range Detector NI-2,while Working in Containment Penetration Box P1L1L1.Caused by Problem in Coordination of Work Performed.Cut Cable Reconnected 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & Pnpp QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML20249A4121998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20196B5221998-05-23023 May 1998 10CFR50.59 Summary Rept of Facility Changes,Tests & Experiments Dbnps,Unit 1 for 960602-980523 ML20236E7581998-05-19019 May 1998 Rev 0 to Davis-Besse Unit 1 Cycle 12 Colr ML20236N7501998-04-30030 April 1998 Rev 2 to Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit ML20247F6721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Davis-Bess Nuclear Power Station,Unit 1 ML20249A4141998-04-30030 April 1998 Revised Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20217P8041998-04-0707 April 1998 11RFO OTSG ECT Insp Scope ML20216B4041998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216C5131998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20202D3721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20199G6321998-01-26026 January 1998 Rev 1 to Davis-Besse Unit 1,Cycle 11,COLR ML20198R4771998-01-13013 January 1998 SER Approving Second 10-year Interval Inservice Inspection Program Plan Requests for Relief for Davis-Besse Nuclear Power Station,Unit 1 ML20198K7931997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20217K6401997-12-31031 December 1997 1997 Annual Rept First Energy ML20203A3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Davis-Besse Nuclear Power Plant,Unit 1 ML20198S5371997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Davis-Besse Nuclear Power Station ML20217H7701997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20216H3261997-08-31031 August 1997 Monthly Operating Rept for August 1997 for DBNPS ML20217K0241997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Davis Besse Nuclear Power Station,Unit 1 1999-09-30
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LICENSEE EVENT REPORT CONTROL BLOCK: l 1
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(PLEASE PHINT OR TYPE ALL REQUIRED INFORMATION) 0 t 8 9 l 0 l HLICENSEE l D l CODE B l S l 114 l@l15 0 l 0 l - l 0 lLICENSE P l 1:' l - l d ! 'I25 hl 26 0 l N lNuveEn 4 l 1LICENSEl 1 l 1TYPE l 140@l57 l CAI b3 lh OON'T 0 1 8
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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 l At 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on 1/3/79, High Pressure Injection (HPI) Pump 1-1 was started per "Emer-j O 3 l gency Core Cooling System Subsystem Monthly Test", ST 5051.01. At 1406 hours0.0163 days <br />0.391 hours <br />0.00232 weeks <br />5.34983e-4 months <br />, HPI l o 4 i Pump 1-1 was stopped due to a low recirculation flow indication. This placed the unitj O 5 l in violation of T.S. 3.5.2 which requires that two independent Emergency Core Cooling l 0 6 i System subsystems be operable. There was no dange to the public or station personnel.l I
60 7 A safety evaluation determined the HPT m nn n ct voitld have oerformed their intended safet?
I 20 8 I function for any actual Reactor Coolant System leak that the HPI oumos are reauired. I D CODE SLBCO E COMPONENT CODE SUBC DE SU E O 9 8
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43 44 Bl0l1',0lh 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O l This incident was caused by the inability of the heat trace to maintain the HPI pump l i i l recirculation line temperature above freezing. The thermostat settine for the HPI I i 2 l pump recirculation line heat trace was increased and a temporary heated enclosure was l i a built around it. At 1105 hours0.0128 days <br />0.307 hours <br />0.00183 weeks <br />4.204525e-4 months <br /> on 1/5/79, ST 5051.01 was successfully completed and i i 4 l the unit was no longer in violation of Technical Specification 3.5.2. l 8 9 80 ST S % POWER oTHER STATUS Dis O RY DISCOVERY DESCRIPTION 1 5 [ E,jh l 0 l 8 l 6 lhl NA l l B lhl Surveillance Test ST 5051.01 l ACTIVITY CONTENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELE ASE 1 6 8 9 lZlh 10
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PERSONNE L EXPOSURES NUVBER DESCRIPTION 1 7 l 0l 0l 0lhlTYPEZlhl "
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- P E e S_ et' ,- v'"'e s NuveEn DESCniPTiONh 2232 156 i a 8 9 1010 Ol@l 11 12 NA 80 l
LOSS OF OR D AV AGE TO F ACILITY TYPE DESCHiPTION 1 9 (_Z_jhl NA 8 9 10 80 DESCR1PTION e 2 o p;5UjEL 81 .., 79060702rt i 68 69 i i i i i i i i ii l 8 3 to 80 5 VR 79-048 NAME OF PREPARER David H. Brown PHONE:
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-32-79-03 DATE OF EVENT: January 3, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE:
Inoperability of High Pressure Injection Pumps 1-1 >
and 1-2 due to minimum recirculation line freezing The unit was in Mode 1, with Power (MWT) = 2384, Conditions Prior to Occurrence:
and Load (Gross MWE) = 763.
