ML19207B972

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LER 79-037/01X-0:on 790828,during Surveillance Test,Valve SI-4145-MOV Was Open & SI-4143-MOV Was Shut,Causing ECCS Subsys & Containment Spray Sys to Become Inoperable.Caused by Personnel Error
ML19207B972
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 08/28/1979
From: Davis S
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
References
LER-79-031-01X-02, LER-79-31-1X-2, NUDOCS 7909060259
Download: ML19207B972 (1)


Text

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LICENSEE EVENT REPORT CONTROL BLOCC l l l l -l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 3 6 lo t i 5 9

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DATE E 60 61 DOCKET NUMBER EVENT DESCRIPTION AND PRCB ABLE CONSECuENCES h o . :1 1 At 0600 durino nerfomance nf a curvaillanc, test, the operator discovered I oi3  ; that SI-4145-MOV. (12 Header Containment Sumo Valve) was ooen and SI-4143-TV I

,1 ,, l(12 Header UT Suction valve) was shut, causing or.a ECCS subsystem and one 1 at3 i containment soray syster to become inocerable (T.S.3.5.2 and 3.6.2.1) . The I Of6 l Operator ifTiediately reDCsitioned the valves to their DroDer Dosition. The I _

joi7; ] redundant contain. scray and ECCS systems remained ocerable durine the event. I a -i iThis is not a- rettetitive occurrence. j

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[ g g 43 lNlg 42 lZl@ lVl0l8l5lg 43 44 47 CAuSE DESCR!FTION AND CC ARECTivE ACTIONS i , , , i 10n 8-27-79, the Control Room Goerator inadvertently shut SI-41a3 u0V while 1

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, , (A0V. The immediate corrective action was to shut SI-4145-W'V and oren SI 4143- 1

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