ML19270G382

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LER 79-009/03L-0 on 790429:while Measuring MSIV Limit Switch Trip positions,10 of 12 Switches Were Set Greater than 10% of MSIV Closure.Caused by Lack of Precise Field Calibr of Exact Limit Switch Trip Point.Special Procedure Developed
ML19270G382
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 05/11/1979
From: Vahrenwald J
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19270G379 List:
References
LER-79-009-03L-04, LER-79-9-3L-4, NUDOCS 7906060245
Download: ML19270G382 (2)


Text

NiiC FORM 366 U. S. NUCLE AR REGULATORY CCMMISSION (7 7J) .

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NUYBER 63 63 EVENT DATE 74 75 HEPORT DATE 80 EVENT DESCRIPTION ANo PROBABLE CONSEQUENCES h o 2 l While measuring the MSlV limit switch trip positions during a weekend outaqe. 10 of thel go;3; [ 12 switches measured on 6 MSIV's were found to be set greater than 10% of MSIV closure.1 0 4 l These measurements were performed at the request of NRC Inspector G. Wright. The I o s l 10% closure settings were originally set at the factory prior to installation and l o e unit startup. Monthly MSIV closure scram functional testing has been perfarmed to l 0 7 l verify scram function operability. The remaining 2 MSIV's will be checked at a j o a i future outage of sufficient length. I 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUSCOOE 9

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i o l The need for prior precise field calibration of the exact limit switch trio ,n'nt had I

, , not been deemed necessary to be performed. A special procedure was developed to enable]

, , exact measuring of the switch trip position in the field. As-found and corrected g 3 3 l switch positions are attached. The switches were adjusted tog 10% closure and l gij,j [ functionally tested. [

7 8 9 . 83 ST S *.POWER OTHER STATUS iSCO HY DISCOVERY DESCmPTIGN i s W@ l0 l0 l0 l@l NA l lCl@l Test l A CTIVI TY CO TENT RELE ASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE 7

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