Description of Occurrence:
At 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br /> on January 3,1979, High Pressure Injection (HPI) Pump 1-1 was started per " Emergency Core Cooling System Subsystem Monthly Tes ST 5051.01. At 1406 hours0.0163 days <br />0.391 hours <br />0.00232 weeks <br />5.34983e-4 months <br />, HPI Pump 1-1 was stopped due to a low flow indication on the HPI pump to the Borated Water Storage Tank (BUST) minimum recirculation line (3" HCC-91) . Further investigation discovered that this line Maintenance had frozen outside somewhere personnel were between the BWST Pipe Tunnel and the top of the BWST.
hmuediately notified.
Maintenance personnel increased the thermostat setting for the HPI pump minimum re-circulation line heat trace and built a temporary heated enclosure around the exposed line. The recirculation line was thawed and ST 5051.01 was successfully completed for HPI Pump 1-1 at 1105 hours0.0128 days <br />0.307 hours <br />0.00183 weeks <br />4.204525e-4 months <br /> on January 5,1979.
At the time of the incident, an analysis of the frozen recirculation line by the station indicated that the minimum flow rate required for pump cooling would flow through the injection line if the HPI pumps were started during a loss of coolant As a result, both HPI Pump 1-1 and HPI Pump 1-2 were considered operable, accident.
and the unit was not in violation of any Technical Specifications.
On March 12, 1979, in a discussion between station personnel and TECo Power Engineer-they had donc an analysis of a ing personnel, Power Engineering personnel stated that (see Licensee Event Report NP-32-77-16 dated September previous HPI initiation event the minimum required HPI flow may not have existed if 24, 1977) which indicates that As a result of this initial analysis, both HPI the recirculation line was plugged.
2l pumps must now be considered to have been inoperable between 1406 hours0.0163 days <br />0.391 hours <br />0.00232 weeks <br />5.34983e-4 months <br /> on January 3 1979 and 1105 hours0.0128 days <br />0.307 hours <br />0.00183 weeks <br />4.204525e-4 months <br /> on January 5,1979.
In April 1979, a detailed safety evaluation was performed which determined the HPI pumps would have performed their intended saf ety function and thewould not have HPI pumps been are re-2 damaged for any actual Reactor Coolant System (RCS) leak that quired. See the attached safety evaluation for details.
in violation of Technical Specifi-The inoperability of the HPI pumps two placed the unitEmergency Core Cooling System sub-independent cation 3.5.2 which requires that I pump, systems shall be operable with each subsystem comprised of one operable HP, one operable Low Pressure Injection Pump, one operable Decay Heat Cooler, and one operable flowpath capable of taking suction from the BWST.
'"" #7'- ' 22L32 157
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-32-79-03 PAGE 2 Designation of Apparent Cause of Occurrence: This incident was caused by the inabi-lity of the heat trace on the HPI pump to BWST minimum recirculation line, 3" HCC-91, to maintain a pipe temperature above freezing. As a result, this line froze during sub-zero weather and rendered the HPI pumps inoperable.
