05000259/LER-1979-018-01, /01T-0:on 790823,during Insp,Restraints on Certain Core Support Structure Sys Found Inoperable.Caused by Pipe Vibration &/Or Improper Installation During Const.Restraints in Units 1,2 & 3 Being Inspected.Rept Will Be Issued

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/01T-0:on 790823,during Insp,Restraints on Certain Core Support Structure Sys Found Inoperable.Caused by Pipe Vibration &/Or Improper Installation During Const.Restraints in Units 1,2 & 3 Being Inspected.Rept Will Be Issued
ML19253B032
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 09/06/1979
From:
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19253B030 List:
References
LER-79-018-01T, LER-79-18-1T, NUDOCS 7909140398
Download: ML19253B032 (2)


LER-1979-018, /01T-0:on 790823,during Insp,Restraints on Certain Core Support Structure Sys Found Inoperable.Caused by Pipe Vibration &/Or Improper Installation During Const.Restraints in Units 1,2 & 3 Being Inspected.Rept Will Be Issued
Event date:
Report date:
2591979018R01 - NRC Website

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EVENT DESCRIPTION AND PROS ABLE COMEQUENCES h [TT"O l With unit in normal operation at 95% power, inspections were'made in accordance with__]

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IE Bulletin,79-14. During this inspection it was found that restraints on certainCSSCl 6

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cAuse r,cscH@ TION AND COqnECTivE ACTIONS h l Pipe vibration and/or improper installation during construction caused the inoperabili-l j

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Tennessee Valley Authority Form BF-17 Drr>..ns 1 tery Nuclent vlant DF 15.2 1/!0/79 LER SUPPLEMENTAL INFOIDIATION f 5FitO-l20- 259_/_7918_ Technical Spectfication Involved NA Hrported I'nder Technical Specification _6.7.2.a.9 Dar.. cf Occur renc.

8/23/79 Ttme of Occurrence 3:45 p.m, Unit 1

identif" sticn and Descr;ption of Occurrence: During inspections in accordance with IE Bulletin 79-14, PHRSW restraint R-8 was found to be inoperable in that of the four bolts required, the nuts on two through-bolts had fallen off and two through-bolts were missing.

Conditions Prior to Occurrence:

Unit 1 at 1045 MWe.

Unit 2 at 1095 MWe.

Unit 3 at 0 MWe - Maintenance Outage Action specified in the Technical Specificcticn Surveillance Requirements met due to tnoperable equioment. Describe.

None App <trent Cause of Occurrence:

Pipe vibration and/or improper installation during construction apparently caused the two nuts to loosen and fall off. The missing through bolts were apparently not installed during constructirn.

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Restraint R-8 has been repaired to design specifications. EN DES performed an evaluation and supplied a list of 41 similar restraints in units 1, 2 and 3 to be inspected. Of these,31 have been inspected and of those inspected R-5, R-18, R-19,and R-22 on the RHRSW system. required repair work. A followup report will be issued at a later date.

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  • Revision :

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