ML19209B299

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LER 79-028/03L-0:on 790904,hydraulic Snubber Located on Main Steam B Atmospheric Dump Valve Found Inoperable.Caused by Broken Snubber Reservoir.Snubber Replaced
ML19209B299
Person / Time
Site: Millstone Dominion icon.png
Issue date: 10/01/1979
From: Crockett J
NORTHEAST UTILITIES
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19209B297 List:
References
LER-79-028-03L-01, LER-79-28-3L-1, NUDOCS 7910090466
Download: ML19209B299 (1)


Text

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HEPOFlT DATE B3 EVENT DESCHIPTION AND PROD AOLE CONSEQUENCES h o ,, l During routine power operation, a hydraulic snubber located on the B main steam I o 3  ; atmospheric dump valve was found to be inoperable. The fluid reservoir had been [

g 4  ; broken off the snubber. The faulty snubber was removed and a replacement unit [

o 3 ; ins tal led . Facility operation was in accordance with Technical Specification 3.7.8.1. [

g g  ; Snubber - Hanger 405388, ITT Grinnell, Fig. 201, 2 1/2 inch bore x 5 inch stroke. I o 7 I I O 8 l  !

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[i i a l The snubber reservoir was inadvertently broken off by contract insulators during i ii i [ reinsulation of a steam line in the vicinity. Snubber replaced. The periodic snubber I

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