05000251/LER-1978-007-03, /03L-0 on 780710:for 11.5-h,condensate Storage Tank Level Was Below Tech Spec Limits.Caused by Condenser Leaks in Both Units.Water Treatment Was Shut Down & Storage Tanks Filled

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/03L-0 on 780710:for 11.5-h,condensate Storage Tank Level Was Below Tech Spec Limits.Caused by Condenser Leaks in Both Units.Water Treatment Was Shut Down & Storage Tanks Filled
ML17338A837
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 08/07/1978
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17338A836 List:
References
LER-78-007-03L, LER-78-7-3L, NUDOCS 7907110412
Download: ML17338A837 (4)


LER-1978-007, /03L-0 on 780710:for 11.5-h,condensate Storage Tank Level Was Below Tech Spec Limits.Caused by Condenser Leaks in Both Units.Water Treatment Was Shut Down & Storage Tanks Filled
Event date:
Report date:
2511978007R03 - NRC Website

text

NRC FORM 344 jT 77)

LICENSEE EVENT REPORT U. S NUCLEAR REOULATORY COMMI.

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$0 EVENT OESCRIPTION ANO PROBASLE CONSEQUENCES Qlo er tion a

d for a eriod of about 11.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> the Conder

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sate Stora e Tank contained less than the 185,000 allons re uired by a

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roximatel 162 000 allon P blic health and safet was not affected.

Re ortable Occurrence 250-78-4 was the onl revious occurrence of this t e.

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re enerate exhausted cation resin beds..

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resulted in tank levels less than the T.S. 3.8.1.c minimum.

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REPORTABLE OCCURRENCE 251-78-7 LICENSEE EVENT REPORT PAGE TWO Additional Event Descri tion and Probable Conse uences The only effect of having a reduced volume in the tank is illustrated in FSAR, Figure 9.11-1.

Additional Cause Descri tion and Corrective Action Regeneration of the resin beds required 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />, after which filling the Condensate Storage Tanks was commenced.

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