05000259/LER-1979-001-01, /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod

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/01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod
ML19270F310
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 01/31/1979
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19270F305 List:
References
LER-79-001-01T, LER-79-1-1T, NUDOCS 7902060235
Download: ML19270F310 (2)


LER-1979-001, /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod
Event date:
Report date:
2591979001R01 - NRC Website

text

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8 60 61 DOCKET NUMBE R 68 69 EVENT DATE 14 75 REPOR T DATE 80 EVENT DESCHIPTION AND PROBABLE CONSEQUENCES h lal2l lWhile pulling rods at the end of a refueling outage, the reactor scrammed due to high l lo tal flux actuating the IRM high-high neutron monitoring circuit. The reactor was approachF ing criticality in the B1 number 1 rod sequence. The estimated reactor period l

o 4 [o ig approached 5 seconds. Reactivity anomaly is reported in accordance with T.S. 6.7.2.a.4p o 6 There have been no previous occurrences. There was no hazard to the public health or 10171 i safety.

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33 34 35 36 J1 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS lilol The fast period was caused by withdrawal of a high reactivity worth rod.

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791 Technical Specification Involved None

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Reported Under Technical Specification 6.7.2.a.4 T! ate of Occurrence 1-18-79 Time of Occurrence 2328 Unit 1

Identification and Description of Occurrence:

Reactor scrammed due to high flux detected by the IRM neutron monitoring circuit.

Conditions Prior to Occurrence:

Pulling control rods to obtain criticality.

Action specified in the Technical Specification Surveillance Requirements met due to inoperable equipment. Describe.

None Apparent Cause of Occurrence:

Too rapil withdrawal of a high reactivity worth control rod.

Analysis of Occurrence:

Withdrawal of high reactivity worth control rods must be slow enough to allow full development of ensuing reactor periods.

Corrective Action

The fast period was caused by withdrawal of a high reactivity worth control rod.

The operator, following normal practice, allowed the rod to continuously withdraw since neutron monitoring instruments indicated the reactor to be far subcritical.

Operator action to reinsert the rod failed to reduce the period and resulted in a reactor trip. Administrative controls have been implemented to require the fiist Failure Data: rod in a RWM grbup to be notched before criticality.

Precautions pertaining to high rod worths have been inserted into operating instructions.

None Tennessee Valley Authority - Browns Ferry Nuclear Plant