ML19211A264

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LER 79-039/03X-1:on 790527,during NRC Audit of Category E Valve Positions in Mode 3 Operation,Low Pressure Safety Injection Discharge Header Valve 2SI-5091-3 Found Closed. Caused by Operator Error.Valve Modified
ML19211A264
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 12/06/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19211A258 List:
References
LER-79-039-03X, LER-79-39-3X, NUDOCS 7912170281
Download: ML19211A264 (1)


Text

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.. UPDATE REPORT Previous Report Date 6/26/79 NRC F ORM 3t,4 U. S. NUCLE AR RE GL'L ATORY COMMi$$ ION f7 77)

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  • VENT DESCRIPTION AND PROBA8LE CONSEOVENCES h ITTTl I During an NRC audit of Category "E" valve positions while in Mode 3  :

o Loperation, Low Pressure Safety Injection Discharoe Header valve i o . I 2SI-5091-3 was discovered to be in the closed position. The redundant I r8 FO 1 flow path, thru 2CV-5091, was operational; therefore, full Low Pressure i FETin Injection flow would have been available if required. There have been i o , i no similar occurrences. This occurrence is reportable per T.S.6.9.1.9.c.

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