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. No event requiring the actuation of the HPI pumps occurred.
The HPI pumps would have performed their intended safety function and would not have 2 been damaged for any actual RCS leak for which the HPI pumps are required. See the attached safety evaluation for details.
Corrective Action: Maintenance personnel increased the thermostat setting for the HPI pump to BWST minimum recirculation line heat trace and built a temporary heated enclosure around it. The recirculation line was thawed and ST 5051.01 was success-fully completed for HPI Pump 1-1 at 1105 hours0.0128 days <br />0.307 hours <br />0.00183 weeks <br />4.204525e-4 months <br /> on January 5,1979.
Facility Change Request 79-168 has been written to request a design change for the recirculation line heat trace to prevent recurrence.
Failure Data: There have not been any previous reportable occurrences with the HPI pumps recirculation line.
LER #79-014 '
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ATTACHMENT 1 TO LICENSEE EVENT REPORT NP-32-79-03 SAFETY EVALUATION FOR AN INOPERABLE HPI RECIRCULATION LINE 1.0 Reactor Coolant System pressure at time of HPI start The HPI pumps are automatically started at a RCS hot leg pressure setpoint of 1650 + 25 psig. Maximum instrument string inaccuracy including setpoint drift is 50.75 psig. Therefore, the HPI pumps may be started at a hot ]jgt pressure range from 1575 to 1725 psig.
Since the HPI pumps discharge into the cold legs of the RCS, the core pressure drop and the static pressure due to the dif ference in elevation of hot legs and cold legs must be considered. The core pressure drop with all four Reactor Coolant Pumps running (worst case) is approximately 100 psig and the static pressure due to difference in elevation amounts to approximately 20 psig.
Accounting for the above correction, the cold leg pressure range within which SFAS will actuate the HPI pumps is 1695 to ' *45 psig. ;
2.0 Reactor Coolant System depressurization rate after HPI start To aid in this analysis, data from the September 24, 1977 depressurization transient was analyzed. This data reprasents a very small break in the RCS piping caused by the pressurizer electromatic relief valve being stuck open, and is a conservative representation of a small RCS-break leading to HPI initi-2 ation with a very low depressurization rate. The rate of depressurization was approximately 3.4 psi per second.
3.0 Time until minimum flow into Reactor Coolant System is obtained The HPI pumps require a minimum flowrate of 34 gpm to prevent the pwmps from heating up. By evaluating the pump head curves and suction pressure, it was determined the HPI pumps would attain the 35 gpm injection rate at an RCS cold Jygt pressure of 1680 psig. Since the HPI pumps would be started within the range of 1695 to 1845 psig cold ljgt pressure, and the rate of depressuriza-tion is at least 3.4 psi per second,1680 psig will be reached anywhere from 4.4 to 48.5 seconds after the pumps are started.
4.0 Time until pump damage would occur Based on the information from the HPI pump manufacturer (B&W Canada, now Hayward Tyler), if the minimum flow of 35 gpm was not obtained, boiling will eventually occur in the HPI pumps which could cause damage to them. The vendor has stated that with zero pump flow the pump seal temperature will raise 170F per minute, and the pump would be damaged at a seal temperature of 230 F. Assuming that the pump started at an ambient temperature of 1220F (500C), it would take approxi-mately six minutes to damage the pump.
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ATTACH'4E!iT 1 TO LICE';SEE EVENT REPORT !!P-32-79-03 PAGE 2 OF 2 5.0 Summary For any actual RCS leak for which the HPI pumps are required, it would have 2 taken ati most 48.5 seconds af ter the pump was started to establish the mini-mum required injection. HPI pump damage would not occur until approximately six minutes without flow. The re fore , the HPI pumps would perform their intended safety function and would not be damaged if they were actuated with the recirculation line frozen.
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